Safe Room HEPA Filter - The Preparedness Podcast
Transcription
Safe Room HEPA Filter - The Preparedness Podcast
Safe Room Fan September 6, 2004 Using the information based on a “Fan in a Can” Safe Room filter from (alpharubicon.com), I set out to create my own safe room fan/filter unit. The result was a successful creation of a fan assembly and safe room test. Here’s how I did it: The materials needed for this fan assembly: 1- Squirrel cage fan from Grainger, part number 4C447 (2011 Note: This fan is now discontinued, but pulled 135 CFM @ 0.500-In. Static Pressure; the Dayton 7063-3277 is an exact duplicate) 1- Power supply cord, 12 feet, from Grainger 2 – Cable/cord connectors 1- 30mm ammo can w/ good gasket, inside dimensions: 8.75” x 17.25” x 14” 1- Tube silicone sealant 3- Wire nuts, 16 gauge 6 inches of wire 4 – bolt assemblies, 1/2 inch length (bolt, nut, lock washer, flat washer) 1 – HEPA filter, 99.97% efficiency (I used a Holmes HAPF 600) I ordered the fan from Grainger, along with a power cord because one does not come with the fan. I also ordered 2 cord connectors to provide stress relief for the wiring connections. Construction The green wire on the power cord goes to the ground connection on the fan, I had to use a short length of wire for this; the other two wires can go to either fan lead, as it’s an AC motor. Once this was wired up, I plugged it in for a test. I used wire nuts so that field repairs could be effected easier than if I had soldered the connections. I used one cable/cord connector on the fan housing (there’s a pop out on the fan housing for it) for stress relief. One side of the fan’s squirrel cage was higher than the other and was scrapping the intake housing. Closer inspection showed that the motor was not mounted evenly. I removed the intake cowl and, using a Torx driver, I loosened the cam nut and removed the cage from the shaft. I adjusted the fan mounting screws so that the motor was more parallel with the housing, but it was still canted. However, the shaft was long enough to provide plenty of adjustment on where the cage sat, so I just lowered it enough so that it didn’t scrape the housing. Placing the fan in the location where it was going to be in the ammo can, I marked the holes for the bolts with a marker. I drilled two holes and then lined up the fan on the outside to mark the other two mounting holes. This was necessary because I wasn’t able to access the other holes to mark them. This worked out fine, as the fan’s mounting frame is symmetrical. Once the holes were drilled; I did a quick mounting check with the bolts to ensure that everything lined up properly. Since everything lined up, I grinded down the holes to remove burrs and moved onto the next step of cutting the exhaust hole. I drew a line from caddy-corner holes so that an X was formed. This X allowed me to center the cardboard template I used to outline where the hole was going to be cut. (Note: The only tools I had available to me were a drill and a jigsaw. There are other ways of accomplishing cutting in metal, but I used what I had.) I drilled a half-inch hole and using a jigsaw and a metal-cutting blade, cut out the square hole for the fan exhaust. After a quick check to make sure the hole was the size I wanted, I grinded the edges to remove burrs. I made the hole of the exhaust slightly smaller than the fan’s output for two reasons. First, I didn’t want the hole to be too big and have problems making an airtight seal, and second, I wanted a small lip in order to attach duct tape to. Cutting the hole for the filter was next. The only filter I found that was worth using was a 99.97% HEPA filter from Holmes. Not only was it a 99.97% efficiency, but it was also rated to last 12-18 months and had a built-in rubber gasket on the bottom that would aid in creating an air-tight seal. It’s larger than I wanted, but with limited availability in filter sizes, I decided to see if I could make it work. The problem was that the filter was so large that I would need to remove a portion of the support brace on the side of the ammo can in order to have room to tape the filter to the can. This caused some concern, as I wasn’t sure if it was possible to remove this without compromising the integrity of the airtight seal. In the image below, you can see two outlines, the inner outline is the hole size that needed to be cut out and the outer outline is the size of the filter. I figured that I would need at least an extra inch of support removed in order to have enough space to effectively tape the filter to the can. Looking at the support brace more closely, I found that it was held in place by four pairs of spot welds, and I hoped that it also wasn’t glued into place. Drilling 4 holes at each corner for the jigsaw blade, I proceeded to cut the hole for the intake. Once the hole was cut, including the small bit of support brace that needed to be removed, I was able to see if the support brace was glued; luckily it was not. Now that I knew that the support was only held in place with only spot welds, it made the prospect of removing the part that I didn’t want more likely. But, the trick was to do it without cutting through the skin of the ammo can. I tried using the jigsaw, but it only took two seconds to determine that it wasn’t going to work. I ended up pulling out my Dremel tool and used a cutting wheel to delicately cut through the support without damaging the ammo can itself. I used a screwdriver to lift the support away from the ammo can enough so that I could cut it without cutting the can. Once this was all done, I grinded down all the edges and used a wire brush in the drill to clean off the gunk and rust that was under the support. You can see the result in the image below. The diagonal line that is in the upper right corner of the hole is a jigsaw cut I made to break the spot weld. The cut was still well within the outline of the filter housing, so the integrity was not compromised. The next thing that had to be cut into the ammo can was the opening for the power cord. I didn’t have a drill bit large enough to make a hole large enough for the cable/cord connector, so I drilled a hole for the jigsaw blade and then chewed away metal to enlarge the hole. Once the hole was almost big enough, I used the conical grinding stone on the drill to enlarge it just enough so that the connector would fit. Once finished, I again grinded the edges to remove any burrs. After all of this was completed, I washed the entire ammo can to make sure that it was free of dirt and any oily residue that might be present; I didn’t want to take any chances with the airtight seal. Once the ammo can was dry, I installed the cord connector and then removed the wires from the fan. This allowed me to pass the cord through the small hole in the connector. Leaving enough slack in the cord, I reattached the wires to the fan and tightened the connector. Just before mounting the fan, I put a liberal amount of silicone around the face of the mounting plate of the fan and bolted it to the can. At this point the unit was assembled. All that remained was to silicone around the power cord coming into the can, both inside and outside the can. At this point, I let the silicone cure overnight before testing the unit. The finished unit: Testing Now that the unit was fully assembled, it was time to test it. In order to do so, I had to not only attach the filter, but also create the entire safe room in order to test whether it was going to provide enough positive pressure in the area that I had selected as the safe room. First though, I needed to attach the filter to the fan assembly. Using Nashua 324A foil tape, I taped the filter over the intake hole, making sure that the tape had a good seal all around. Once that was in place, it was ready to go. Before bringing it up to the safe room, I plugged it in again to see what the airflow was like with the filter on. The amount of air that it was pushing out was dramatically reduced. The area that I had selected to be the safe room of the house was the master bedroom, master bathroom and master closet. I chose this area of the house for the logical reasons of it having a bed, toilet, sink, storage space and it was on the second floor. There was only one other area that I could have used as a safe room, but it was vastly smaller and didn’t offer the same advantages as the master rooms. The total cubic feet of the selected area is 4,296. I was a little concerned that the fan wouldn’t be able to pressurize this size of area, so testing was the only way to be sure. One of the reasons I selected this area was that I could seal off the closets to make a smaller area to pressurize, if needed. The entrance to the master bedroom has “French Doors,” or double doors, that open into the bedroom. The only way to seal off the room and still be able to get in and out would be to take off one of the doors. So, off it came. After the door was off, I cut the plastic and taped it around the door. I also taped it along the floor, but I did not tape a large section of it as I needed to go in and out of the safe room for testing purposes. My plan was to tape it only if the room failed to pressurize. I placed the fan assembly with its taped on filter just outside of the plastic and cut a hole in the plastic where the exhaust was and taped it into place. I then plugged the fan in and crossed my fingers. I thought it was doing great as the plastic was bowing out from the room nicely when I realized that the air conditioning was running. So, I turned that off and went back inside the safe room. At this time, I had not put plastic over any of the air or fan vents in any of the master rooms. I had wanted to see how well the fan would pressurize before sealing these. Without any vents sealed, the pressurization was minimal; it took several minutes for the plastic to go from a neutral to slightly taut. I figured that this wasn’t good enough, so I started sealing vents. My thought was that if I had sealed all the vents and still had poor pressure, I’d have to tape up the rest of the plastic around the door as I assumed that it was leaking quite a bit of air. There are 3 main vents in the master bedroom itself, two HVAC vents and one air return. I sealed these and noticed a dramatic improvement in the pressure on the plastic. At this point I had an idea hit me and I turned on the bathroom fan … the pressure on the plastic immediately ceased and when I turned the ceiling fan off, the pressure immediately returned. This was enough to convince me that I had enough pressure to accomplish the job. Once all of the vents were sealed and the plastic around the door was fully taped up, I would have a fully pressurized safe room. The only thing left to do was conduct the “vanilla test.” After placing an open bottle of vanilla immediately next to the filter, I re-entered the safe room and starting sniffing. The motor itself made the air smell ‘electrical,’ like the smell that comes from the KitchenAide mixer when I’m mixing dough, so it was tough trying to determine exactly what smells I was detecting. After about 5 minutes of not smelling vanilla, I reached under the plastic and brought the bottle inside and placed in front of the exhaust so I could see what it would smell like mixed with the motor smell. The vanilla was quite easy to discern, therefore, there was none coming fan and filter assembly! Yea!! I let the fan run for four hours and then checked it. The motor was hot, but nothing else; the air coming out of the unit was cool, the ammo can was cool, the power cord was cool, and since the motor has a automatic thermal shutdown feature, it must have been running within normal tolerances. While I let the fan run, I measured and precut all of the plastic that I would need to seal up the safe room. Once I turned off the fan, I found that I was able to store everything that I’d need to create the safe room: plastic, filters, foil tape, duct tape, and extra plastic sheeting. With the successful conclusion of this test, I now know for a fact that the fan will pressurize my safe room and keep my family safe! Afterward: about the only thing that I’d do different if I built another unit, would be to rotate the intake hole 90 degrees so that the intake of the fan had a more direct shot through the filter.