bmw r50 for restoration
Transcription
bmw r50 for restoration
Allan‟s BMW R50/2 Restoration (Abridged) BMW R50/2 RESTORATION PROJECT Allan Bester December 2013 Rev 1.1 24 December 2013 Rev 1.1 1 Allan‟s BMW R50/2 Restoration (Abridged) BMW R50/2 RESTORATION PROJECT TABLE OF CONTENTS Page ACQUISITION ……………………………………………………………………………………………3 ACKNOWLEDGEMENTS ………………………………………………………………………………4 PUBLISHED SPECIFICATIONS FOR BMW R50/2 …………………………………………………5 SPECIFICATIONS FOR MY BMW R50/2 …………………………………………………………….7 RESTORATION LOG ……………………………………………………………………………………13 DEFECTS BEFORE …………………………………………………………………………………….109 IMPROVEMENTS & KNOWN DEFECTS (AFTER) ………………………………………………….110 PARTS FABRICATED …………………………………………………………………………………..111 PARTS PROCURED ……………………………………………………………………………………115 STAINLESS STEEL PARTS ……………………………………………………………………………120 TOOLS PROCURED ……………………………………………………………………………………122 NOTES …………………………………………………………………………………………………….123 LESSONS LEARNT ………………………………………………………………………………………127 LINKS ………………………………………………………………………………………………………128 REFERENCES ……………………………………………………………………………………………128 RECORD OF EXPENDITURE ………………………………………………………………………….130 24 December 2013 Rev 1.1 2 Allan‟s BMW R50/2 Restoration (Abridged) ACQUISITION ADVERT: VMC‟s Kickstart newsletter August 2007: “BMW R50. Complete, for restoration R10 000. Contact Jimmy D*****” CONTACT: Called Jimmy on Monday 1 October 2007 on his cellphone. Arranged to see the bike on Wed 3 October around 16h00 with Ian Holmes. DETAILS: Bike was 60% assembled, balance in boxes. Jimmy assured me the bike is COMPLETE. New set cables made up, new sparkplugs (NGK B7ES), ignition key, speedo & gauges, tank knee pads, BMW roundels for tank, foot rests, side stand, original (rusted) crash bars. PAPERS: None MODEL/YEAR: +- 1961 - 1969 SERIAL #: Frame # = 622 372 (R60/2) 1961 Engine # = 648 460 (R50/2) 1969 (Casting date on heads = 1968) DESCRIPTION & SHORTCOMINGS: Earle‟s forks, 6 volt, ex-Durban, tyres = Yokohama, Front rim = steel. rear rim = alloy, colour = black, petrol tank has dents & filler taped closed, no accident damage visible. Frame and tank painted (needs to be redone), stainless steel header pipes made up (with nuts/collars). Many parts dismantled completely, surface rust, non-original rear tail light, number plate light lens broken, spare barrels pitted with rust, seat needs to be reupholstered. SPARES: Seat, handle bars, c-spanner, 4 x loose barrels (unusable), 5 x pistons (unusable), extra Bing carb, new headlight, extra tank knee pad W/SHOP MANUAL: No, but BMW twins Restoration book (Motorbooks International) by Roland Slabon included, no owners manual PRICE: On 9 October 2007 telephonically mutually agreed to R7000 all inclusive. ACTIONS: Internet transferred kR7 on Thursday 10 Oct, Receipt from Jimmy (full & final settlement. Collected bike on Fri 12 October 2007 24 December 2013 Rev 1.1 3 Allan‟s BMW R50/2 Restoration (Abridged) ACKNOWLEDGEMENTS This is to acknowledge the significant contributions of selected individuals and organisations in the restoration of my BMW R50/2, of which I am justifiably proud. Ian Holmes, for persuading me to become a member of the Vintage Motorcycle Club (VMC) and thereby gaining access to people with a wealth of knowledge and skill without which this restoration would not have been possible. The origin of the restoration project was advertised in the VMC “Kickstart” newsletter, and it was also Ian who accompanied me to see the bike at the seller‟s premises and who inspired me to tackle this enjoyable task. Jan Cornel, an absolute gentleman of great technical skill and experience who provided parts, used and new, as well as much technical advice, assistance and access to some BMW special tools, such as the jig used to ream the small-end bushes in the conrods in situ. Mike Lester, for putting up with my numerous persistent phone calls, for his friendship and inspiration, his knowledge and his outstanding spray painting and pinstriping skills. Also for introducing me to Al Gibson, Charlie Hamer and Roly Tilman, of whom more later. Roly Tilman, for his depth of knowledge, his inspiration and especially his generosity with used parts for my restoration project. Truly a philanthropist of note! Al Gibson, for his willingness to share his unsurpassed and irreplaceable technical knowledge of the BMW marque, his decades of experience in engine preparation, and for his inspiration to “do the job right”. Charlie Hamer, for his awesome welding skills at a very reasonable price. Rian Emerich, for his willingness to assist in my project with sand and bead blasting of numerous rusty bits for no monetary reward, and for his inspiration and cheerful enthusiasm. Zane Mannell, for his friendship, his sound advice, some special BMW tools from his deceased father, unflagging inspiration, and my “sounding board” at all times. Bill Speight, for providing restorers of 1950s and 1960s BMW motorcycles with access to locally manufactured quality rubber parts at very reasonable prices. Classic Motorcycle Club (CMC), for access to Bill Speight‟s rubber parts for BMW‟s, used BMW parts, as well as copies of BMW workshop manuals and service bulletins (thanks, Bob Harpin). Also for the introduction to people like Hennie van Zyl, Derek Marsden, and one of the friendliest guys around, Pierre Cronje! Jeff Talbot in Cape Town (referred by Roly Tilman) for very reasonably priced stainless steel silencers for my restoration project. Ivan Snell, a long-suffering friend, for his vast experience, technical knowledge and sound advice. Suppliers such as African Electroplating, Sheffield Electroplating, JKM (fasteners and engineering supplies), Classic Auto Trimmers (upholstery), Randburg Automotive Paints (paints), Uli‟s Motorradladen (high quality substitute BMW parts), and many more. The Internet, specifically the “Yahoo Slash2 Group” for an entire world of knowledge, experience and advice on restoring Slash2 BMW motorcycles. My long-suffering family, who had to put up with my absolute obsession with my mid-life crisis project for more than two years of nights, weekends, holidays and any other time that I could spare. It is no exaggeration to state that this project would not have been completed in the time achieved and of the quality attained without the contributions and support of the individuals and organisations mentioned above, as well as those I have not acknowledged by name. My thanks and appreciation to all. 24 December 2013 Rev 1.1 4 Allan‟s BMW R50/2 Restoration (Abridged) PUBLISHED SPECIFICATIONS FOR BMW R50/2 Engine Internal Designation 252/2 Motor Type Four-stroke, two cylinder, air-cooled flat twin Bore x Stroke 68mm x 68mm (2.67” x 2.67”) Displacement 493 cc Max Power 26 hp at 5800 rpm (35 hp at 7650 rpm for R50S) Compression Ratio Valves Carburation System 7.5 : 1 (with later pistons), 9.2 : 1 (with R50S pistons) 125–147psi (8–10 bar) sea-level = 106-125psi (7-8 bar) 1700m asl OHV 2 x carburettor Bing 1/24/45 - 46 or 1/24/131 - 132 or 1/24/149 - 150 Engine Lubricating System Forced feed lubrication Oil Pump Gear pump Power Transmission Clutch Single dry plate, diaphragm spring Number of Gears 4 Shifting Foot shifting Gearbox Ratios 4.17 / 2.73 / 1.94 / 1.54 Rear Wheel Ratio 1 : 3.18 Bevel/Crownwheel 8 : 25 (after 1961) Electrical System Ignition System Magneto ignition Generator Bosch LJ/CGE 960/6/1/1700 R5 Spark Plugs Bosch W240 T2 (= long reach) W260 T2 for R50S NGK B7ES NGK B8ES (colder) for R50S gap = 0.6mm Bosch W5CC 24 December 2013 Rev 1.1 Bosch W4CC 5 Allan‟s BMW R50/2 Restoration (Abridged) Chassis/Frame Designation R245/1 Frame Double loop steel tubular frame Front wheel suspension Long swing arm with suspension units and oil pressure shock absorbers Rear wheel suspension Long swing arm with suspension units and oil pressure shock absorbers Wheel rims Deep bed 2.15B x 18” (with sidecar, rear 2.75C x 18), 40 spokes Tyres, Front 3.50” x 18” Tyres, Rear 3.50” x 18” (with sidecar = 4” x 18”) Brakes, Front Drum brake 200mm / 7.87” diameter duplex full hub Brakes, Rear Drum brake 200mm / 7.87” diameter simplex full hub Dimensions/Weights Length x Width x Height 2125 x 660 x 980 mm (83.66” x 25.98” x 38.58”) Wheel Base 1415 mm / 55.66” (with original sidecar 1450 mm / 57.08”) Fuel Tank Capacity 17 litres / 3.73 gal / 4.49 gal US Unladen Weight with Full Tank 195 kg / 429 lb (320 kg / 704 lb with original sidecar) Idle/Riding Noise 82/76 phon (from June 1967: 72 dB (A), 84 dB (A)) Load Rating 360 kg / 792 lb (with original sidecar, 600 kg / 1321 lb) Fuel Consumption Approx. 5.1 litres per 100 km / 55 mpg / 46 mpg US Oil Consumption Approx. 0.5 - 1 litre per 1,000 km Top Speed 140 kph / 87 mph 24 December 2013 Rev 1.1 6 Allan‟s BMW R50/2 Restoration (Abridged) SPECIFICATIONS FOR MY BMW R50/2 Frame Serial No: 622372, stamped on plate screwed to steering head, and stamped on side of steering head, for R60/2. Other numbers stamped on frame = BSI SIUS on RHS upright and 51.51.813.03 on LHS upright of rear swing arm mounting points Engine Serial No: 648460, stamped on RHS of engine casing above cylinder for R50/2. Casting date for cylinder heads = 1968 Carburettors: Bing 1/24/132 (R/H) and 1/24/131 (L/H), main jet #105, idle jet #35, needle jet #1308, with “lever top” float chamber covers (after August 1967), jet needle = #46-255, clip position = 3 (from top), 7g floats Fitted 120 main jets (see Service Info 257) Wheels: Before, Front = steel rim (not BMW) Rear = BMW OEM alloy rim After, Front = BMW OEM alloy rim Rear = BMW OEM steel rim Tyres: Before, Front = Yokohama 3.00 x 18”, tube = Yokohama Before, Rear = Yokohama 4.00 x 18”, tube = Bridgestone After, Front = Metzeler ME22, 3.50” x 18”, new Viper tube After, Rear = Metzeler ME22, 3.50” x 18”, new King Tube Air Filter Element: Purolator PM 1042 Wheel Bearings: 30204 taper roller (front & rear). Front FAG bearings replaced with DYZV, one rear NSK bearing replaced with DYZV. Front Hub seals: Outer = TC 25 x 35 x 7 fitted, and felt seal inner was fitted (replaced with TC 25 x 38 x 7 Nitrile oil seal). Use 25 x 38 x 6mm inner Rear Hub oil seals: Outer = TC 24 x 35 x 6 was fitted, & TC 25 x 38 x 7 inner fitted. Use 25 x 38 x 6mm inner. Turned new top hat spacer to fit new outer oil seal = 25 x 35 x 7 Swing Arm oil seals: TC 22 x 40 x 8 (fitted front & rear) (spec = 22 x 40 x 10) Front Spring Length: 285mm Swing Arm Bearings: 30203 taper roller (front & rear). Rear bearings replaced Gear lever oil seal: 15 x 24 x 7 (used double lip type, Nitrile) Gearbox input shaft seal: 30 x 40 x 7 (Viton) Gearbox output seal: 36 x 54 x 7 (Nitrile) Engine rear main seal: 52 x 72 x 10 (original was Kaco Silicon). Replaced with Viton. Engine Oil: SAE 40, sump capacity = 2 litres (fill only to bottom of threads) Drive shaft Oil: SAE 40, capacity = 120 cc Bevel drive Oil: SAE 90, capacity = 150 cc (fill only to bottom of threads) Gearbox Oil: SAE 40, capacity = 0,8 litre (fill only to bottom of threads) Generator: Bosch G7V.15A17 24 December 2013 Rev 1.1 (None supplied with the bike) 7 Allan‟s BMW R50/2 Restoration (Abridged) SPECIFICATIONS FOR MY BMW R50/2 Steering head bearings: As purchased = 2 x SKF 355243 ball bearings, 23 balls each (one was missing), surfaces rust pitted, OD = 51mm, ID = 34mm, balls 5.5mm. Replaced with 51W/34W taper roller bearings from Ed Korn (USA) Spark Plugs: NGK B7ES = 19mm thread reach for LK heads, gap = 0,6mm Cylinder Heads: Improved “LK” heads fitted, with rotating valves (cast in 1968) Points Gap Spec: 0.35mm – 0.4mm Battery: Original Spec = 6V 8Ah, B49-6 (LxWxH = 90mm x 82mm x 160mm) Oil Drain/Fill Plugs: M14 x 1,5, M10 x 1, gaskets = steel/asbestos (I fitted solid copper) Tyre Pressures: Front = 170 kPa Engine mounting bolts: M12 x 1.5 (Fine thread), 19mm AF Valve diameter Specs: Inlet = 34mm, Exhaust = 32mm, stems = 7mm nominal Pushrod dimensions: Length = 242mm Valve Clearance Specs: Inlet = 0,15mm (0.006”) Actual = 0.2mm (inlet) Clutch disk spring: Reinforced version part number = 00 70 183 (red -) Clutch Backing Plate: Later type from /5 fitted with webs on bell housing ground away to clear shallow Allen cap screws. This is the preferred type. Has genuine BMW part number = 12320772 Clutch Plate: F&S Transmission shaft: End play = 0.00 + 0,1mm (reduced from 1967) Final drive ratio: 25 : 8 (as specified after 1961) Final Drive studs: M8 x 1 thread on final drive studs for swing arm mounting Driveshaft bolts: 12-point, 10mm AF with spring washers Brake shoes: Front = riveted, Rear = bonded (Front & rear replaced with softer bonded linings 4mm thick) Camshaft Bearings: 2 x 6203 (was SKF), replaced Generator Bearing: 1 x 6004 (was SKF), replaced Cylinder base gaskets: Aluminium = 0,5mm (Fitted new gaskets) Magneto journal oil seal: 25 x 35 x 7 (Kaco) – replaced with Viton Generator hub oil seal: 20 x 32 x 7 (Kaco) – replaced with Viton Kickstart Oil Seal: 17 x 28 x 7 (Used double lip type, Nitrile) Cylinder Bore Diameters: 1st oversize = 68.5mm nominal. Measured 68.51mm (68.52) at tops of bores, and 68.53mm in middle of bores 24 December 2013 Rev 1.1 Rear = 190 kPa Diameter = 7mm Exhaust = 0,2mm(0.008”) 0.25mm (exhaust) (Jan Cornel specs) 8 Allan‟s BMW R50/2 Restoration (Abridged) SPECIFICATIONS FOR MY BMW R50/2 Pistons: High compression = 68,42mm for R50S, 1st oversize, spec clearance = 0,08mm, measured clearance = 0.1mm. Skirt diameter = 68.395mm on both pistons Rocker arm end play: LHS = 0.2mm Old Piston Gaps: Ring Old Ring Clearance: End Groove Spec = 0.01mm – 0.02mm Top ring gap ½” below top of bore = 0.55mm LHS and 0.58mm RHS, Top ring gap ½” above bottom of bore = 0.6mm LHS and 0.65mm RHS 2nd ring at top of bore = 0.8mm. Spec = 0.25 – 0.4mm (new) Measured 0.05mm top & middle grooves (Spec = 0.07 – 0.1mm) Top ring gap 13mm below top of bore = 0.40mm LHS cylinder New Piston Ring End 2nd ring gap 13mm below top of bore = 0.40mm LHS cylinder Gaps: Oil ring gap 13mm below top of bore = 0.45mm LHS cylinder New Piston Dimensions: Ring Top ring width = 2.92mm – 2.95mm, 1.98mm – 1.984mm thick 2nd ring width = 3.02mm – 3.03mm, 1.984mm – 1.986mm thick Oil ring width = 2.988mm – 2.99mm, 4.988mm – 4.99mm thick Wrist/Gudgeon pins: 20,0mm diameter, no discernable wear, C20 wire snap rings Crank Bearings: 2 x 6207 (old = NSK, replaced with new = NTN) Flywheel lateral run out: Spec = 0,1mm (0.004”) maximum Actual = 0,2mm RHS Exh Outer/In = 42.38/35.2mm, RHS Inlet Outer/In = 42.0/35.5mm Old Valve Spring Length LHS Exh Outer/In = 42.35/35.5mm, LHS Inlet Outer/In = 42.37/35.5mm (Free): Spec: Outer = 42.3mm Inner = 37.5mm New Valve Spring Length Inner = 37.5mm Outer = 43.5mm (Free): RHS Exh Out = 35.7mm LHS Exh Out = 35.5mm New Valve Spring Length RHS Inlet Out = 34.6mm LHS Inlet Out = 34.8mm (Installed) Spec = 30.5mm for inner, and 34.0mm for outer springs Could have fitted shims under springs (0.5mm inlet, 1.5mm exhaust) LHS Exh = 6.926mm LHS Inlet = 6.94mm Old Valve Stems: RHS Exh = 6.92mm RHS Inlet = 6.93mm Spec = 6.95mm – 6.935mm when new New Valve Stems: Exh = 6.935mm Valve Stem Play in Guide RHS Exh = 0.45/pi = 0.14mm RHS Inlet = 0.15/pi = 0.05mm LHS Exh = 0.5/pi = 0.16mm LHS Inlet = 0.2/pi = 0.064mm Spec = 0.04 – 0.07mm (or 0.050 – 0.085mm) Old Valve Guide bores: RHS exh = 7.20mm RHS inlet = 7.07mm LHS exh = 7.22mm LHS inlet = 7.07mm Spec = 7.005mm max when new (use 7mm K7 reamer) 24 December 2013 Rev 1.1 9 Allan‟s BMW R50/2 Restoration (Abridged) SPECIFICATIONS FOR MY BMW R50/2 Valve Guide Dimensions: New guide OD = 13.05mm ID = 6.96mm before reaming Old guide OD = 13.05mm New guide L = 43.0mm (8,5mm) Old guide L = 50.0mm (15,9mm) For next rebuild use 13,10mm OD valve guides Interference fit spec = 0,03 – 0,05mm (heat head to 200 deg C) Old Valve Seat Widths Measured about 2mm for all valves before refurbishing Spec = 1,5mm for inlet valves and 2.0mm for exhaust valves (or 1,5mm for R50S) Eccentricity spec < 0,03mm Timing Gear Set: -2 (stamped on top of main engine casing) Conrod Big-End Lateral RH = 0,15mm Play: Spec = 0,07 – 0,10mm LH = 0,25mm Crank Main Bearing Front = 35,0mm Journal Diameter: Spec = 35,0mm Rear = 34,97mm Used Ritelok RT20G retainer Exhaust Headers: Supplied with fabricated s/steel headers & fabricated s/steel nuts Also supplied with one original header and damaged nut Fitted stainless steel headers from Powerflow (Durban) OD = 35mm (spec) Exhaust Silencers: Metac s/steel (supplied with the bike) Purchased new s/steel silencers from Jeff Talbot (Cape Town) Silent Blocs: 4 x Front = OD = 22mm, ID = 10mm, L = 16mm (replaced) 2 x Rear = OD = 25mm, ID = 12mm, L = 20mm (replaced) Speedometer: VDO, W1.12, 0 – 120 mph Clutch Push Rod: 195mm (appears to have been shortened) Wiring Harness: BMW Scheme #1 Oil Pump Gears: End clearance = 0,11mm (driver), and < 0,05mm (driven) Spec = 0,04mm max Backlash = 0,2mm (spec = 0,05mm max) Idle speed: Spec = 600 – 800 rpm Torque values: Oil drain plugs Cylinder heads Gearbox cover nuts Generator bolt Magneto bolt Spark plugs Drive shaft coupling nut Flywheel hex screw Drive shaft drain/fill plugs Axle spindle nuts Clutch cap screws 24 December 2013 Rev 1.1 Opening ODO = 90770 miles = = = = = = = = = = = 20 Nm 35 Nm in 3 stages 15 Nm 20 Nm 20 Nm 15 Nm 120 Nm 230 Nm 15 Nm 35 Nm 20 Nm 10 Allan‟s BMW R50/2 Restoration (Abridged) SPECIFICATIONS FOR MY BMW R50/2 Headlamp: 6V 35W/35W Bilux Parking light: Pilot lamp 6V, 2W Neutral indicator: Pilot lamp 6V, 2W Charging indicator: Pilot lamp 6V, 2W Speedo lamp: Pilot lamp 6V, 1.2W Tail & stop lamp: Twin filament 6V 5/18W Handlebar & risers: Supplied handlebar = 26” x 7/8”, not Magura Replacement handlebar = 25” x 22mm Φ, from Jan Cornel Supplied risers are vertical for R68 (rare) Used correct risers from Melville Price, re-chromed Fuel: LRP or Leaded fuel with additive Gearbox input bearings: Gearbox lay bearings: Gearbox output bearings: shaft shaft shaft Final drive bearings: Base = BA20D Front = 6204/C3 Rear = 6302/C3 Front = 3203 A /C3 Rear = 6203/C3 Front = 6303/C3 Rear = 6204/C3 Pinion front = 3304 A Wheel drive side = 16013 Gearbox output flange OD = 21mm castellated nut: M14 x 1.5 Throttle cables: Outer = 910mm Inner = A1.6, 1030mm Clutch cable: Outer = B3, 1060mm (1090) Inner = A2, 1340mm (1365) Front brake cable: Outer = B3, 1095mm (925) Inner = A2, 1300mm (1195) Wheel spokes: 140mm x 3.5mm (M4) x 40 per wheel, Berg Union (4-leaf clover) Spoke nipple: 5.5mm AF, Berg Union (4-leaf clover) Top-hat wheel spacers Outer= 25mm OD x 20mm ID x 14mm L, flange = 30mm OD x 1.5mm t Inner= 25mm OD x 20mm ID x 10mm L, flange = 31mm OD x 1mm t Axle nuts: M14 x 1.5, 22mm AF (new s/steel nuts fabricated) Brake drum diameter: Front & rear (after skimming) = 201mm Wheel offset: Spec = 6.5mm +/- 0.2mm Carb mixture adj screw: M7 x 0.75 thread Bowden cable adjusters: M7 x 1 thread Basic carb settings: Carb float setting: 24 December 2013 (my clutch adjuster is now 5/16” BSW) Needle position = 3rd hole from the top Idle air screw = 2 turns out (clockwise = richer, anti-clock = leaner) Idle speed screw = 1 turn in from just touching the slide Set lever at 22mm from cover surface when resting on needle. Set tab so that lever moves another 4mm when fully open Rev 1.1 11 Allan‟s BMW R50/2 Restoration (Abridged) SPECIFICATIONS FOR MY BMW R50/2 Front fork dimensions: Front brake setting: Front brake cam: Distance between inner mounting faces for swing arm = 200mm 14mm – 16mm free play at the handlebar lever Lever arms on the hub to be at 90 deg to cable when operated. Rotate front brake adjuster anticlockwise to reduce free play (rotate clockwise to increase play between leading brake shoe and drum) Toolbox lock key: LF 60121 (fitted new cupboard lock) Mirror thread in LH Perch M8 x 1.25 Left Hand Thread Mech Advance springs: 11mm Woodruff key - Gearbox 4 x 6.5mm output shaft: Woodruff key- cam shaft: 4 x 6.5mm Woodruff key – flywheel: 5 x 6.5mm Bevel Drive Oil Seals: 30 x 42 x 7 (Nitrile) Wheelbase: RHS = 1425mm Spec = 1415mm Gearbox – clearance: overshift LHS = 1405mm 1.0mm Front crank spacer: 3.5mm thick Rear crank spacer: 2.0mm thick 24 December 2013 65 x 85 x 10 (Nitrile) 28 x 47 x 7 (Nitrile) Rev 1.1 12 Allan‟s BMW R50/2 Restoration (Abridged) RESTORATION LOG 12 October 2007 Collected the bike from Jimmy D******* in Johan van Zyl‟s 6” trailer. As offloaded at home: 24 December 2013 Rev 1.1 13 Allan‟s BMW R50/2 Restoration (Abridged) 13 & 14 October 2007 10 Hours (Total -= 10 hours) Replaced M10 x 1.5 cap screws on handlebar pillars with polished stainless steel cap screws and stainless steel spring washers Swapped rear suspension units (adjusting handles on wrong sides) Wire-brushed rust from rear suspension components, especially lower portion. Wire-brushed rust from M10 x 1.0 nuts and bolts on front suspension Cleaned up filler plug in lathe for swing arm flange, and cleaned up internal thread with M10 x 1.0 tap Replaced some M8 and M6 nuts and various flat washers with stainless steel Cleaned M6 and M8 threads on tappet covers with die nuts Wire-brushed rust from rear footbrake components Replaced M10 x 1.5 cap screws with M10 x 1.5 high tensile bolts and nuts on centre stand – need to complete repair work on centre stand (springs missing) Fabricated stainless steel pivot screws for front brake lever (brake lever has mild steel bush 8mm ID), and for the clutch lever – fitted stainless steel spring washers and M6 nuts. Fabricated bush 10,5mm OD x 8mm ID (EN1A Pb) for clutch lever, as well as Aluminium M6 threaded bush for clutch handlebar fitting Placed carb bodies & parts in lacquer thinners (didn‟t make any difference a week later!) Bought M6 and M8 chromed dome nuts Bought GP primer aerosol (Dulux) and metallic silver aerosol (Dulux) and primed and painted lower portions of rear suspension Primed and painted top suspension mounting caps (rear) aerosol (Dulux) = Black Limo Stripped front wheel hub – needs new seals (inner seal is felt, outer seal is Nitrile), and perhaps new bearings. Preload to be set later. (See 9 Feb 2008) 18 - 22 October 2007 8 Hours (Total = 18 hours) Cleaned and de-rusted throttle control assembly. Assembled carbs Stripped & wire brushed rear brake levers & bell crank. Reamed bell crank 12,4mm Fabricated new bush (EN1A Pb) for bell crank = 8mm ID, 12,4mm OD, grooved for grease. Fitted stainless steel washers, nuts and cotter pins to rear brake lever assembly. Wire brushed and sanded black paint from air filter housing & components. Primed and spray painted air filter housing, round knob for housing screw, brake lever & bell crank metallic silver. (Re-painted - see 16/17 February 2008) 24 December 2013 Rev 1.1 14 Allan‟s BMW R50/2 Restoration (Abridged) Prepared, primed and spray painted brake pedal Black Limo. (Re-painted - see 8/9 Dec 2008) Prepared and primed hand control bodies. At VMC meeting, Jimmy D***** gave me spring clip for headlight bulb and his partly fabricated rear mudguard. He told me Andy Stead told him he has a workshop manual for me – I must call him. 27 October 2007 3 Hours (Total = 21 hours) Spraypainted L/H hand control Black Limo & polished aluminium hand levers. Turned new 5/16” BSW threaded cable adjuster for clutch lever (used 5/16” BSW threaded rod, drilled through 3mm diameter, silver soldered straight knurled 12mm diameter thumb wheel on, with straight knurled 20mm diameter lock nut) 28 October 2007 5 Hours (Total = 26 hours) Removed and wire brushed front engine/magneto cover. Wire brushed frame hanger for top engine mount, together with its bolt and spacer. Made cardboard template for triangular engine top mounting bracket – to be fabricated from 2,5mm flat plate. Cleaned & repaired rear brake stop light switch, replaced M4 screws and nuts with s/steel, new internal spring, fabricated and fitted brass rivet. (Later replaced with new switch from Uli‟s) Fabricated engine mounting spacer = 27mm OD x 12,5mm ID x 8,75mm thick (EN1A Pb) to match existing (on 21 Dec 2008, fabricated 2 x new aluminium spacers). Removed lower engine mounting bolts and cleaned M12 x 1,5 threads with die nut. Reinstalled with new spring washers and appropriate mounting spacers on LHS. Wire brushed bolts and nuts for the steering friction damper lower assembly. Wire brushed all engine, gearbox and transmission fill and drain plugs and fitted copper gaskets. Cleaned internal threads with M14 x 1,5 tap, and M10 x 1 tap. 24 December 2013 Rev 1.1 15 Allan‟s BMW R50/2 Restoration (Abridged) 31 October 2007 3 Hours (Total = 28 hours) Fabricated top engine mounting bracket from 2,5mm flat MS plate Marked out lower fuel tank mounting bracket for bending Cut 6 x 27mm diameter rubber spacers for top engine mounting bracket and fuel tank lower mounting bracket using 32mm hole saw 1 - 7 November 2007 12 Hours (Total = 40 hours) Fabricated lower petrol tank mounting bracket from 2,5mm flat MS plate Cleaned, primed and sprayed Black Limo topcoat on frame bracket, top engine mounting bracket, lower petrol tank mounting bracket and tubular spacer. Replaced 7 x M6 nuts and flat washers for transmission cover with stainless steel equivalents. Fitted M8 x 75 bolt, spring washer and nut (all s/steel) for gearbox mounting Replaced 4 x M12 x 1,5 nuts with plated Nylock nuts on lower engine mounting bolts Replaced 4 x M10 x 1.0 nuts on upper & lower mounting bolts for front suspension Replaced all M8 bolts, washers & nuts for top engine mounting brackets with stainless steel. Cleaned & derusted M10 x 1 nut on brake lever, replaced spring washer Cleaned out spark plug threads with M14 x 1,25 tap Set valve clearances (inlet = 0,15mm, exhaust = 0,2mm) Removed gearbox Removed engine Fabricated clutch lever bolt (from 80mm plated cap screw) and fitted split pin (3 x 28) Clutch push rod needs to be checked out. (21 Dec 2008 = appears to work OK) Reversed gear lever cotter pin, fitted s/steel nut & washer – housing for g/lever oil seal distorted! Found suitable spring/s for bell housing clutch lever Replaced clutch adjusting M6 bolt & nut with s/steel, fitted M4 screw to neutral indicator. Fabricated cotter pin (EN1A Pb) for kick start lever – fitted M6 s/steel nut & washer Fitted M8 x 45 s/steel bolt for rear brake bell crank 24 December 2013 Rev 1.1 16 Allan‟s BMW R50/2 Restoration (Abridged) 8 & 9 November 2007 5 Hours (Total = 45 hours) Fitted M8 x 75 s/steel bolt, nut & washer to gearbox mount on engine Dismantled front suspension (info from Duane‟s website) Flatted and buffed/polished aluminium tubes on front suspension, also used Autosol Sanded painted tubes with water paper to remove up to 2 layers of paint, black and metallic blue. (Both previous spray jobs did not involve the removal of the tubes!) Panel beat one tube to restore roundness. Removed headlight brackets – rust patches on the inside surfaces 10 & 11 November 2007 8 Hours (Total = 53 hours) Removed wheels, rear swing arm, final drive unit, front swing arm, front & rear suspension units, steering friction damper components, rear brake lever & components Removed centre stand, fettled to fit frame brackets, welded stop on RHS of frame Wire brushed steering friction damper parts to bare metal, removed rust in hydrochloric acid. Wire brushed driveshaft tube end, various bolts and nuts Sanded frame components with 220 grit water paper Polished rear suspension aluminium tubes Purchased 1L MS primer, 1L 2K Black gloss, 1L 2K hardener, 5L thinners = R345, Randburg Automotive Paints Fitted s/steel spring washers x 4 to driveshaft mounting studs 24 December 2013 Rev 1.1 17 Allan‟s BMW R50/2 Restoration (Abridged) 13 - 15 November 2007 4 Hours (Total = 57 hours) Rian Emerich sandblasted: front mudguard, rear mudguard, seat frame, centre stand, both headlight brackets and mounting plates, petrol tank toolbox lid (2,5 hours). Panel beat petrol tank lid Brazed cracked headlight mounting brackets Fabricated another seat mounting bracket (side) from 2,5mm mild steel plate 24 December 2013 Rev 1.1 18 Allan‟s BMW R50/2 Restoration (Abridged) 16 – 18 November 2007 6 Hours (Total = 63 hours) Seat springs and chains removed and de-rusted in Hydrochloric acid. Supplied stainless steel bolts, nuts, washers & lock washers for seat frame. Arc welded seat frame mounting for side bracket. Cleaned rear wheel outer oil seal housing. De-rusted and sanded headlight case with 400 grit water paper. Fabricated tommy bar for tool kit Brush painted bare metal and aluminium parts with Duram Metcote NS5 etch primer. 21 November 2007 1 Hour (Total = 64 hours) Removed steering head, cleaned ball bearings, races pitted from previous rust, 45 balls, should be 46 balls of 5,5mm diameter Large spacer shim missing under yoke – fabricated one (thickness to be measured). Note that this was too thick after fitting the taper roller steering head bearings. 23 – 25 November 8 Hours (Total = 72 hours) Overhauled front brakes – seized on one pivot! De-rusted, greased, fitted new split pins, s/steel lock washers Overhauled rear brakes, de-rusted, greased, fitted s/steel washer under brake operating lever. 24 December 2013 Rev 1.1 19 Allan‟s BMW R50/2 Restoration (Abridged) Started spraying MS primer (mixed 4cm primer + 1cm hardener + 1cm thinners) on rear swing arm, front swing arm, seat frame and brackets, headlight brackets, steering damper components, front suspension tubes. Used about 250mL MS Primer. Flatted primed surfaces using 400 grit water paper. 1 - 2 December 2007 6 Hours (Total = 78 hours) Fitted some new M10 nuts on cylinder studs. Removed clutch plate and pressure plate (using 3 x M8 x 1 bolts and nuts). Clutch plate was “rusted” to pressure plate. Cleaned and de-rusted clutch components. Spray painted MS Primer on main frame, front forks, front and rear swing arms, front suspension tubes, headlight, headlight brackets, centre stand, seat components, steering damper components. About 250mL MS Primer left. Flatted primed surfaces with 400 grit water paper. Bought rubber parts and passenger foot rests from CMC = R375 24 December 2013 Rev 1.1 20 Allan‟s BMW R50/2 Restoration (Abridged) 5 December 2007 3 Hours (Total = 81 hours) Took one day leave and visited Jan Cornel in Germiston Jan says backlash in my final drive unit and splines = fine He says use bit of dishwashing liquid to fit R/H Magura grip - done He says cut paper gaskets for both sides of carb flanges, rear swing arm – cardan flange, etc He says cut cork gaskets for aircleaner body and sump Jan Cornel says don‟t bother with Breather filter insert, etc Jan Cornel says solid copper gaskets on filler/drain plugs = OK, also use some PTFE tape Jan Cornel says replace rear brake linings with softer bonded linings Bought various parts from Jan Cornel = R350-00. Bought 6mm dia x 70mm hardened & ground steel dowel from Toolquip & Allied. Shortened dowel to 60mm as indicated in the spec = too long for generator removal! Shortened to 40mm, now too short, unless I use a longer M8 high tensile bolt! Needed longer dowel to remove the magneto = 80mm Removed generator and magneto from engine – cleaned and de-rusted. Stripped magneto centrifugal advance – pivot pins worn, one spring butchered (subsequently replaced with new from Uli‟s), cam has wear marks. De-rusted portion of front seat bracket bought from Jan Cornel. 8 - 9 December 2007 9 Hours (Total = 90 hours) Sanded and etch-primed (brushed) front and rear mudguards Attempted to braze weld rear mudguard – not very successful Removed generator hub and magneto journal oil seals – hardened by age and heat – use Viton. Turned M5 and M4 electrical screws for generator & magneto connectors respectively. Primed and flatted with 400 grit water paper 1 x footbrake lever, 4 x foot pegs, tank toolbox cover, seat front bracket, rear swing arm touch-up, finished MS primer. Sprayed frame and all components Gloss Black (2K), finished 1L of paint. Cut 2 x paper gaskets for drive shaft housing joint to bevel drive. 15 – 17 December 2007 15 Hours (Total = 105 hours) Sprayed both swing arms, front forks, and yoke plate again to reduce runs, after flatting with 400, 1500 and 2000 water paper Assembled seat frame and cut some treadmill mat for seat backing Fabricated bearing puller to remove outer portion of 30203 taper roller swing arm bearings Replaced LHS & RHS rear swing arm bearings 30203 (DYZV) and seals 22 x 40 x 7 Nitrile. Fabricated magneto & generator extractor from M8 x 100 high tensile bolt Fitted centre stand to frame with M10 s/steel bolts, spring washers and nuts Fitted spring to centre stand (shortened one s/steel bolt to clear spring) Assembled and primed front & rear suspension units, fitted rear units Fitted new rubbers to main foot rests (used dishwashing liquid to ease them on) Flatted with 2000 water paper & burnished headlight brackets, headlight and yoke Buffed M5 round head screws for name plate and fixed name plate to steering head Fitted rear swing arm to frame – slight preload on taper roller bearings (1/8 turn or less) Fitted bevel drive to swing arm using new paper gasket (dry). Fitted Magura grip to RHS hand control – used a bit of dishwashing liquid Fitted rear wheel 24 December 2013 Rev 1.1 21 Allan‟s BMW R50/2 Restoration (Abridged) 18 - 24 December 2007 14 Hours (Total = 119 hours) Disassembled rear wheel, rear suspension units, rear swing arm and bevel drive again Turned frame upside down and spray painted the frame again (4th time!). Touched up rear swing arm in the vicinity of the oil seals. Re-assembled rear wheel, rear suspension units, rear swing arm and bevel drive again Removed tyre and tube from front wheel, and de-rusted the rim with a file and wire wheel. Coated inside of rim with Rusist and painted with Duram Metcote NS5 etch primer. Noted that the rim is not correct for the „bike. Taped over spoke nipples with black electrical insulation tape, 4 – 5 layers (entire new roll!) Refitted tyre to front wheel rim with new tube (tube is too big for tyre! – subsequently replaced) Fitted front seat bracket to frame with s/steel M6 bolts, washers, lock washers and nuts. Removed lower steering head ball bearing inner race (borrowed bearing extractor from Ivan, but the bearing was a loose fit on it‟s seat) Removed ball bearing outer races from steering head – tapped out easily with 12mm round bar. Cut cork gasket for air filter housing. Removed LHS cylinder head – quite a few damaged fins to be repaired! High compression piston marked 68.42 (= first oversize), combustion chamber showing damage. Removed both LHS and RHS cylinders and pistons. Bores looked very good, pistons looked fine, rings looked fine, but end gaps measured to exceed spec. LHS conrod small end bush scored and needed replacing. Very visible radial play between bush and wrist pin. LHS piston showed some wear on ring land consistent with loose wrist pin. Removed RHS cylinder head. This head had been cleaned up prior to purchase. High compression piston marked 68.42 (= first oversize) fitted. Cleaned spark plug threads with M14 x 1,25 tap RHS conrod small end bush loose (turned easily in conrod). No excessive radial play Stripped and cleaned all four rocker arms – excessive axial play to be eliminated when refitting. Dismantled valves, cleaned and ground in. Seat widths = 2.2mm after fine grinding. Spec = 1.5 / 2mm. LH cylinder exhaust valve pitted on face and chrome worn at tops of stems. Measured piston skirt diameters and cylinder bores. All fine. Piston clearance calculated at 0.125mm instead of 0.08mm specified. Measured 0.1mm clearance. 24 December 2013 Rev 1.1 22 Allan‟s BMW R50/2 Restoration (Abridged) 24 December 2013 Rev 1.1 23 Allan‟s BMW R50/2 Restoration (Abridged) 24 December 2013 Rev 1.1 24 Allan‟s BMW R50/2 Restoration (Abridged) 25 - 31 December 2007 10 Hours (Total = 129 hours) Measured piston ring gaps ½” below top of bores = 0.55 / 0.58mm for top rings, = 0.8mm for 2 nd rings (both out of spec) Measured piston ring groove clearances = 0.05mm (spec = 0.07 – 0.1mm) Cleaned cylinder base stud threads with M10 die nut Checked wrist pin radial play in conrod bushes. LHS had excessive play. Cleaned and oiled valve lifters (tappets). Cleaned cylinders/barrels in hot water & caustic soda Fabricated 2 x stainless steel washers for steering yoke. (Redone – see 5/6 January 2008) Fabricated heavy stay (with lever) to clamp flywheel for removal of the 41mm AF bolt Removed 41mm AF bolt using heavy tube spanner, with impact from 2kg hammer - VERY tight! Cleaned up outer face of 41mm AF bolt in the lathe Removed flywheel – came off with only finger pressure, fortunately. Removed rear silicon oil seal – to be replaced. Crank/Flywheel woodruff key to be replaced. Cleaned inside of engine case bell-housing Washers missing from rear crank bearing carrier (replaced, see 2 January 2008) Removed rust from cylinder fins by electrolysis 24 December 2013 Rev 1.1 25 Allan‟s BMW R50/2 Restoration (Abridged) 1 January 2008 2.5 Hours (Total = 131.5 hours) Cleaned Everbest fuel petcock. Needed fibre gaskets and top nut. Fabricated pivot pin from stainless steel for foot brake bell crank, also s/steel washers Fabricated 4 x M5 stainless steel bolts for tops of carb float covers. 2 January 2008 2 Hours (Total = 133.5 hours) Visited Jan Cornel again. Confirmed order of spares (to arrive mid-February 2008). Jan also measured pistons and bores – confirmed 0.1mm diametral play between pistons and bores which should be OK with the high compression pistons. Measured gudgeon pin wear = negligible. Also checked for big end bearing play – said they are also OK. Jan said the valve rocker ends need to be polished flat by engineering works. He said one could lap the taper and seat on the crank and flywheel using grinding paste after the crank is removed from the engine. He recommended removing the crank to clean the slingers. He also said the Silicon rear crank oil seal can be replace with either Nitrile or Viton seals. He showed me new examples of both seals (the Viton one was 8mm thick vs 10mm for Nitrile & Silicon. Jan said pushrod tube rubber seals on the motor are too hard. Bead blasting will require total dismantlement with all holes blanked off, etc. This also applies to wheel hubs, etc. Jan steam cleans the inside of the engine casing before taking it for bead blasting. He quoted R1100 for new Metzeler ME11 front tyre, R750 for tappet cover, R450 for set of tank knee pads. He said try to keep fuel cock soaked in petrol to stop it from leaking. He also gave me “top hat” for ignition switch. He said the valve pushrod tubes I showed him will be fine, no need to re-chrome them. He confirmed that the foot brake lever uses the foot peg rubber as a stop, and not the brake light switch! The seat bracket fits between the mudguard and the frame on the front mounting bolts. Jan also said there should be no spring washers on a BMW (not a British bike that vibrates the fasteners loose!). Use flat washers. Also visited Mike Lester in Edenvale. Mike recommends Supreme Bumpers for chroming. He said I can try the Wynns Cleaner polish on the 2K topcoat after flatting with 2000 water paper – milder than burnishing compound. He recommends s/steel exhaust system from Bob Baker at R3500 (no longer available!). He has painted his cylinder fins with Black 2K – says do NOT powder coat cylinders as it may lead to overheating! He says I could use etch primer on cylinder fins before coating with 2K. He clearcoats the petrol tank after pin striping (light grey) because jeans will rub against paintwork and remove pin striping. Removed 4 x stripped M6 studs from rear bearing carrier, and fabricated 5 new M6 studs from high tensile 8.8 bolts. Supplied new high tensile nuts and flat washers. Brush-painted Duran Metcote NS5 etch primer on cylinder fins. 3 January 2008 2.5 Hours (Total = 136 hours) Cleaned threads in cylinders (for cylinder head bolts) with M10 tap Removed sump, cleaned and flattened around bolt holes. Oil strainer bolts were less than finger tight. Cleaned oil pump strainer in petrol. Sump to be bead blasted prior to spray painting – silver with clearcoat. Note that there is no sieve or baffle plate, and no holes for mounting one either. Cut new sump gasket from 2mm cork sheet Bought black gloss engine enamel spray and spray-painted both cylinders/barrels Placed Everbest fuel cock in petrol to swell the cork material 24 December 2013 Rev 1.1 26 Allan‟s BMW R50/2 Restoration (Abridged) Removed timing cover – used part of bearing puller to pull the cover off the generator bearing. The inside of the motor was black from oil and heat! Note: there is no facility for a wire circlip to retain the engine breather disk. 4 January 2008 3.5 Hours (Total = 139.5 hours) Removed oil pump gear (14mm AF nut Left Hand thread!). Pulled gear off with 3-leg puller. Removed camshaft and gear. Fabricated a puller using 100mm high tensile bolt and nut. Camshaft pulled out of inner race of rear bearing. Needed to extract bearing from engine casing. Pressed cam gear off shaft (5 tons), & pressed bearing off camshaft. Washed timing gear cover in petrol and hot water & soap. Ordered 2 x 6203, 1 x 6004, 2 x 6207 bearings, 1 x 52 x 72 x 8 Viton seal from Invicta. Available Thursday next week. All bearings supposed to be KBC. Collected taper roller bearings for steering head from Post Office (no additional charges!) Fitted taper roller bearings (51W/34W) to steering head and assembled forks. Fabricated spacer was too thick. Need to fabricate a thinner spacer. 5 - 6 January 2008 6 Hours (Total = 145.5 hours) Polished & fitted valve push rod tubes to cylinders (about 2mm below mounting surface) Assembled Earle‟s forks, front suspension, fitted front wheel, fitted headlight brackets with s/steel hardware. Fabricated a thin spacer for steering head from tinplate. Adjusted preload in steering head and fitted steering friction damper. Fabricated 6 x 25mm diameter stainless steel washers to fit on steering yoke and front suspension bolts. Levered 6004 bearing off crank gear with two large screwdrivers. Purchased more rubber parts from CMC = R150 24 December 2013 Rev 1.1 27 Allan‟s BMW R50/2 Restoration (Abridged) 7 – 8 January 2008 5 Hours (Total = 150.5 hours) Used 2-jaw bearing puller to remove crank gear (very tight) from crankshaft. Note that there are no circlips restraining the crank gear, but there is a spacer between the 6004 bearing and the crank gear. Cleaned M8 threads in main bearing carrier for the removal tool. Screwed 2 x 150mm lengths of M8 threaded rod into the removal tool holes. Screwed a short M8 bolt into top of crankshaft to take the pressure of the puller. Placed “universal” puller plate over the crankshaft nose and over the two lengths of threaded rod. Used M8 nuts over washers to pull main bearing carrier, complete with main bearing, off the crankshaft. Used SKF internal jaw puller to extract 6203 camshaft bearing from engine housing – easy removal. Removed screw from front slinger and removed front slinger from crankshaft. There was one spacer between the slinger and the crank gear. Removed and labelled valve lifter/tappets. Also labelled all spacers on the crankshaft. Tapped rear of crankshaft forward with a nylon hammer. The rear bearing started moving with the crankshaft out of its carrier. Used internal jaw puller to push crankshaft out of rear bearing and to pull rear bearing back into its carrier. (Later I found that the crank should be removed with the rear bearing fitted to the crank!). Tilted front of crankshaft downward and rotated crank assembly until it came out of the engine casing. Removed screw from rear slinger and removed rear slinger from crankshaft. There were two spacers between the slinger and the rear crankshaft bearing. Cleaned all M6 threads in engine casing with M6 tap. Purchased 1 metre of spark plug wire from Blitz Motor Spares. 9 January 2008 3.5 Hours (Total = 154 hours) Cleaned muck from slingers. Removed about 60 grams of muck from both slingers! 24 December 2013 Rev 1.1 28 Allan‟s BMW R50/2 Restoration (Abridged) Prepared cylinder heads, tappet covers, sump, slingers and engine cover for bead blasting. 10 January 2008 0 hours (Total = 154 hours) Zane took slingers, sump, front cover, heads and tappet covers for bead blasting (I supplied a bottle of Red Heart Rum as compensation to the other party) Collected 2x 6203, 1 x 6004, 2 x 6207 bearings and 1 x Viton seal 52 x 72 x 8 from Invicta. Collected samples of Nitrile sheet in 1mm and 1,5mm thickness from Shidawei, no charge. Purchased 300 x 200 x 2,5 flat MS plate and 3m of 16mm x 3mm MS flat bar from Fleet Steel. 24 December 2013 Rev 1.1 29 Allan‟s BMW R50/2 Restoration (Abridged) 12 - 13 January 2008 5 Hours (Total = 159 hours) Painted sump cover exterior with self-etching NS5 primer. Washed engine main casing with paraffin, engine cleaner, water jet, hot water with soap, rinsed in cold water and dried with compressed air Stripped cylinder heads of valve gear and washed them in hot soapy water. Dried with compressed air. Washed front engine cover, tappet covers in hot soapy water, dried with compressed air. 24 December 2013 Rev 1.1 30 Allan‟s BMW R50/2 Restoration (Abridged) Washed all valves, springs, cotters etc to remove all traces of bead blasting residue. Measured valve stems, valve springs (outer springs in spec, inners springs a bit short) Cut Nitrile gaskets for fuel tank emblems Pressed front crank bearing out of carrier = 2 tons on hydraulic press (next time use heat!). Removed lock from fuel tank lid Measured clearance between valve stems and guides with dial indicator – stems projecting 15mm from top of guides, indicator about 12mm from top of guides. RHS exh = 0.5mm, RHS inlet = 0.2mm: LHS exh = 0.45mm, LHS inlet = 0.15mm. Spec = 0.040 – 0.070mm diametral clearance. Measured bore diameter of guides with small bore gauges: RHS exh = 7.22mm, RHS inlet = 7.07mm; LHS exh = 7.20mm, LHS inlet = 7.06mm. Spec = 7.005mm maximum when new. Measured valve stem diameters average = 6.92mm for exhaust valves and 6.93/6.94mm for inlet valves. This was within a wear limit of 1 thou inch (0.025mm) of the diameters when new (6.935 – 0.0254 = 6.91mm) 20 January 2008 2 Hours (Total = 161 hours) Fitted new high tensile M6 studs to rear crank bearing carrier with Ritelok Studlock, after cleaning threads in engine casing with an M6 tap and Meths. Found ¼” diameter s/steel wavy washers and fitted 5 to rear bearing carrier. Cleaned and washed front main bearing carrier. Staked the blanking grub screw in front main bearing carrier 26 - 27 January 2008 4 Hours (Total = 165 hours) Honed cylinders using Zane‟s hone and H32 oil. Washed cylinders in hot water and dishwashing soap. Oiled bores lightly with H32 oil for storage. Fabricated metal clamping ring for sump cover using 16 x 3mm flat bar. Made bends with oxyacetylene heating, drilled holes 6.8mm Washed crank assembly in petrol. Measured conrod (axial) end play = excessive, and rear main bearing journal was undersize (34.97mm) 24 December 2013 Rev 1.1 31 Allan‟s BMW R50/2 Restoration (Abridged) 29 – 30 January 2008 1 Hour (Total = 166 hours) Visited Al Gibson and Mike Lester Al Gibson verified crankshaft OK, gave me 7mm Matra reamer for valve guides, crank rebuild instructions Mike Lester gave me a pair of old OEM mufflers (both rusted through) Dropped off seat at Classic Auto Trimmers for recovering. To be collected 6 Feb. Bought springs from Starco and fabricated another centre stand spring. 3 February 2008 1 Hour (Total = 167 hours) Visited CMC again, mainly to swap out silent blocs. The new stock should arrive next week. Swapped out silent blocs for the correct 2 for the rear suspension units. Fitted new silent blocs to rear suspension units. Enquired about best tyres and was told by Hennie, John and Graham that Metzeler is still the one to go for, but buy the cheapest one = ME22. Hennie confirmed that the 4.00 x 18” Yokohama on the rear of my bike should also be changed for a 3.50 x 18” tyre. Hennie also confirmed that Loctite could be used on the rear main bearing journal of the crank. Asked Hennie to look out for rear mudguard – he says front one is even more rare! 5 – 7 February 2008 0 Hours (Total = 167 hours) Bought 2 x Metzeler ME22 3.50 x 18” tyres from Mosskays @ R325-00 each including VAT, fitting & balancing. New King Tube fitted on rear wheel = R50-00. Bought 5L Shell Rotella Tx SAE 40 oil from Midas, Primrose Hill. Jan Cornel phoned with good news and bad! Spares from Uli‟s are in the country, but Customs want to charge around R2500 in Duty! Referred back to Customs, could take a while to resolve. There should be no duty on these parts. 8 February 2008 0 Hours (Total = 167 hours) Went to Classic Auto Trimmers to collect BMW seat. Piping was black, not white, no strap. To be corrected – most disappointed (petrol = R150 to date already!) 9 – 10 February 2008 7 Hours (Total = 174 hours) Faced front wheel hub seal retainer in the lathe and countersunk 4 x 4mm diameter holes Turned new top hat spacer (LHS/outer) from BMS for front wheel bearing stack to suit new 25 x 35 x 7 Nitrile oil seal for hub nut. Old top hat spacer was less than 24mm diameter and scored. Fitted new DYZV 30204 bearings to front wheel (old FAG bearings were pitted), and adjusted preload by lapping the “wedding band” spacer and the large outer spacer. Replaced old felt oil seal on the inner hub of the front wheel with a 25 x 38 x 7 Nitrile seal. Refitted front wheel to the frame. Replaced one rear wheel bearing with a DYZV 30204 (old NSK bearing had evidence of minor rust pitting) and adjusted preload by lapping the “wedding band” spacer and the large outer spacer. Note that the outer oil seal on the rear wheel is 24 x 35 x 7 (a new 25mm OD top hat spacer was fabricated on 24 Jan 2009), and the inner seal is 25 x 38 x 6. Refitted rear wheel to the frame. 24 December 2013 Rev 1.1 32 Allan‟s BMW R50/2 Restoration (Abridged) Used Shell Retinax HD2 grease to pack wheel bearings 12 – 14 February 2008 0 Hours (Total = 174 hours) Collected re-covered seat from Classic Auto Trimmers = R513-00 Bought 2 x oil seals = 24 x 35 x 7, and 25 x 38 x 7 from Bearing Man, Ontdekkers Rd. 24 December 2013 Rev 1.1 33 Allan‟s BMW R50/2 Restoration (Abridged) 15 February 2008 0 Hours (Total = 174 hours) Phoned Bill Speight re rubber parts – gave me new e-mail address and e-mailed price list. Phoned Jan Cornel re length of inner valve springs – he said should be OK, can try to stretch them a bit. Still no news from Customs. Phoned Hennie van Zyl – he said buy new valve springs now. Still looking for rear mudguard for me. 16 – 17 February 2008 6 Hours (Total = 180 hours) Brush-painted Duram Metcote NS5 primer on fabricated sump support strip. Stripped Dulux silver spray paint off airfilter housing and both rear suspension mounts. De-rusted airfilter housing and hooter parts in Hydrochloric Acid. Primed sump, sump support strip, airfilter housing, airfilter clamp bolt, hooter front grill and hooter plate with MS 2K primer. Spray painted sump, sump support strip, airfilter housing, airfilter clamp bolt and both rear suspension mounts with silver paint (2K). Filled bevel drive with 150mL of Shell Rotella Tx SAE40 oil (drained and replaced with SAE90 oil on 21 Dec 2008). Fabricated tank toolbox lock. 20 - 22 February 2008 0 hours (Total = 180 hours) Requested Piet B to assist in purchasing spares from Germany. He confirmed on 22 February that he would purchase the spares on my behalf and bring to South Africa. 23 - 24 February 2008 3 Hours (Total = 183 hours) Added another thin brass shim to Earle‟s fork pivot, and readjusted tapered roller bearing preload. Cut 4 x paper gaskets for carburetor flange/manifolds. Inspected wiring harness = very good condition Inspected control cables – disappointing quality of fittings. Missing front brake swivel joints. 24 December 2013 Rev 1.1 34 Allan‟s BMW R50/2 Restoration (Abridged) 25 - 26 February 2008 1.5 Hours (Total = 184.5 hours) Rubbed fuel tank down with 400 and 600 water paper Mark Bell of Pratley confirmed use of Quick Set White Epoxy to glue ceramic resistor. 28 February 2008 Jan Cornel phoned, still no word from Customs. He had small-end bushes, pushrod tube rubbers, and gaskets in stock. He said piston rings can be purchased from Cord Rings. I told him I would wait for Uli‟s parts from Customs. Craig Harmse confirmed Chemence has stock of RT20G. He delivered 50mL container on Saturday 1 March 2008 = R68-00. 2 March 2008 1 Hour (Total = 185.5 hours) Bought more spares from CMC (mudguard, silent blocs, side stand). Pressed 4 x new silent blocs into front suspension. 4 March 2008 0 Hours (Total = 185.5 hours) Collected spares from Jan Cornel, including tail light shell. 7 March 2008 Phoned Allcoweld (Russell) re welding of fins on cylinder head. Minimum charge = R150 and hourly rate = R300. Phoned MCR Specialised Welding (Ryan) and went to see him in Strijdom Park. Quoted R235 + VAT for cylinder head and R450 + VAT for tappet cover, including shaping/forming. Phoned Charlie Hamer of Aero Tig and he quoted around R140 for welding only of both tappet cover and cylinder head. Arranged to meet with him at Piston Ring Club Swap Meet on 16 March. 8 - 9 March 2008 2 Hours (Total = 187.5 hours) Removed rust from crank lobes with sandpaper & paraffin. Removed old small end bushes in the hydraulic press. Cleaned new bushes and conrod holes with methylated spirits. Applied RiteLok RT20G retainer to outside of new bushes and to inside of conrod holes. Pressed new bushes into conrods using the hydraulic press. Drilled oil holes in small end bushes with 3,2mm drill bit and pressed steel ball on inside. De-burred rear bearing seat on crankshaft, and liberally oiled crank assembly. Repaired generator load resistor with Pratley Quick Set White Epoxy 15 – 16 March 2008 1 Hour (Total = 188.5 hours) Fitted new advance spring to magneto. Fitted new float guide pins to both carbs. Confirmed that new trim ring for speedometer fits. Fitted new drain/filler plug to drive shaft housing, with new copper washers. Took one cylinder head, one tappet cover and front mudguard to Charlie Hamer for welding. Purchased 6 x Norma 70 – 90mm hose clamps at Piston Ring Swap Meet. 24 December 2013 Rev 1.1 35 Allan‟s BMW R50/2 Restoration (Abridged) 19 –20 March 2008 Collected welding from Charlie Hamer - very reasonable price! 21 – 24 March 2008 7 Hours (Total = 195.5 hours) Machined welded fins on tappet cover and cylinder head – used 8,5mm end mill in milling machine, rotary burr in Dremel, lots of hand filing. Smoothed dents in front mudguard & petrol tank with body filler. Sourced M5, M6 and M8 s/steel hex screws, washers, lock washers and nuts from stock for fitting front & rear mudguards. Faced and polished some s/steel hex screws and s/steel washers. Removed old chrome trim ring from speedometer – need to paint pointer off-white and clean dial face before fitting new chrome trim ring. Roly Tilman gave me rear mudguard, front fender brace, tappet cover, sump cover, damaged tail light shell, exhaust headers & cross over tube. I gave him my R67/R68 rear mudguard in exchange. 26 March 2008 1 Hour (Total = 196.5 hours) Zane bead blasted one cylinder head, 2 x tappet covers and domed engine cover. Bought s/steel bolts & nuts from JKM Washed bead blasted parts in hot water & soap, dried with compressed air, and coated tappet covers and dome with Shield penetrating oil. 24 December 2013 Rev 1.1 36 Allan‟s BMW R50/2 Restoration (Abridged) 29 – 31 March 2008 4 Hours (Total = 200.5 hours0 Fabricated sheet metal sleeve for rear mudguard. Fabricated 12 x s/steel M6 studs and fitted to sump with RiteLok Studlock. Removed both 5/16” BSW studs from Roly Tilman tappet cover, turned them down for a length of 23mm and threaded them M6. Fitted modified studs to tappet cover with RiteLok Studlock. 3 April 2008 Collected set of two new middle/second rings from Uli‟s at Post Office (R12-00 Customs clearance). New rings have steps that face the bottom of the piston. 4 April 2008 3 Hours (Total = 203.5 hours) Fabricated an inclined block from chipboard to mount cylinder head for valve guide replacement. Turned a 12mm diameter bar down to 7mm diameter for a length of about 30mm to use as a drift to remove old valve guides. Heated both cylinder heads in the domestic oven at 200 deg C for 30 minutes, and placed new valve guides in freezer. Placed heated cylinder heads on inclined block and drifted out old valve guides – came out easily. Inserted new (frozen) valve guides in cylinder heads. One guide in each head virtually dropped in place requiring no persuasion with a hammer & drift. The other two guides went in about half way using finger pressure and then required very light taps with the drift and hammer to seat. Note that the new valve guides are 43mm long, while the removed guides are 50mm long. Most of the difference in length is accommodated in the tappet cover side of the cylinder head. This difference was later clarified with Jan Cornel. Reamed new valve guides with Matra reamer in Ryobi cordless drill (0-500rpm) with cutting oil. Note that in future bronze guides should be reamed DRY. Exhaust valve guide in LHS cylinder head was too loose, and fell out when attempting to ream it. Measured hole in cylinder head = 13,10mm, whereas the guide OD = 13,05mm. 7 April 2008 1.5 Hours (Total = 205 hours) Jan Cornel confirmed that the 43mm long valve guides are correct and that I could lightly knurl the loose guide, and perhaps use some high temperature Loctite to fit it. Knurled loose valve guide to ~13,15mm OD, heated LHS cylinder head to 180 degree C for about 30 minutes, and fitted new valve guide (after freezing) with the drift and hammer successfully (tight fit!). Note that the RT20G hardened too quickly under the heat and had to be dispensed with. Reamed exhaust valve guide in the LHS cylinder head to size when cold, using neat cutting oil. Note that in future bronze guides should be reamed DRY. 12 – 13 April 2008 2.5 Hours (Total = 207.5 hours More fabrication on rear mudguard – hinge, extension pieces, brackets with M8 threads, grinding. More panel beating, filling, smoothing of front mudguard. Took rear mudguard to Rian Emerich for sand blasting Bought 1m of M6 s/steel studding 15 April 2008 0 Hours (Total = 207.5 hours) Collected sand blasted rear mudguard from Rian Emerich. 24 December 2013 Rev 1.1 37 Allan‟s BMW R50/2 Restoration (Abridged) 16 April 2008 Purchased 12mm OD hydraulic steel tubing (2 x 460mm) from Lazer Hydraulics for R15-00 to fabricate stays for rear mudguard. One piece was gratis offcut, and the other cost R33/m. 19 – 20 April 2008 3 Hours (Total = 210.5 hours) Flatted sandblasted rear mudguard components with medium emery cloth and painted them with Duram Metcote NS5 etch primer. Purchased 1kg Formula 40 body filler, 1m P60 sandpaper from Randburg Automotive Paints. Welded brackets with M8 studs to rear mudguard 24 – 27 April 2008 2.5 Hours Total = 213 hours) Turned 2 x front brake swivels using 10mm diameter stainless steel rod. Buffed s/steel front brake swivels, wire brushed & buffed rusted nipple on front brake cable. Heated engine front main bearing carrier to 160 deg C and new NTN bearing dropped in. Cleaned slingers in Caustic Soda 28 April 2008 2.5 Hours (Total = 215.5 hours) Fitted new 6203 bearings (Rollway) to camshaft. Fitted rear oil slinger (staked retaining screw), spacer washer & new rear 6207 bearing (NTN) to crankshaft, heated engine casing to 85 deg C in the domestic oven for 30 minutes and fitted crankshaft in engine casing. Fitted front oil slinger (staked retaining screw), 2 spacer washers, and drew new front 6207 bearing (NTN) and bearing housing onto nose of crankshaft. Before fully seating the bearing, the nuts and bolts retaining the main bearing housing were fitted and tightened incrementally. When tight, the front bearing was drawn some more onto the nose of the crankshaft, until it could go no more. Unfortunately, at this stage the front slinger interfered with the back of the front main bearing housing resulting in heavy rotation of the crankshaft. The crankshaft was pressed back slightly to increase the clearance between the oil slinger and the front main bearing housing resulting in much improved free rotation of the crankshaft. Note that a slightly thicker spacer washer is required between the front oil slinger and main bearing to improve the clearance. Also note that the rear main bearing was covering the oil drain hole in the rear main bearing carrier – a sign that the rear spacer was too thick. 29 April 2008 5 Hours (Total = 220.5 hours) Removed front main bearing and housing with universal puller, removed 2 spacers and the front slinger. Removed crankshaft from the engine housing. Held front slinger by its central hole in the 3-jaw chuck and pressed a piece of wood laterally against the periphery of the slinger while rotating to true/flatten the slinger – worked very well to reduce the lateral runout! Turned a new front spacer OD = 46,5mm, ID = 35,0mm and 3,61mm thick. The two spacers removed added up to a thickness of 3,0mm, thus gaining 0,61mm extra clearance for the slinger. 24 December 2013 Rev 1.1 38 Allan‟s BMW R50/2 Restoration (Abridged) Used SKF internal puller to remove the rear main bearing from the crankshaft, and removed the spacer (3,59mm) and slinger. (My guesstimate of 3,61mm was spot-on for the front spacer!) Held rear slinger by it‟s central hole in the lathe 3-jaw chuck and pressed a piece of wood laterally against the periphery of the slinger while rotating to true/flatten the slinger – worked very well! Re-fitted rear slinger, staked retaining screw and fitted the 2mm thick spacer previously fitted at the front bearing. Cleaned journal surfaces and coated with a thin layer of RT20G high temperature retainer. Seated the rear main bearing on the crankshaft journal – clamped using two old outer bearing shells and the flywheel bolt. Measured oil pump clearances. Gear backlash = 0,2mm (spec = 0,05mm max), end clearance = 0,11mm for the drive gear and < 0,05mm for the driven gear (spec = 0,05mm max). This will have to do for now. Heated engine casing to 90 deg C in the domestic oven for 45 minutes and fitted the crankshaft in the engine casing. Rear bearing dropped fully into place easily – oil slinger right up to inside of engine casing, and oil drain hole visible in the main bearing carrier. Fitted front oil slinger (staked retaining screw), new spacer washer (3,61mm), and drew new front 6207 bearing (NTN) and bearing housing onto nose of crankshaft. Before fully seating the bearing, the nuts and bolts retaining the main bearing housing were fitted and tightened incrementally. When tight, the front bearing was drawn some more onto the nose of the crankshaft, until it could go no more. As planned, there is now sufficient clearance between the front slinger and the back of the front main bearing carrier, with no interference. The clearance between the rear slinger and the rear bearing carrier is now about 1,5mm and fairly even. Measured to confirm that the conrods are centrally located in the engine housing bores. Confirmed that the oil drain hole in the rear main bearing carrier is now visible and accessible. 24 December 2013 Rev 1.1 39 Allan‟s BMW R50/2 Restoration (Abridged) 1 May 2008 2 Hours (Total = 222.5 hours) Visited Jan Cornel 14h00 – 16h00 to ream conrod bushes, using his “Hunger” alignment tool and an adjustable reamer. Piston pins have very little wear. Jan says I can polish the piston pins in the lathe using fine emery cloth. Jan confirmed crankshaft location is fine, enough clearance for front slinger. 2 May 2008 2.5 Hours (Total = 225 hours) Heated camshaft gear to 100 deg C in the domestic oven and pressed it on to the keyed shaft with the hydraulic press (still took 3 tons of pressure to fit the gear). Heated engine casing to 80 deg C in the domestic oven and fitted camshaft into engine casing – went in easily with light hammer taps. Secured into position using the four M6 screws. Heated crankshaft gear to yellow heat on a mild steel plate with oxy-acetylene torch and fitted it to nose of crankshaft to align with mark on camshaft gear. Gear seated easily with light hammer taps on spacer tube; then pulled gear tighter onto crankshaft using the high tensile M8 bolt and nut over the spacer tube and let it cool. Heated oil pump gear to 80 deg C in the domestic oven and seated it in place using the 14mm AF left hand thread nut. Bent locking tab over nut. 24 December 2013 Rev 1.1 40 Allan‟s BMW R50/2 Restoration (Abridged) 3 May 2008 0 Hours (Total = 225 hours) John W****** called at around 13h00 to offer complete rear fender for R1200. Bought complete rear mudguard from him, including tail light, number plate carrier. 10 May 2008 0.25 Hour (Total = 225.25 hours) Tapped thread for tail light screw M4. Fitted s/steel M4 screw, slotted. 17 – 18 May 2008 3 Hours (Total = 228.25 hours) Bought 1m x 1m Flexoid 0,4mm gasket paper from Unnic Midas. Cut new gasket for timing cover from 0,4mm Flexoid gasket paper. Fitted original spacer and new KBC 6004 bearing to crankshaft nose using pipe and bolt as a press. Note that there is no provision for a circlip. Fitted new Woodruff key, oil retainer sheetmetal disc for rear crank bearing, and new wavy spring washer to crankshaft for flywheel. Fitted wavy spring washer and crankcase breather disc to camshaft nose. Cut new cork gasket for oil pump strainer/pickup – replaced with Flexoid 1,5mm gasket on 5 June. Refitted captive nuts (M6) to front engine cover. Measured new rings gaps = 0,4mm for top & middle rings and 0,45mm for oil ring (13mm from top of cylinder and square to the bore in left hand cylinder) Set spark plug gaps to 0,6mm 20 May 2008 0.25 Hour (Total = 228.5 hours) Measured dimensions of new piston rings 24 May 2008 1 Hour (Total = 229.5 hours) Fabricated 2 x wood supports for conrods & pistons Verified that oil passages are clear (used compressed air) Fitted oil pump pickup/strainer using new cork gasket with Hylomar on both sides. Replaced with Flexoid 1,5mm gasket on 7 June 2008. Fitted sump cover using new cork gasket with Hylomar on cover side only. 24 December 2013 Rev 1.1 41 Allan‟s BMW R50/2 Restoration (Abridged) 1 June 2008 0.25 Hour (Total = 229.75 hours) Purchased timing cover gasket from CMC, flattened after soaking in water. Modified red fibre gasket to 19mm x 15mm in the lathe for fuel tap. 2 June 2008 0.25 Hour (Total = 230 hours) Purchased red fibre gaskets from Lazer Hydraulics. Modified red fibre gasket to 21mm x 17,5mm in the lathe for fuel tap. 5 June 2008 0.25 Hour (Total = 230.25 hours) Cut oil pump pickup/strainer gasket from 1,5mm Flexoid. 7 – 8 June 2008 5 Hours (Total = 235.25 hours) Removed sump cover and replaced oil pump pickup/strainer cork gasket with Flexoid gasket. Fitted hard drive magnet in sump cover, replaced sump cover. 24 December 2013 Rev 1.1 42 Allan‟s BMW R50/2 Restoration (Abridged) Fitted rear crank bearing splash cover and Viton rear crank bearing seal, lubed with MS grease. Used Tippex to whiten timing marks on flywheel, buffed flywheel seal surface. Fitted new Woodruff key and wavy spring washer and bolted flywheel on using pneumatic impact wrench. Measured initial flywheel lateral runout using dial indicator = 0,4mm t.i.r. Spec = 0.1mm (max). Removed, scraped internal taper, blued and refitted flywheel about 20 times before achieving a lateral runout of 0,22mm t.i.r. (Total indicated reading) Crimped lock washer against flywheel bolt. 17- 18 June 2008 0.5 Hour (Total = 236 hours) Took heads & valves to J.B Engineering to cut seats – Dave & Camper say exhaust valve stems are worn! R150-00 to cut seats 3-angle. (They damaged bore of exhaust valve guide in RHS head) Stoned rocker tips with a triangular oil stone Camper said not to worry about 0,22mm tir lateral runout on edge of flywheel. 20 June 2008 1 Hour (Total = 237 hours) Returned RHS cylinder head to J.B Engineering. At first Camper was unwilling to believe that the damage was due to their methods, but then one of the workers/operators admitted that the exhaust valve guide had fallen out when he tried to cut the seat. He must have damaged the guide when he replaced it! Camper agreed to turn a new guide out of PB1 bronze with the correct interference fit in the head, and to recess the port end 8mm diameter for about 3mm deep. He would use my Matra reamer on the guide (returned to me!) He would contact me on Monday when the job is completed (never did – in fact not once did J.B Engineering contact me!) Washed LHS cylinder head in hot water and soap, assembled LHS cylinder head, original valves, springs, etc. Measured LHS outer valve spring installed height = 33mm on one valve and 34mm on the other. 21 June 2008 2 Hours (Total = 239 hours) Fabricated flywheel puller using M16 x 1.5 bolt & nut, 12mm plate and 2 x M10 x 1 bolts. Removed, scraped and refitted flywheel again to result in lateral runout of 0,16mm t.i.r. 24 December 2013 Rev 1.1 43 Allan‟s BMW R50/2 Restoration (Abridged) 24 – 27 June 2008 1.5 Hours (Total = 240.5 hours) Collected RHS cylinder head from J.B Engineering on 26 June. At around 11h00, when I went to collect the head, it was ready, but when Dave handed it to me I saw that once again the bore of the new guide was damaged (confirmed by Zane), also no counter-bore (as undertaken). Dave said I must talk to Camper later in the day when he returns from an outside job. I took my reamer with me, and returned after 16h00 when Camper handed me the head – they had tried to disguise the damage to the guide bore using a flex-hone and bell-mouthed the bore! Camper stated, “You are “different” to other people!” Took my cylinder head & reamer (no charge) and “cut my losses!” Fabricated 4 x s/steel M8 x 1 dome nuts for driveshaft tube studs. Purchased 200mm of LG2 bronze 21mm diameter from Metals Centre. 28 – 29 June 2008 1.5 Hours (Total = 242 hours) Polished 4 x s/steel M8 x 1 dome nuts for driveshaft tube studs on buffing wheel. Turned 2 blank exhaust valve guides OD = 13,35mm, ID = 6,5mm, L = 90mm (for two), opposite ends counter-bored with end mill 8mm diameter for 4mm deep, chamfered. This was wasted effort as the bronze was LG2 (leaded gunmetal). The colour, however, appears similar to Uli‟s valve guides. 1 July 2008 Purchased Phosphor Bronze bar PB1 from Gold Circle Metals, 19mm diameter x 200mm. 3 July 2008 1 Hour (Total = 243 hours) Heated RHS cylinder head in oven for 40 min from cold to 200 deg C. Placed heated RHS cylinder head on inclined block and drifted out damaged exhaust valve guide from J.B Engineering – tight fit. Measured J.B Engineering fabricated valve guide OD = 13,10mm. 5 – 6 July 2008 2.5 Hours (Total = 245.5 hours) Turned new exhaust valve guide from PB1 bronze: OD = 13,12mm, ID = drilled 6,90mm, turned groove 9,0mm from top of guide, groove = 1,0mm wide and 0,5mm deep, counterbored with end mill = 8mm diameter and 4,0mm deep, chamfer = 70 deg on port side and 45 deg on spring side. Heated RHS cylinder head in oven for 40 min from cold to 200 deg C, and placed new fabricated exhaust valve guide in freezer, after fitting circlip. Placed heated RHS cylinder head on inclined block and tapped in new fabricated exhaust valve guide covered in talcum powder. The guide was a tight fit! After the cylinder head had cooled, reamed fabricated valve guide dry using Ryobi cordless drill machine – tough to ream! Washed RHS cylinder head in hot soapy water, dried with compressed air, flatted sealing surface with 320 waterpaper, sprayed Wynn‟s lubricant to prevent rust of metal parts. 13 July 2008 1 Hour (Total = 246.5 hours) Assembled original valves in RHS cylinder head, fitted tappet cover & gasket. 24 December 2013 Rev 1.1 44 Allan‟s BMW R50/2 Restoration (Abridged) 18 July 2008 2 Hours (Total = 248.5 hours) Fabricated 1mm shim washer that fits between the cam gear and the wavy spring washer for the engine breather disc. Soaked timing gear cover gasket in water, spread a thin film of Hylomar on both sides, and fitted the timing gear cover. Fabricated three washers for the M6 cap screws, and fitted all twelve cap screws to the timing gear cover and torqued them to 9Nm. Fitted the new Viton oil seals to the magneto and generator positions in the timing gear cover. Cleaned all four tappets in petrol and fitted them in position after coating with Wynns assembly lube. Used the Dremel-type tool to grind semi-circles in rubber seals for all four valve pushrod tubes to ensure the oil splash holes in the engine casing remain clear after fitting. Note that this modification came from the slash2 Group and relates to rubber seals purchased from Uli‟s. Fitted the four modified rubber valve pushrod tube seals to engine casing. 27 July 2008 0.5 Hours (Total = 249 hours) Wire-brushed cylinder head bolts and valve rocker arm components. 28 July 2008 Piet B delivered new exhaust valves and kickstart rubber hardware. 2 August 2008 3 Hours (Total = 252 hours) Fitted new exhaust valves to both cylinder heads, together with new valve springs (outer). Lightly ground valves and seats. Measured outer valve spring installed heights. Lightly polished both piston pins in lathe at 600 rpm with 800 grit water paper. Chamfered both sets of compression and 2nd piston ring gap edges lightly with a needle file. Fitted pistons in lightly oiled bores with the gap for the oil ring at the top of the cylinder, and the other rings spaced at approx 120 degrees – presses in easily with the chamfer at the edge of the bore. Checked that arrows on pistons face front of engine. 24 December 2013 Rev 1.1 45 Allan‟s BMW R50/2 Restoration (Abridged) Smeared light layer of silicon grease in rubber valve guide tube bores, and lightly oiled piston pins and piston pin bores, as well as conrod small-end bores with assembly lube. Fitted new aluminium cylinder gaskets to the block dry. (Subsequently, disassembled on 3 Aug) Pressed piston pins through holes in pistons and through conrod – nice easy press fit with thumbs (LHS needed some heat from heat gun), and fitted wire circlips fully home. Hand-offered cylinders to the engine casing, pressing pistons deeper into the bore until seated on engine casing M10 studs. Filed flats on all 8 s/steel cylinder base washers to clear, and hand tightened M10 s/steel nuts. Touched up black heat-resistant paint on outside of cylinders. 3 August 2008 1.5 Hours (Total = 253.5 hours) Purchased chromed carburettor air pipe for RHS from CMC. Test-assembled cylinder head, gearbox and carb to confirm that it fits. One of the air pipes received with the bike appears to be for an R60 (it is about 25mm longer). Removed both cylinders and cleaned cylinder base gaskets and mating surfaces with Acetone. Applied thin film of Hylomar to both sides of the base gaskets. Re-checked orientation of oil ring gaps in both pistons (facing the pushrod tube side of the cylinders) and replaced one piston pin circlip with a spare (the circlip was worn for about 25% of its diameter where the piston pin had rubbed against it). Replaced the cylinders on the engine casing and tightened the base M10 s/steel nuts with an SW17 flat spanner. Faced and chamfered edges of steering damper base cylinder in the lathe. Removed and collected parts for chroming: 14 August 2008 Delivered the following parts to working days (~ 29 Aug 2008): o 2 x carburettor air pipes o 1 x steering damper knob o 1 x exhaust nut o 2 x rear swingarm nuts o 1 x front swingarm nut o 1 x valve pushrod tube TOTAL: 24 December 2013 0 Hours (Total = 253.5 hours) African Electroplating for chroming – to be collected after 10 – 14 = R 130-00 = R 120-00 = R 35-00 = R 60-00 = R 10-00 = R 30-00 =R 385-00 Rev 1.1 46 Allan‟s BMW R50/2 Restoration (Abridged) 16 August 2008 1 Hour (Total = 254.5 hours) Fabricated spacer for steering damper knob from 25mm diameter s/steel, 10,0mm thick, 8mm diameter bore, 4 holes threaded M4, countersunk and polished on the buff. Note that this spacer is required for the steering damper knob to clear the handlebars. 24 August 2008 1.25 Hours (Total =255.75 hours) Washed and brushed gearbox casing with BH38 and hot soapy water. Cleaned up clutch pushrod tip in lathe – and again on 1 November 2008. Cleaned thread for clutch cable retaining bolt with M6 tap. Cleaned rust off another valve pushrod tube (for electroplating) in the lathe. Sent e-mail to Bill Speight ordering: o 1 x grommet for speedo cable at headlamp = R10-00 o 1 x rubber plug for timing hole = R10-00 o 2 x rubber plugs to fill holes in mudguard = R 8-00 o 2 x rubber washer 30mm OD at headlight = R 8-00 o Courier charge (pro rata) R15-00 TOTAL incl Courier charge = R51-00 27 August 2008 0 Hours (Total =255.75 hours) Collected rubber parts from Bill Speight at Post Office. He provided 4 x rubber washers 30mm OD for headlight mounting. 30 August 2008 1.5 Hours (Total =257.25 hours) Fabricated M8 stud for rear mudguard, welded stud to mudguard. Prepared rear mudguard, luggage carrier and tail light shell for painting 24 December 2013 Rev 1.1 47 Allan‟s BMW R50/2 Restoration (Abridged) 3 September 2008 0 Hours (Total = 257.25 hours) Delivered the following parts plus 1 litre Black 2K paint and ½ litre 2K clear coat paint to Mike Lester for spray painting: o Rear mudguard (two pieces) o Front mudguard o Tail light shell o Fuel tank o Luggage carrier 5 & 6 September 2008 1 Hour (Total = 258.25 hours) Collected electroplated parts from African Electroplating. African Electroplating quoted R385 per exhaust header tube and R85 for the exhaust cross tube for chroming. Also quoted R225 to chrome headlamp reflector (about same price to purchase new reflector from Uli‟s) Fitted chromed steering damper and handlebars – the s/steel spacer is required for the steering damper to clear the handlebars since the R68 risers are higher than standard R50/2 Fitted chromed swing arm dome nuts Wire-brushed rust off speedo cable gland, turned and faced outside edge, soaked in Hydrochloric acid to remove internal rust, oiled. Replaced with s/steel fabricated part on 25 Sep 2008. 8 September 2008 0 Hours (Total = 258.25 hours) Collected parts ordered from Uli‟s – paid E40-00 cash (including shipping pro rata). 15 September 2008 Collected sprayed body parts from Mike Lester (some minor issues – rear mudguard primer showing through in one spot). He used Duco plus a clearcoat, NOT 2K. 20 - 21 September 2008 4.5 Hours (Total = 262.75 hours) Assembled rear mudguard parts – tail lamp housing, number plate bracket - using s/steel hardware, new rubber lamp beading. Inserted 3-core cable in rear mudguard channel. Fabricated new M4 screw for number plate light terminal. Terminated wires with crimped bootlace ferrules. 24 December 2013 Rev 1.1 48 Allan‟s BMW R50/2 Restoration (Abridged) Wired tail lamp fitting (Grey = earth, Black = common, Red = stop light) Fabricated s/steel M6 x 22 hex screw for speedo cable retainer. Faced hex head, centre-drilled and drilled 1.5mm Φ hole through screw, necked down to about 5mm Φ for about 12mm. Hung speedo cable up to lubricate with oil. Spray painted speedo needle white Fitted speedo chrome bezel Fitted speedo to headlamp bucket Fitted new rubber washers to headlamp bucket mounting bolts Fitted speedo cable rubber grommet to headlamp bucket (removed on 28 Sep 2009) Fitted fuel tank toolbox lid, greased hinge pins Fitted weatherstrip to fuel tank toolbox lid Fitted rubber knee pads to fuel tank Fitted BMW badges to fuel tank Fitted rubber gasket to headlamp glass 23 September 2008 1 Hour (Total = 263.75 hours) Fitted new carbon brushes to generator. Missing bushing for ignition key – obtained from Jan Cornel on 26 Sep 2008. Turned s/steel steering damper bolt, threaded M8. 24 September 2008 1 Hour (Total = 264.75 hours) Fitted rear brake pedal, bell crank, etc. 25 September 2008 1.5 Hour (Total = 266.25 hours) Machined new s/steel clutch cable bushing for gearbox mounting. Shortened M6 speedo cable clamp screw (20 Sep 2008) to 16mm, to fit new bushing. Fabricated another clutch lever pin from M6 capscrew to take Nylock nut. Fabricated speedo cable bushing/gland out of stainless steel (304). Polished on buffing wheel. 26 September 2008 0.25 Hour (Total = 266.5 hours) Visited Jan Cornel. Jan gave me a red/green lens, an old switch cover with spring, and a plastic bush for the ignition key/switch – no charge. Fitted spring to new ignition switch cover. 28 September 2008 0.25 Hour (Total = 266.75 hours) Fitted large rubber grommet (for headlight bucket) to speedo cable Fitted red/green lens to headlight bucket (temp) – drilled 1mm dia holes and fitted spring wire. 29 September 2008 Bought Black RTV silicon to fit red/green lens. Bought plug spanner and reversible screwdriver. 3 October 2008 0.25 Hour (Total = 267 hours) Refitted red/green lens using black RTV silicon and wire clip. 24 December 2013 Rev 1.1 49 Allan‟s BMW R50/2 Restoration (Abridged) 4 October 2008 6 Hours (Total = 273 hours) Fabricated 2 x s/steel M8 castellated nuts for steering damper bolts (8mm thick). Fabricated 1 x s/steel M8 castellated nut for rear brake bell crank bolt (9.5mm thick). Fitted new s/steel castellated nuts and split pins to steering damper bolts and to rear brake bell crank bolt. Refitted speedo and fitted ignition switch chrome cover, lightly bent tabs. Fitted headlight bucket to fork ears. Fitted wiring harness to frame with black cable ties. Fitted fuse holder (10A fuse) in battery positive cable using crimped terminals. Fitted rear brake switch and connected it to wiring harness – used crimped bootlace ferrules. Fitted 3-way connector block to frame using M3 s/steel screws and nuts. Connected main wiring harness wires to 3-way connector block. Fitted rear mudguard using s/steel bolts, nuts & washers. Connected tail light wires to 3-way connector block using crimped bootlace ferrules. Fitted kickstart lever rubber bumper to frame. 11 October 2008 0.25 Hour (Total = 273.25 hours) Visited Roly Tilman o Obtained some spares (2 x steel rims, 1 x alloy wheel complete, 2 x cable clips). Note: one steel wheel rim was returned to Roly on 24 Nov 2008. o Ordered (telephonic) 2 x new s/steel mufflers from Jeff Talbot in Cape Town. Roly will bring them back with him on 6 November 2008. o He has spare genuine BMW casing for dim/bright/horn switch – looking for switch portion. o Gave Roly a copy of my wiring diagram (laminated) Fitted cable clips to frame. 12 October 2008 2.5 Hours (Total = 275.75 hours) Completed all wiring. Changed white wire to brown (headlight 31), fitted blue, yellow, red and black wires in PVC sleeving for dim/bright/horn switch, connected to 4-way connector block in headlamp. Fitted ignition switch and main switch board. In headlamp bucket. Fitted headlamp reflector, glass and trim ring. Fitted front mudguard and chrome brace. Removed front wheel to fit washers and Nylock nuts. Refitted front wheel. Fitted both perches on handlebar, with Magura hand grips. Updated wiring diagram. Test fitted fuel tank and seat – took photographs. Removed fuel tank and seat for safe storage. Inflated tyres to 170kPa front and 190kPa rear. 24 December 2013 Rev 1.1 50 Allan‟s BMW R50/2 Restoration (Abridged) 17 October 2008 0 Hours (Total = 275.75 hours) Bought 2 x (short) rubber boots for plug caps, Blitz. 18 October 2008 3 Hours (Total = 278.75 hours) Cleaned all three wheel rims obtained from Roly Tilman Re-torqued flywheel bolt. Confirmed flywheel lateral runout = 0.2mm (t.i.r). Bent locktab over flywheel nut. Turned clutch centring mandrel from 25mm Φ aluminium bar. Fitted clutch components using centring mandrel and a little Loctite on all 6 cap screws. Torqued cap screws to 20Nm. Fitted rubber stop for centre stand, using a bit of silicon grease. Fitted new spark plug HT leads through rubber grommets into engine casing – used a bit of silicon grease. Fitted spark plug caps and boots to new HT leads. 19 October 2008 1.5 Hours (Total = 280.25 hours) Removed old input oil seal from gearbox and fitted new double lip Viton seal (30 x 40 x 7). Cleaned outer surfaces with acetone and used a small amount of silicon gasket sealer on those surfaces. Lubricated moving surfaces with assembly lube. Seal pushed in easily with my fingers – fitted seal deeply so that both lips made contact with the input shaft journal. Removed gear lever and old gear lever shaft seal. Seal = 24 x 15 x 7 Nitrile. Turned a mandrel with which to correct the damaged gearbox casing around the gear lever seal. Mild steel OD = 24mm, ID = 15mm, L = 25mm. Heated gearbox casing and tapped bush over gear lever shaft. Cracked casing. Needed to have the casing welded by Charlie Hamer, completed on 23 October 2008. Notched 2 x 50mm lengths of 35mm OD steel pipe using 32mm Φ Starrett holesaw in drill press for exhaust header crossover pipe. (Not used). 24 December 2013 Rev 1.1 51 Allan‟s BMW R50/2 Restoration (Abridged) 21 October 2008 0 Hours (Total = 280.25 hours) Purchased ½ L Black and ½ L Clear 2K paint, Randburg Automotive Paints. 23 October 2008 0 Hours (Total = 280.25 hours) Took gearbox to Charlie Hamer of Aero Tig for welding. 24 October 2008 1 Hour (Total = 281.25 hours) Filed gearbox welding and fitted new double lip Nitrile gear lever shaft oil seal – used some gasket sealer around edges. 25 October 2008 1 Hour (282.25 hours) Removed old oil seal and fitted new double lip Nitrile oil seal behind kick-start lever – used some gasket sealer around edges. Buffed kick-start lever and gear lever before refitting them – greased cotter pins to prevent rust. Fabricated large adjustable pin spanner as stay for gearbox output flange. Tried to undo castellated nut on gearbox output shaft – unsuccessfully (broke Mannell tool!) 29 October 2008 0 Hours (282.25 hours) Took 2 x steel wheel rims to Rian Emerich for sandblasting. 24 December 2013 Rev 1.1 52 Allan‟s BMW R50/2 Restoration (Abridged) 1 November 2008 0.5 Hour (Total = 282.75 hours) Turned a new extension sleeve for clutch pushrod = 8.3mm OD x 6mm ID x 10.5mm L, using leaded free cutting steel. Polished pushrod and cleaned up tapered end 60 degrees in the lathe. 2 November 2008 1.5 Hours (Total = 284.25 hours) Purchased 4 x screws for tank badges and spare drain plug, CMC Jan Cornel used his BMW tools to loosen and remove castellated nut on gearbox output shaft, as well as remove the output flange. Very tight, needed pneumatic impact wrench to loosen both items. Purchased gear lever rubber sleeve, as well as 2 x exhaust crush gaskets from Jan. Cleaned up castellated nut (M14 x 1.5) in the lathe, OD = 21mm. There was no washer behind the castellated nut. Fitted rubber sleeve to gear lever. Fitted 4 x new s/steel screws to tank badges. Removed output shaft oil seal (hardened & brittle) = 36 x 54 x 7 5 November 2008 1.5 Hours (Total = 285.75 hours) Ordered 1 x 6203, 2 x 6204, 1 x 6302, 1 x 6303 ball bearings (all C3) from SKF. Checked that there was no oil in the gearbox – drained a very small amount out. Removed speedo gear and speedo cable s/steel sleeve. Loosened and removed 7 x s/steel M6 nuts and washers from gearbox cover. Removed neutral switch rubber cover, gear lever. Heated gearbox in the oven for 15 minutes at 100 deg C. Tapped gearbox cover off using a wood drift and hammer while pressing the kickstart lever down a bit – tapped output shaft bearing down while tapping the cover off. Fairly easy. Removed circlip and captive gear from gearbox cover and reheated it in the oven again for 15 minutes at 100 deg C. Tapped input shaft 6203 bearing out of the cover easily with a wood drift and hammer. Inspected gearbox components = some light rust on internal parts, including bearings. Otherwise, the gears and other parts look remarkably good. The previous mechanic used only grey RTV silicon gasket material on the cover joint without a paper gasket. Some paper gasket material remained on the mating surface of the cover behind the kickstart gear. There was no sign of any shims behind the input and lay shaft bearings on the cover side. Also missing the stop washer that should be fitted over the spring on the input shaft. Woodruff key was sheared off on output shaft taper. 24 December 2013 Rev 1.1 53 Allan‟s BMW R50/2 Restoration (Abridged) 7 November 2008 0 Hours (Total = 285.75 hours) Collected 1 x 6203, 2 x 6204, 1 x 6302, 1 x 6303 ball bearings (all 2Z / C3) from SKF. 8 November 2008 3 Hours (Total = 288.75 hours) Fabricated 40 x 5 angle iron bench vice-mounting bracket for gearbox Fabricated castellated nut socket/driver from new 13mm Mastercraft deep wall impact socket (ruined 2 x 3/16” end mills and one 24T Eclipse hacksaw blade!). Note that this driver will also fit later M16 castellated nuts. Cleaned thread of castellated nut with M14 x 1.5 tap. Removed shields from the 5 x new SKF bearings. 9 November 2008 1.0 Hour (Total = 289.75 hours) Fabricated gearbox cover gasket using 0.4mm Flexoid. Fabricated 2 x new M6 galvanised studs for gearbox cover. One has damaged threads when fitting earth cable – to be replaced with s/steel next time around! Removed old studs and fitted 2 x new M6 studs using Studlock. 10 November 2008 0 Hours (Total = 289.75 hours) Confirmed with Jan Cornel that a thick flat washer must be placed behind gearbox output shaft castellated nut. Jan also confirmed he can supply gearbox input shaft stop washer and large shim washer. 11 November 2008 0 Hours (Total = 289.75 hours) Collected s/steel exhaust silencers from Roly Tilman = very nice! Ordered FAG 3203 C3 bearing from Barney at Bearing & Belting Supplies. 14 November 2008 FAG 3203 B TVH C3 bearing delivered COD. This bearing may need to be replaced with one that uses a pressed steel cage, and also with a smaller contact angle (A). 15 November 2008 2 Hours (Total = 291.75 hours) Fabricated 2 x Tufnol heat-resistant spacers for carb manifolds. Fabricated 2 x perch wedges, 18mm long, out of ¼” diameter silver steel, unhardened. 22 November 2008 4 Hours (Total = 295.75 hours) Collected two sandblasted wheel rims from Rian Emerich. Wire-brushed both sandblasted wheel rims and coated with aerosol lubricant. Selected one rim to retain and have electroplated. Loosened M6 cap screws retaining the gearshift forks, heated end of case with a gas blowlamp and removed the gear clusters. 24 December 2013 Rev 1.1 54 Allan‟s BMW R50/2 Restoration (Abridged) Washed main gearbox case and cover with petrol and Reinol BH38, dried with compressed air, and coated steel parts with aerosol lubricant. Inspected gearbox parts: most of the bearings appear sound, but some may be too loose in their housings. The input shaft bearing (closest to the splined side) shows signs of damage on it‟s outer ring due to excessive axial play that caused it to rub against the lowest gear on the intermediate shaft (to be expected since the input shaft was missing the stop washer and the spacer shim). The output shaft (output flange end) bearing was rusted. Gears have very little pitting, except for the drive gear at the splined end of the input shaft. The face of lowest gear on the intermediate shaft has been worn smooth by the input shaft bearing face due to excessive axial play from the lack of the stop washer and spacer shim. The lower gear select fork shows more signs of wear than the upper fork. Some light rust on steel parts. Circlip on output shaft worn. Woodruff key sheared off. Removed old bearings from the three shafts using the 20T hydraulic press and the bearing separator/puller combination. Pressed the spring on the input shaft down using the 20T hydraulic press and a short piece of water pipe with two cutouts to remove the wire clip. Replaced all five bearings on the three shafts using the 20T hydraulic press and bits of water pipe. Fabricated 2 x 8mm steel washers for M8 cap screws retaining the gear selector forks. 23 November 2008 0.25 Hours (Total = 296 hours) Fabricated another gearbox cover gasket using Flexoid 0.4mm gasket paper. 24 December 2013 Rev 1.1 55 Allan‟s BMW R50/2 Restoration (Abridged) 24 November 2008 0 Hours (Total = 296 hours) Returned one sandblasted steel wheel rim and one (incorrect) handlebar to Roly Tilman. 25 November 2008 0.5 Hours (Total = 296.5 hours) Purchased 2 off 17 x 1 external circlips, one off 4 x 6.5 Woodruff key, JKM = R4-40. Fitted new 17 x 1 circlip on gearbox output shaft. Removed sheared-off Woodruff key from gearbox output shaft taper. Ground-in gearbox output shaft taper to the output flange using fine grinding paste. 29 November 2008 1 Hour (Total = 297.5 hours) Fabricated 3 x gearbox input shaft stop washers, 2 x 1.11mm thick and 1 x 1.92mm thick, all OD = 25mm and ID = 15mm. Fabricated 1 x gearbox input shaft shim washer OD = 45mm, ID = 15mm, 1.20mm thick 30 November 2008 1 Hour (Total = 298.5 hours) Measured gearbox shaft clusters to calculate endplay (using ½: square HSS bars as parallels): Input shaft height above gasket (0.4mm), measured to top of 1.92mm stop washer Distance to input shaft bearing seated in gearbox cover Output shaft bearing height above gasket (0.4mm) Distance to output shaft bearing recess seat in gearbox cover Distance to intermediate shaft bearing recess seat in gearbox cover 1.15mm 2.28mm 14.27mm 14.88mm 13.02mm Input shaft endplay = 2.28mm – 1.15mm = 1.13mm. Shim thickness required for endplay spec of 0.1mm = 1.0mm. (Either reduce thickness of stop washer to 1.72mm, or reduce thickness of fabricated shim washer to 1.0mm). Output shaft endplay = 14.88mm – 14.27mm = 0.61mm. Shim thickness required for endplay spec of 0.1mm = 0.5mm. Note: existing shim washer = 0.32mm thick. 6 December 2008 1 Hour (Total = 299.5 hours) Measured gearbox shaft clusters to calculate endplay (using ½” x 3/8” Starrett parallels and Mitutoyo micrometer depth gauge (0.01mm) from Ivan): Input shaft height above gasket (0.4mm), measured to top of 1.92mm stop washer Input shaft height above gasket (0.4mm), measured to top of 1.11mm stop washer Distance to input shaft bearing inner, seated in gearbox cover Output shaft bearing height above gasket (0.4mm) Distance to output shaft bearing recess seat in gearbox cover Distance to intermediate shaft bearing recess seat in gearbox cover Intermediate shaft bearing height above gasket (0.4mm) 1.31mm 0.52mm 2.40mm 14.0mm 14.77mm 12.99mm 12.30mm Input shaft endplay = 2.40mm – 1.31mm = 1.10mm. Shim thickness required for endplay spec of 0.1mm = 1.0mm. (Either reduce thickness of stop washer to 1.72mm, or reduce thickness of fabricated shim washer to 1.0mm). 24 December 2013 Rev 1.1 56 Allan‟s BMW R50/2 Restoration (Abridged) Output shaft endplay = 14.77mm – 14.0mm = 0.77mm. Shim thickness required for endplay spec of 0.1mm = 0.67mm. Note: existing shim washer = 0.32mm thick. Intermediate shaft endplay = 12.99 – 12.30 = 0.70mm. Require shim of 0.6mm to reduce endplay to 0.1mm. 7 December 2008 0.5 Hours (Total = 300 hours) Gearbox - fitted a thin Aluminium shim washer to the lower limiting bolt to increase the over-shift to ~ 1mm in 1st gear. The over-shift in 4th gear appears to be in spec (upper limiting bolt) Purchased fabricated and electroplated exhaust headers with captive nuts from CMC. 9 December 2008 2 Hours (Total = 302 hours) Fabricated 2 x eccentric bushes threaded M8, offset by 1mm for gear selector forks using silver steel – adjustment range = 2mm. 10 December 2008 2 Hours (Total = 304 hours) Milled 16mm hex on ends of gear selector eccentric bushes, stamped bushes and selector forks “A” and “B” respectively (1 hour labour). Checked “twist” of lower (“B”) selector fork by inserting a rod in the bush mounting and placing the rod in precision v-blocks on a surface plate, then measure the slight offset of the hardened surfaces to precision parallels. Maximum “twist” was less than 0.4mm, using a feeler gauge. Assembled selector forks in gearbox and adjusted eccentric bushes until the selector rings were central between the gears. Marked the eccentric bushes and the respective selector forks with a file. 11 December 2008 1.5 Hours (Total = 305.5 hours) Moved the eccentric bushes to alternative positions to move the selector forks closer to the gear selector cam plate and marked the bushes with two centre punch pricks. Removed the silver steel eccentric bushes, coated them with liquid soap, heated to cherry red (non-magnetic) and quenched in a bucket of cold water (“glass-hard”). Polished the bearing surfaces of the eccentric bushes and tempered them to “blue”, re-polished the bearing surfaces and reinstalled them in the gearbox, resulting in the selector forks being precisely in the centre between the two gears, and slightly offset toward the gear selector cam plate. Very successful modification! There may be some difficulty to fit the input shaft in its bearing seat – the input gear just catches on the hex head of the new lower eccentric bush. However, it is probably possible to successfully fit the input shaft with some manipulation of the loose 3rd/4th gear selector fork. 24 December 2013 Rev 1.1 57 Allan‟s BMW R50/2 Restoration (Abridged) 13 December 2008 0.25 Hours (Total =305.75 hours) Fabricated another gearbox cover gasket using 0.4mm Flexoid gasket paper. 14 December 2008 0.5 Hours (Total =306.25 hours) Assembled all 3 shafts, selector forks, etc in gearbox casing. Heated casing with gas blowlamp, and inserted a 3 shafts together with the selector forks. Measured output shaft and intermediate shaft projections above case and gasket (0.4mm) again. 15 December 2008 2.5 Hours (Total = 308.75 hours) Visited Jan Cornel: o Compared his stop washer and shim washer for gearbox input shaft with my fabricated items. Need to reduce OD of stop washer and thickness. o Jan checked that gear selector forks are in the middle between the gears, and also checked that there is a small gap between the selector disk and the gears when selected. o Jan says I can replace the Woodruff key in the output shaft – remember to clean and dry the mating surfaces before assembling them. o He also checked the speedo drive gears – said they should be OK. o Purchased 22mm Φ handlebar from Jan that he has recently had electroplated – I paid for the electroplating = R250. o Jan‟s clutch pushrods are longer than mine – perhaps because my clutch is the later version! Tightened M8 gear selector fork cap screws with 6mm hex socket. Turned down fabricated stop washer for gearbox input shaft – reduced OD as well as thickness to 1.75mm. Pressed a joggle in fabricated input shaft spacer shim to match sample from Jan Cornel. Measured shim thickness after flattening on sandpaper= 1.17mm. Measured distance from gasket on gearbox casing to newly thinned stop washer = 1.10mm. Input shaft height above gasket (0.4mm), measured to top of 1.75mm stop washer Distance to input shaft bearing inner, seated in gearbox cover 1.10mm 2.40mm Input shaft endplay = 2.40mm – 1.10mm = 1.30mm. Shim thickness required to achieve 0.1mm endplay = 1.20mm. Fabricated shim of 1.17mm thick is almost perfect! Performed a quick check on projection of both stop washer and shim washer above gasket on gearbox casing = 2.35mm, so endplay = 2.40mm – 2.35mm = 0.05mm = good enough! Measured output shaft and intermediate shaft projections above case and gasket (0.4mm) again. 24 December 2013 Rev 1.1 58 Allan‟s BMW R50/2 Restoration (Abridged) 16 December 2008 4 Hours (Total = 312.75 hours) Fitted output shaft flange oil seal to gearbox cover – 1mm proud, spring facing outside cover. Cleaned up output shaft flange in the lathe 4-jaw chuck. Cleaned M8 x 1 threads in output shaft flange and associated 12-point bolts. Fabricated new thinner washer for output shaft flange castellated nut – bored to fit over taper. Removed old handlebar and risers. Filed clutch hand lever for better fit in perch. Cut 2 x shim washers out of tinplate 0.6mm thick, OD = 47mm and OD = 40mm. Spread a thin layer of Hylomar on the gearbox casing and placed the gasket on top. Heated the gearbox cover with the gas blowlamp. Placed all three shim washers in the recesses in the gearbox casing using a bit of grease to hold them in place. While holding the kickstart lever down a bit, tapped the gearbox cover on the gearbox shafts and casing using a rubber mallet, fitted flat washers and M6 nuts, and tightened the nuts evenly. Checked that the gearbox shafts were not binding while tightening the cover in place. Cleaned the output shaft and flange mating tapers with acetone, and smeared a bit of assembly lube on the flange oil seal surface. Placed the gearbox output flange on the output shaft taper, fitted a flat washer and the castellated nut. Note: did NOT fit a (new) Woodruff key. Tightened castellated nut to 120 Nm using a torque wrench. Fitted speedo drive gear and speedo cable flange collar, fitted M6 s/steel vent bolt. 24 December 2013 Rev 1.1 59 Allan‟s BMW R50/2 Restoration (Abridged) Fitted clutch operating thrust washer components, pushrod and clutch lever. Fitted plastic cap over neutral switch. Filled gearbox with 800mL Shell Rotella SAE 40 oil (to bottom of threads in filler hole) Checked that the gearshift works satisfactorily though all four gears up & down. Removed gear lever for storage. Gearbox finally completed! 21 December 2008 3.5 Hours (Total = 316.25 hours) Drained SAE 40 oil from final drive. Filled final drive with Castrol HypoyB SAE90 EP (GL4) oil to bottom of filler plug threads. Placed rubber bellows over driveshaft flange (on frame). Fabricated 2 x new engine mounting spacers from Aluminium, OD = 27mm, ID = 12.5mm, t = 8.8mm (rust proof!). Covered frame in layers of newspaper to protect paintwork. Lifted engine into frame – used upside down bucket under sump for support. Greased gearbox input splines with MS2 grease. Lifted gearbox into frame behind engine, lightly bolted to engine. Greased engine mounting bolts and inserted through spacers, footrests, etc. Tried to assemble gear lever onto gearbox shaft, but there was no space to fit the cotter pin. Removed rear engine mounting bolt, placed bottle jack under sump and tried to lift gearbox. Bike toppled over and fortunately there was only a light dent on the rear mudguard which would be hidden by the dual seat. Lifted bike back onto centre stand and used a broomstick to lever the rear of the gearbox up to enable fitment of the gear lever cotter pin. Tightened a new Nylock s/steel M6 nut on cotter pin. Refitted rear engine mounting bolt through spacer and footrests, etc. Tightened nuts. Assembled top engine stay and tightened M8 s/steel bolts and nuts. Aligned kickstart rubber stop on frame and tightened M5 bolt and nut. Tightened gearbox mounting bolts. Filled engine with 2L Shell Rotella SAE40 oil. 22 December 2008 4 Hours (Total = 320.25 hours) Cleaned M12 threads in frame and fitted passenger footrests with M12 MS bolts. Fitted valve pushrods with “cracked” ends towards camshaft – used assembly lube on ends. Fitted cylinder heads – checked for 0.1mm rocker axial play. Note: this is far too much, the spec = 0.01mm! Corrected on 24 December 2008. Torqued cylinder heads to 35 Nm in two stages, oiled threads on head bolts. Set valve clearances to inlet = 0.15mm and exhaust = 0.20mm. 24 December 2013 Rev 1.1 60 Allan‟s BMW R50/2 Restoration (Abridged) Oiled rocker shaft assemblies and fitted tappet covers with new gaskets, dry surfaces. Fitted spark plugs and loosely fitted new exhaust headers and s/steel silencers. Fitted new handlebar using existing risers – need to shim risers to close tighter on handlebar. Connected wire to neutral indicator switch. Connected ground wire to gearbox stud (this “new” stud appears to be stripped!) Routed main engine wires through engine casing. Allocated 2 x s/steel M8 bolts, washers and Nylock nuts for exhaust silencer hangers. Replaced thick spring washers on engine mounting bolts with thin s/steel flat washers. Thinned two M12 x 1.5 Nylock nuts in the lathe for rear engine mounting bolt. 24 December 2013 Rev 1.1 61 Allan‟s BMW R50/2 Restoration (Abridged) 24 December 2008 3 Hours (Total = 323.25 hours) Fitted 12-point M8 x 1 bolts to driveshaft flange (without spring washers), then had to remove them because they were scraping against the gearbox cover. Refitted the four 12-point M8 x 1 bolts using Loctite 243 and new spring washers. Confirmed no more scraping against gearbox cover. Fitted hose clamps to driveshaft rubber bellows. Filled driveshaft housing with 200mL Castrol HypoyB SAE90 (GL4) gear oil. Removed tappet covers and loosened cylinder head bolts to correct rocker shaft axial play. Removed valve rocker shafts and adjusted them all to about zero axial free play, but free movement (to meet the spec of 0.01mm axial play). Refitted valve rocker shafts and torqued cylinder head bolts to 35 Nm in 3 stages. Reset valve clearances to inlet = 0.15mm and exhaust = 0.20mm. Oiled valve rockers and refitted tappet covers, dry surfaces. 26 December 2008 2 Hours (Total = 325.25 hours) Fitted generator. Fitted magneto with the rotor mark aligned with the stator mark when the flywheel is on the “S” mark. Connected wiring to generator and magneto, using crimped terminals. Fabricated a new steel screw for the LHS sparkplug wire terminal on the magneto = 2BA (should be M4.5). Ran a 2BA tap through the terminal. Connected sparkplug leads to magneto using crimped terminals. Checked that ignition switch places an earth on the magneto wire when pulled out – mine did not. The contacts on the ignition switch PC board needed to be bent to connect to earth. This was corrected on 31 January 2011. Shimmed handlebar in risers borrowed from Jan Cornel. 27 December 2008 10 Hours (Total = 335.25 hours) Lubricated clutch and front brake cables. Fitted clutch cable. Machined handlebar end down to fit into adjuster. Fitted front brake cable. Removed front wheel twice to reposition brake levers. Brake levers need to be 205mm apart (c – c) to take up cable slack. Fitted a new s/steel M6 bolt, spring washer and nut to the rear brake lever. Fabricated 2 x M8 x 1 s/steel nuts. Fitted one M8 x 1 s/steel nut to front axle pinch bolt. 24 December 2013 Rev 1.1 62 Allan‟s BMW R50/2 Restoration (Abridged) Fitted oiled speedometer cable. Removed lower fuel tank bracket and re-bent locating tab, filed holes, and re-fitted. Fitted fuel tank and fuel cap. Fitted fuel tap to fuel tank, using new red fibre washers. Adjusted carburetor lever arms to 22mm from flange with the needle valve closed. Tab had broken off lever arm on RHS carb – to be fabricated and soldered on to lever arm (see 28 Dec 2008). Drilled and tapped (M5) RHS carburettor float chamber cover retainer holes (x 2) deeper. Slotted 4 x s/steel M5 hex head screws for float chamber covers. Fitted a longer hex screw to RHS carb float chamber cover to compensate for stripped threads. On 18 Jan 2009, fitted M5 Helicoil insert. Fitted carburettors with new gaskets, spacers, s/steel M8 nuts and wavy washers. Fitted carburettor tubes and rubbers. Fitted fuel hoses to fuel tank, carburettors. Fitted air filter housing. Need a thicker o-ring for air filter element. Oiled throttle cables. They are too short and have too little free length – modified one cable to attain 105mm free length (to inside of nipple). Sheath/outer length = 900mm. Fitted front engine cover (mag/gen cover) 28 December 2008 0.5 Hours (Total = 335.75 hours) Fabricated a new brass tab for float lever of RHS carburettor, soldered in place. 29 December 2008 0.5 Hours (Total = 336.25 hours) Telephonically confirmed cable lengths with Jan Cornel. Modified one throttle cable to result in 110mm free length and 1010mm overall length (both measure to insides of small nipples). Successfully fitted modified throttle cable to RHS carburettor and throttle grip. 30 December 2008 0.5 Hour (Total = 336.75 hours) Wired up Horn/Dim/Bright switch and attached to handlebar. Checked with multimeter that neutral indicator switch earths when gear selector is in neutral. Connected 6V battery briefly. Generator light came on for a short while, then went out. Neutral indicator light did not come on. 31 December 2008 1.0 Hour (Total = 337.75 hours) Rotated driveshaft rubber boot and retightened clamps to cure oil leak. There appears to be a small tear on the seam of the rubber boot close to the 70mm end. Fitted ¼” diameter fuel hose to bottom of fuel tank. Charged 6V battery and used it to check brake light – was “on” all the time. Turned brake switch adjuster to ensure that brake light is “off” until the brake pedal is pushed down. 5 January 2009 1.0 Hour (Total = 338.75 hours) Took CMC exhaust headers to Honeydew Exhausts, Lazer Park. Bent using hydraulic ram, but kinked the top. To repair, I would need to cut the pipes off, weld together again, bend and then weld the T-pieces on. Bought 2m of inner cable and 4 x end caps from Eagle Canyon Cycle shop. 24 December 2013 Rev 1.1 63 Allan‟s BMW R50/2 Restoration (Abridged) Anropa want more than R100 per throttle cable to make up. 6 January 2009 1 Hour (Total = 339.75 hours) Bought & fitted 2 x M12 x 30 s/steel bolts for passenger foot pegs, JKM. Drilled threaded hole for speedo cable retaining bolt to 6.2mm Φ. Tapped hole with Recoil tap and fitted Recoil M6 thread insert (s/steel). Fabricated a new (shorter) M6 s/steel retaining bolt with a 1.5mm Φ breather hole. 7 January 2009 2 Hours (Total = 341.75 hours) Fabricated 2 x 3.2mm Φ x 6mm L and 2 x 3.2mm Φ x 6.5mm L brass nipples for throttle cables with 1.7mm Φ holes drilled through. Cable inners are 1.5mm Φ. Fabricated 2 x 6.35mm OD x 5mm ID (for 8.5mm) x 10mm long stainless steel cable end caps with 1.8mm Φ holes through the closed ends. Fabricated one throttle cable using the outer from one cable and the inner from another surplus cable to result in outer length = 900mm, free length = 110mm. I did try 115mm free length, but there was more than 5mm slack, even with the throttle gear moved by one tooth. Sweated cable nipples on with solder. 8 January 2009 0 Hours (Total = 341.75 hours) Jan gave me 20 cable end caps and 4 nipples. He confirmed throttle cable length he gave me was total length including nipples. This makes sense as it results in a free length of around 110mm. 24 December 2013 Rev 1.1 64 Allan‟s BMW R50/2 Restoration (Abridged) 9 January 2009 1 Hour (Total = 342.75 hours) Fabricated 2 more 6.35mm OD x 5mm ID (for 8.5mm) x 10mm long stainless steel cable end caps with 2.0mm Φ holes through the closed ends. Fabricated another throttle cable as before. Lubricated cables with oil. 10 - 11 January 2009 4.5 Hours (Total = 347.25 hours) Fitted throttle cables. Flushed the fuel tank with petrol. Fuel petcock leaked, so removed and dismantled petcock. Old cork has shrunk, dried out. Scraped all the old cork out of the body of the petcock and cleaned the bore. Cleaned up some pitting of the pintle of the fuel petcock in the lathe using file and emery paper. Purchased a sheet of 3.2mm cork from Wizard Midas. Made a paper template 50.0mm x 26.0mm to position the holes – join in the lining must be on the side (horizontal). Punched holes in the template to line up with the holes in the petcock body. Cut cork to rectangle shape 50.0mm x 26mm. Punched 4 x 8mm Φ holes using the template. Greased the inside of the petcock housing as well as the cork gasket with Silicon grease and inserted with the join on the side so that the holes line up. Pressed the pintle and handle into the cork-lined petcock housing, using the bench vice. Recrimped the body of the petcock over the pintle using a small punch. Checked that the holes are clear, and that the tap seals. Refitted the petcock to the fuel tank. Cut exhaust headers to suit s/steel silencers. Fitted exhaust system temporarily. Fitted seat. Refitted fuel tank and hoses. 17 January 2009 0.5 Hours (Total = 347.75 hours) Tested neutral indicator lamp = faulty (6V 2W). Purchased 1 x 6V 3W lamp = R8-00, and 2 x in-line fuel filters = R30-00 Randburg Motorcycle. Replaced neutral indicator lamp with 6V 2W lamp from parking light and fitted new 3W lamp in parking light fitting. Cut fuel hoses and fitted new in-line fuel filters. 18 January 2009 0.5 Hours (Total = 348.25 hours) Fitted M5 Helicoil insert in RHS carb float chamber. Fitted shorter M5 s/steel bolt. Removed wheel bearings from Roly Tilman alloy wheel. Inner bearing = FAG, outer = SKF, both in excellent condition. Top hat spacer needs to be polished up, and outer oil seal was hard as a rock. Requires new oil seals 25 x 35 x 7, and 25 x 38 x 7. Checked bearing play and wedding band spacer needs to be lapped to reduce the play. Filled cavity in wheel with newspaper in preparation for sand and bead blasting. 20 January 2009 0.5 Hours (Total = 348.75 hours) Jan Cornel purchased a battery for me (B49-6) from his local Battery Centre – I must collect from him (no acid). Jan Cornel says he has had a lot of trouble with ignition points from Uli‟s lately. 24 December 2013 Rev 1.1 65 Allan‟s BMW R50/2 Restoration (Abridged) 23 January 2009 0.5 Hours (Total = 349.25 hours) Disconnected front brake cable. Removed front wheel, removed front wheel bearings, and stripped brake drum. Prepared hub and brake backing plate for bead blasting. 24 January 2009 3.0 Hours (Total = 352.25 hours) Removed rear wheel, removed rear wheel bearings. Prepared rear wheel and hub for bead blasting. Rian Emerich bead blasted front wheel, rear wheel, front brake plate and Roly‟s wheel = ¾ hours. Washed and cleaned all three wheels and front brake backing plate to get rid of all traces of glass beads. Sprayed steel and iron surfaces with Q20 to prevent rusting. Fabricated a new (BMS) top hat spacer LHS for the rear wheel = 20mm bore, 25mm OD sealing surface and 30mm Φ collar, collar thickness = 1.5mm and total height of spacer = 14mm. Faced and cleaned the Roly Tilman wheel hub seal retainer. Note that the original rear wheel hub seal retainer (that was previously fitted with a 24 x 35 x 7 oil seal) has a bore of 35.5mm. The new 25 x 35 x 7 metal seal is a very loose fit in this retainer. I will use the Roly Tilman wheel hub seal retainer fitted with a new SB2 25 x 35 x 7, single lip oil seal. Measured thickness of brake drums: o Front wheel = 6.0mm o Rear wheel = 7.0mm o Roly wheel = 7.5mm Measured brake drum diameters: o Front wheel = 203mm o Rear wheel = 200.5mm o Roly wheel = 200.5mm Noted that spokes on (incorrect) front wheel cross with lots of space on one side of the wheel, but are touching on the other side. Also, some spokes appear to be bent. It may be preferable to use the Roly Tilman wheel and hub for the front wheel, with new spokes. The only other decision required is whether to use a steel rim or an alloy rim. 26 - 27 January 2009 1.0 Hours (Total = 353.25 hours) Removed spokes from Roly Tilman wheel. All the spokes are rusted and pitted. Measured rim/hub offsets: o Front wheel = 11.5mm (way too much!) o Rear wheel = 7.0 – 7.5mm o Roly wheel = 6.5 – 7.0mm Cleaned M4 threads in all the nipples with an M4 tap. Some nipples should be replaced. Polished the outer surfaces of the Roly Tilman alloy rim with Autosol. Note that this rim is marked “Akront”, and does not have the dents in the rim. 24 December 2013 Rev 1.1 66 Allan‟s BMW R50/2 Restoration (Abridged) 29 January 2009 1.0 Hours (Total = 354.25 hours) Went to Jan Cornel: o Returned his handlebar risers. o Bought 6V 3W globe and 2 x cable nipples o Collected B49 battery. o Took Roly brake hub and front wheel brake backing plate with brake shoes to Hercules Brake and Clutch for brake relining and drum skimming. Jan will collect on Friday. o Jan also asked me to turn 2 x s/steel washers, OD = 26mm o Jan says exhaust clamps & brackets not required o Jan says wheel offset = 5mm Filled B49 battery with about 0,5L battery acid. 30 January 2009 2.0 Hours (Total = 356.25 hours) Fabricated 6 x s/steel washers (OD = 25mm, ID = 10.5mm, t = 3mm) and buffed them. Two each are for Mike Lester and for Jan Cornel, and two are spares. 31 January 2009 4.5 Hours (Total = 360.75 hours) Charged battery @ 0.8A for 5 hours, to 6.76V fully charged. Polished Akront alloy rim on the buffing wheel and by hand with Autosol. Polished rear wheel BMW alloy rim by hand with Autosol. Removed tyre and tube from front wheel (steel rim). Stripped spokes from front wheel – note that the steel rim is incorrect for the bike (British). Straightened the 40 front wheel spokes. Wire brushed the spoke threads and cleaned them up with an M4 die. 1 February 2009 2.0 Hours (Total = 362.75 hours) Bought another rubber driveshaft boot from CMC. Bought 2 x carb pipes from CMC – one is for BMW R60/2. Saw Mike Lester at CMC, gave him 2 x s/steel washers for steering top plate mounting. Collected brake drum and relined brake shoes from Jan Cornel. Gave Jan Cornel 2 x s/steel washers for steering plate mounting. Jan Cornel gave me a piece of rubber for the battery tray. Cleaned about 30 Tilman spokes using the wire wheel. Cleaned threads of 20 selected Tilman spokes with M4 die nut. Cleaned threads of 30 front wheel nipples with M4 tap. Selected 40 spokes and nipples for re-chroming, 30 from original front wheel. 2 February 2009 0 Hours (Total = 362.75 hours) Took the following items to Sheffield Electroplating for re-chroming –two weeks lead time: o One steel wheel rim = R220 +VAT o 40 x spokes and nipples = R400 + VAT o 1 x aircleaner housing = R140 + VAT o 2 x hubcaps = R280 + VAT Christine cautioned that some spokes may be thinner, especially those that are half chromed. The acid will eat away the chrome, but also the steel. Sheffield quoted R380 to chrome both exhaust header pipes. Measured Roly brake drum after skimming. Thickness = 6.85mm, diameter = 201mm. 24 December 2013 Rev 1.1 67 Allan‟s BMW R50/2 Restoration (Abridged) 3 February 2009 0.0 Hours (Total = 362.75 hours) Ordered 40 x spokes and nipples from Uli‟s. Purchased 2 off 25 x 35 x 6 double lip oil seals from BMG 5 February 2009 0.0 Hours (Total = 362.75 hours) Purchased 3.50 x 18” Viper inner tube and rim tape from Randburg Motorcycles. Purchased 2 off 5.33 x 56.52mm O-rings from BMG (too small cross-section) 6 February 2009 0.0 Hours (Total = 362.75 hours) Purchased 6mm x 55mm O-ring from BMG. 7 February 2009 1.0 Hours (Total = 363.75 hours) Removed front brake cable and filed off the crimped steel nipple from the handle bar end. Turned a new brass nipple holder that fits in the brake lever = 8mm OD and 9mm long. Through hole = 4mm ID and recess = 6mm ID. Turned a new s/steel cable guide sleeve for the brake end of the cable to replace rust-pitted steel fitting = 9mm OD, stepped to 6mm OD, with a 2.5mm ID through-hole, and a recess = 6.2mm ID. Lengths the same as sample. Fitted end caps to the cable outer sheath and soldered one of Jan Cornel‟s brass nipples on the end of the cable. Note that cable outer length = 1000mm (spec = 1095mm) 8 February 2009 2.0 Hours (Total = 365.75 hours) Washed front brake backing plate in hot water and soap. Fabricated s/steel washer for front brake adjuster (ID = 8mm). Fabricated M8 x 1 s/steel nut (13mm AF) for front brake adjuster, as well as one spare M8 x 1 nut. Assembled front brakes. Fabricated a s/steel washer for front axle. 14 February 2009 0.5 Hours (Total = 366.25 hours) Polished Akront alloy rim on the buffing wheel and by hand with Autosol, again. 16 February 2009 0.0 Hours (Total = 366.25 hours) Collected set of 40 spokes (from Uli‟s) from Thomas Schmidt of R&S. Discovered that the spokes are incorrect = too short at 120mm. Arranged to return spokes to Thomas Schmidt. 17 February 2009 0.5 Hours (Total = 366.75 hours) Replaced hose clamps for driveshaft rubber bellows with two BMW clamps obtained from Jean of House of BM. 24 December 2013 Rev 1.1 68 Allan‟s BMW R50/2 Restoration (Abridged) 18 February 2009 0.0 Hours (Total = 366.75 hours) Returned incorrect spoke set to Uli‟s.. Sent e-mail to Uli requesting confirmation of the correct part number for 140mm x M4 spokes. 20 February 2009 0.5 Hours (Total = 367.25 hours) Collected chromed parts from Sheffield. Fitted air filter assembly. Had to remove the thin, large diameter O-ring between the dome and the base to ensure that the air filter sits tight between the upper and lower O-rings. Idle air screws appear to be a loose fit in the carb bodies. Initial idle mix setting is 2 turns out. Unusual thread = M7 x 0.75 21 February 2009 2.5 Hours (Total = 369.75 hours) Washed and steel brushed new front hub (ex Roly). Started lacing front wheel using hub ex Roly and Akront alloy rim ex Roly. To ensure the correct offset, I placed 6.5mm thick spacers under the rim with the hub brake-side down. Holes on the Akront rim are larger diameter than the nipples. So far, 7 x re-chromed spokes are unserviceable due to increased nipple thread diameter – the spokes pull straight through the threaded nipples. Obviously, Sheffield did not protect the nipple threads from the Hydrochloric acid (HCl attacks the zinc in the brass aggressively!) Replaced unserviceable spokes and nipples with the set of ten best spokes and nipples that I did not send for re-chroming. Need to purchase 30 more spokes and nipples from Uli‟s. 24 February 2009 0 Hours (Total = 369.75 hours) Holger at Uli‟s telephonically confirmed that no e-mails had been received from me (possibly in SPAM box) and that their correct part number for 140mm x M4 spokes & nipples is 6044, and that they will exchange spokes and nipples with part number 21044. 13 March 2009 0 Hours (Total = 369.75 hours) Collected 70 x spokes & nipples from Casper. 24 December 2013 Rev 1.1 69 Allan‟s BMW R50/2 Restoration (Abridged) 14 March 2009 4 Hours (Total = 373.75 hours) Removed tyre and tube from rear wheel. Removed spokes and cleaned masking tape from wheel well. Buffed BMW OEM alloy rim and polished with Autosol. Dismantled wheel using Akront rim and re-chromed spokes. Using the ex-Roly Tilman hub with the skimmed brake drum and the BMW alloy rim (ex rear wheel), laced front wheel with 30 x new spokes and nipples from Uli‟s and 10 old spokes and nipples. Centred hub in rim using a rule to within 0.5 mm, with uniform offset of about 6.5mm. 15 March 2009 0 Hours (Total = 373.75 hours) Bought aluminium dome nut for rear swingarm from Piston Ring Swap Meet. 16 March 2009 0.5 Hours (Total = 374.25 hours) Had rear brake shoes fitted with new bonded linings and brake drum skimmed, at CBF in Strijdom Park (same day service). They appear to have bruised the bearing seat on the opposite side to the brake drum and the skimmed surface is ridged – looks like chatter. Brake shoes have been sand-blasted, one lining is too narrow for the shoe. Measured rear brake drum diameter after skimming = 201mm. Wire-brushed rear brake shoes by hand. 19 March 2009 1.5 Hours (Total = 375.75 hours) Laced rear wheel using chromed steel rim and 40 new spokes and nipples from Uli‟s. Refitted newly bonded brake shoes to rear hub. Centred hub in rim using a steel rule to within 0.5 mm, with uniform offset of about 6.5mm. 21 March 2009 1.5 Hours (Total = 377.25 hours) Tightened spokes on both front & rear wheels using spoke wrench. Fitted bearing assemblies to both wheels. Adjusted front brake adjuster to suit new brake shoes and the skimmed brake drum. 27 March 2009 0.5 Hours (Total = 377.75 hours) Mounted rear wheel on bike and measured runout with a dial indicator as follows: o Lateral = 0.2mm – 1mm = 0.8mm. o Radial = 1mm – 3mm = 2mm 28 March 2009 3.5 Hours (Total = 381.25 hours) Purchased rim tape from Randburg Motorcycles. Fabricated spoke wrench from 12mm diameter MS bar 75mm long. Milled 5.75mm slot, knurled handle. (This tool was too weak and was re-made using 13mm hex bar – see 29 Mar 2009. This tool also broke and was remade using 16mm Φ EN8 – see 2 Oct 2010). Tightened spokes and adjusted rear wheel runout as follows: o Lateral = 0.8mm o Radial = 1mm Wheel offset = 6.5mm – 7.0 mm 24 December 2013 Rev 1.1 70 Allan‟s BMW R50/2 Restoration (Abridged) Fitted rim tape, new tube and tyre to rear wheel, inflated to 180kPa. Fitted inner and outer oil seals to rear wheel hub, and fitted hubcap. Removed and displaced rear brake lever on hub by one spline, re-fitted lever. Lever is now closer to a right angle when foot brake lever is actuated. Greased drive splines and re-fitted rear wheel, assembled rear mudguard. 29 March 2009 4.5 Hours (Total = 385.75 hours) Fabricated another spoke wrench from 13mm hex MS bar 75mm long. Milled 5.75mm slot, knurled handle. Tightened spokes and adjusted front wheel runout as follows: o Lateral = 0.5mm o Radial = 0.8mm o Wheel offset = 6.0mm – 6.5mm Fitted rim tape, new tube and tyre to front wheel, inflated to 180kPa. Fitted inner and outer oil seals to front wheel hub, and fitted hubcap. Re-fitted front wheel to bike. Removed and displaced rear brake lever on front hub by a few splines to result in a distance between levers of about 190mm, re-fitted lever. Re-fitted front brake cable and adjusted free-play. 7 April 2009 1.0 Hours (Total = 386.75 hours) Fabricated a new adjuster nut for front brake lever using 10mm AF hex s/steel, turned down to 9.8mm Φ for a distance and drilled and tapped M6 x 1. Milled half-moon shape in the end of the nut using a 10mm end mill. Fitted the new s/steel nut to the front brake cable, and adjusted front brake free play. 18 April 2009 2.5 Hours (Total = 389.25 hours) Fabricated 2 x stainless steel special nuts for generator front cover, using 16mm Φ bar, turned down to 14mm Φ for circular collar (2,5mm wide), then down to 10mm Φ for main body. Turned a recess for the retaining wire clip at the end of the 10mm Φ shank. Drilled 5mm Φ, and threaded M6 x 1 and milled 10mm AF hex on ends. 24 December 2013 Rev 1.1 71 Allan‟s BMW R50/2 Restoration (Abridged) 25 April 2009 2.0 Hours (Total = 391.25 hours) Tightened exhaust manifold nuts with a “C” spanner. Removed the generator front cover. Set contact breaker points gap to 0.4mm. (The base plate was loose and rotated, so I had to tighten the screws holding the base plate). To tighten the base plate I had to remove the advance mechanism. Replaced slotted M4 screw on contact breaker base plate Turned engine to align “S” mark with the mark on the crankcase. Loosened the two nuts holding the magneto base plate and rotated the base plate until the scribed line on the rotating magnet lined up with the bottom of the “V” notch on the brass base plate. Disconnected the coil wire from the contact breaker points and clipped leads for a test lamp across the breaker points and a 12V battery. Set the static ignition timing by rotating the points base such that the test lamp extinguishes just as the “S” mark aligns with the mark on the crankcase as the engine is turned slowly. I rotated the contact breaker base plate as far clockwise as possible, and then had to widen the contact breaker points gap a slight amount (0.45mm) to get the static ignition timing spot on. Note that rotation of the contact breaker base plate requires removal of the advance mechanism to get to the base plate screws. Reconnected the coil wire to the contact breaker points and re-fitted the generator front cover. 27 April 2009 2.0 Hours (Total = 393.25 hours) Pumped tyres = 200kPa front and rear. Loosened LHS float cover and removed LHS carb float. Unsoldered old piano wire from float, bent new piano wire (0.8mm) to fit, and soldered onto float. Filled LHS float bowl with petrol and refitted float cover. Loosened RHS float cover and removed float (was in upside down) and filled float chamber with petrol. Refitted float cover. Fitted battery. Checked that all electrical circuits are working. Tried to start „bike – no joy. Checked for spark = none at plugs. Measured resistance of plug wires and found that spark plug caps have internal resistance of 5k ohms. Removed spark plug caps and attached pieces of wire between plug leads and spark plugs. Verified that there is a weak spark. Removed generator front cover and removed condenser to use as a sample for a new one. Applied some Shell Retinax HD grease to ignition points cam. Refitted front generator cover. Removed front wheel to access surface rust under the fixing bolt for the fender bow. Removed surface rust and coated with paste wax before refitting bolt and washer. Refitted front wheel. 30 April 2009 0.0 Hours (Total = 393.25 hours) Purchased new Echlin EP258 condensor from Blitz Motor Spares. 1 May 2009 0.5 Hours (Total = 393.75 hours) Fitted new Echlin EP258 condensor. Tried to start „bike – no joy! 24 December 2013 Rev 1.1 72 Allan‟s BMW R50/2 Restoration (Abridged) 2 May 2009 0.5 Hours (Total = 394.25 hours) Fitted temporary spark plug caps (twisted wire) and managed to start the „bike for the first time!!! It ran until the fuel in the float chambers ran out. The ignition cutout still does not work (earthing of the magneto). One potential problem observed was that the nose of the camshaft (axis for the magneto advance mechanism) is running out of true by a substantial amount. The effect of this on the ignition timing will need to be verified with a timing light. (Not much!) The centre stand is inhibited from rising to its stop position by the LHS exhaust silencer. The problem is not the silencer, but the LHS header pipe that does not fit properly – catching on the frame at the front engine mounting point, in the way of the gear shift lever, does not mate well with the balance tube. 3 May 2009 1.0 Hours (Total = 395.25 hours) Visited CMC, bought throttle cable perch gear cover. Obtained 1 x 6V 2W lamp, 1 x 6V 3W lamp, 1 x ignition condenser, 1 x magneto advance retaining bolt. Bob Harpin to scan Clymer Workshop manual for R50/2, as well as the Haynes Twins Workshop manual for /5/6/7s. Visited Jan Cornel, obtained 9mm advance spring. Fabricated a points setting tool (17.5mm OD, 12mm ID, leaded free-cutting mild steel). Confirmed points setting = 0.45mm. Checked advance mechanism – both centrifugal weights appear to be firmly sprung in the rest position. Removed ignition points baseplate, cleaned in Benzine and reversed felt on rubbing block so that the clean, unworn side rubs against the points cam – attached with small Aluminium pop rivet. Elongated points baseplate mounting holes with a round file to obtain more advance. Filed stationary side of ignition points contact flat with diamond file, and fitted new Bosch moving contact arm. Refitted baseplate and points. Set points gap to 0.4mm using my new points gap setting tool. This resulted in static ignition timing about 10mm retarded from the “S” mark, so the points gap was reset to 0.45mm to result in timing spot-on the “S” mark. However, there is now no room for further advancing the ignition timing unless I elongate the base plate mounting holes some more, or widen the points gap to 0.5mm. I also tried to see if the nose of the magneto rotor is out of true by checking the points gap using the new tool and rotating the engine. If it was out, it was almost impossible to measure with a feeler gauge. I will try with a dial indicator later. 5 May 2009 0.5 Hours (Total = 395.75 hours Drove to NGK at Jet Park to collect 2 x LZFH spark plugs caps (as free samples) from Giles Palmer, Technical Manager. Fitted new NGK spark plug caps. 9 May 2009 1.0 Hours (Total = 396.75 hours) Connected magneto and condenser wires to ignition points, cleaned voltage regulator contacts, and checked generator brushes (they were only contacting the commutator in a very small area – need to bed in properly). Started the „bike and checked dynamic timing with inductive pick-up timing light (separate 12V battery). At idle speed, the timing marks are aligned with the “S” mark, and as speed is increased the marks align with the “F” mark, but also move beyond the “F” mark at higher revs. The centrifugal advance springs will need to be adjusted to limit the advance to the “F” mark. At idle speed there appear to be two separate timing marks about 6mm apart. This differential timing is small enough not to be concerned about. 24 December 2013 Rev 1.1 73 Allan‟s BMW R50/2 Restoration (Abridged) The generator light now extinguishes at speed above idle, and the charging system appears to be operating correctly. Refitted front generator cover. Oil leaking from RHS cylinder/head. 10 May 2009 1.0 Hours (Total = 397.75 hours) Removed RHS tappet cover, cleaned gasket mating surfaces and applied a thin layer of Hylomar along the bottom face of the cylinder head. Refitted the tappet cover. There were a few metal particles in the residual oil in the tappet cover – probably left over from the machining and installation process. (Still leaking oil, from both cylinder heads!) Removed the centrifugal advance mechanism and bent the stop spring to limit the maximum advance. Refitted the centrifugal advance mechanism. Swapped the spark plug leads on the magneto coil. Started the „bike – first kick! Checked timing at idle with timing light = spot on, and still two lines about 6mm apart. Didn‟t rev high enough to get to the “F” mark (it may be limiting before it gets to the “F” mark). 14/15 May 2009 0.0 Hours Total = 397.75 hours) Surmised (wrongly!) that the oil is leaking from the cylinder head junction because the cylinder heads must have been skimmed in the past, allowing the ridge on the cylinder to make contact with the depression in the cylinder head. Jan Cornel confirmed that there needs to be a small gap between the cylinder ridge and the head, and that the gasket needs to form the primary seal. He suggested that the cylinders be removed and the ridge machined down to suit. David Cain at MPPE suggested that I remove the head and gasket, and then replace the head without the gasket, but with some short pieces of solder wire between the surfaces. Remove the head and measure the thickness of the flattened solder wire. Also measure the height of the cylinder ridge, the depth of the depression in the cylinder head, and the gasket thickness. Allow 10% – 15% for gasket crush when calculating amount to machine off the ridge. 16 May 2009 6.5 Hours (Total = 404.25 hours) Removed both cylinder heads, replaced them without the gaskets and with short pieces of solder wire at top and bottom, and took the following measurements: MEASURED Cylinder ridge height Cylinder head recess Gasket thickness Solder wire Available crush Head bolt length (effective) Cylinder head depth RHS Top = 3.62mm Bottom = 3.71mm Top = 3.52mm Bottom = 3.42mm Steel rim = 1.17mm Other = 1.01mm Top = 0.46mm Bottom = 0.49mm 1.01 – 0.49 = 0.52mm 108 – 25mm = 83mm 88mm LHS Top = 3.59mm Bottom = 3.51mm Top = 3.45mm Bottom = 3.44mm Steel rim = 1.15mm Other = 1.0mm Top = 0.38mm Bottom = 0.34mm 1.0 – 0.38 = 0.62mm 108 – 25mm = 83mm 88mm Filed lower end of RHS cylinder ridge to result in a height of 3.51mm. 24 December 2013 Rev 1.1 74 Allan‟s BMW R50/2 Restoration (Abridged) Used a piece of galvanised wire to confirm that oil can drain back into the crankcase down the small tubes at the lower ends of the cylinder heads. Scraped recesses in cylinder heads with M&W scraper - minimal. Flatted both cylinder head mating surfaces on 320 grit water paper on my granite surface plate. They were both a bit low around the oil return holes. Flatted carburettor flanges on 320 grit water paper on my granite surface plate. Replaced cylinder heads and gaskets and torqued oiled head bolts to 35Nm in 3 stages (= 40Nm on my torque wrench). Clamped rockers to minimise end play. Ensured that the cylinders were at TDC on the compression stroke (valves closed) before torqueing the head bolts. Applied CopaSlip paste to exhaust port threads and tightened exhaust nuts. Adjusted inlet tappets to 0.15mm and exhaust tappets to 0.20mm and refitted tappet covers. LHS exhaust header needs to be remade – the stub tube for the balance tube is pointing downwards and is also not opposite the stub for the RHS exhaust header, and the header pipe is hard up against the frame (front engine mounting bolt). It is obvious from the foregoing that my initial supposition was incorrect – the cylinder ridge is NOT preventing the gasket from being crushed sufficiently to form an effective seal. On both cylinders, there was more than 0.5mm available to crush the head gaskets. Furthermore, there is sufficient movement on the cylinder head bolts (88mm – 83mm = 5mm) to torque the heads down effectively before the bolts bottom in the cylinder threads. One possibility may be that the steel bolt guides in the cylinder heads had loosened when the heads were heated to replace the valve guides, and had not settled into position when the cylinder heads were fitted the first time. Another possibility may relate to the much increased compression ratio due to the use of R50S pistons and skimmed heads. Duane Ausherman‟s “butter heads” may also be the cause of the oil leaks. (Not true) Started and ran the „bike twice for a few minutes each time. 17 May 2009 0 Hours (Total = 404.25 hours) RHS head gasket still leaking oil!! 21 May 2009 0 Hours (Total = 404.25 hours) Phoned Jan Cornel again about head gasket leak. He confirmed that his new gaskets also have the metal reinforcing rim around the bore. He confirmed head bolt torque = 35 Nm. Phoned Hennie van Niekerk re head gasket leak. He said that a lot of Uli‟s spares are becoming problematic. He now cleans mating surfaces with Meths and applies gasket sealer to both sides of the head gasket before fitting. He confirmed head bolt torque = 25 ft-lb, and that he does not loosen bolts before retorqueing. 24 December 2013 Rev 1.1 75 Allan‟s BMW R50/2 Restoration (Abridged) Hennie suggested that the oil could be coming past the rings (before they seat properly) and then past the gasket – I need to check this! Note that when I removed the head and gasket, there was no sign of oil leaking from the bore to the outside – the only sign of oil leaking was from the vicinity of the return oil galleries. I also did not see any sign of oil bubbling (with lost compression) when the „bike was running, and there is no smoke from the exhaust. 23 May 2009 0.5 Hours (Total = 404.75 hours) Removed RHS tappet cover and checked head bolt torque = 35 Nm (40Nm on my torque wrench). No movement. Topped engine oil up with 0.25 litre. Still leaking oil. 21 June 2009 1.5 Hours (Total = 406.25 hours) Removed ignition points base plate and elongated mounting slots with a round file. Checked timing again with timing light = almost perfect on “S” mark and “F” mark. Still differential timing = 6mm apart. The magneto HT terminal on the LHS was sparking to ground every now and then – cut the ends of the crimped bootlace ferrules for the HT leads = no more sparking to ground. Checked tyre pressures = 190kPa front & rear. Removed oil dipstick after running for a while = no positive crankcase pressure. I also checked that the crankcase breather is working while the engine is running. „Bike started on the first kick late in the afternoon, and idles well. RHS head gasket still leaking oil!! 26 July 2009 1.0 Hours (Total = 407.25 hours) Fabricated knurled clutch cable adjuster locknut from 20mm Φ s/steel, 5mm thick, tapped 5/16” BSW. 29 July 2009 0 Hours (Total = 407.25 hours) Ordered 2 x cylinder head gaskets from Northside M/C at R36-70 each (10 day lead time). 27 August 2009 Collected cylinder head gaskets and air filter element from Northside Motorcycles. Gaskets are composite 1mm thick with no metal reinforcing. 29 August 2009 1.5 Hours (Total = 408.75 hours) Removed slide from RHS carburettor, RHS tappet cover and cylinder head. Rotated the engine to ensure that the RHS cylinder was at TDC on the compression stroke (both valves closed and valve pushrods loose when rotated). It appears that the Uli‟s cylinder head gasket is not sealing properly – the metal collar around the bore of the gasket appears to be preventing the gasket from sealing at the lower end. Both sides of the Uli‟s gasket were wet with oil in the vicinity of the oil return hole, spreading widely to the space between the lower bolt holes. Oil was also visible in the lower portion of the combustion chamber – possibly due to the non-sealing of the gasket. The new BMW OEM gaskets do not have the metal collar around the bore of the gasket. 24 December 2013 Rev 1.1 76 Allan‟s BMW R50/2 Restoration (Abridged) Chamfered all 4 cylinder head bolt hexagons in the lathe. The spotfacing on the rocker shaft supports/towers has receded causing the corners of the hex heads to catch on the spotfacing. This may also have prevented the bolts from reaching the correct torque. Used a pointed rod to ensure that the oil return hole is clear at the cylinder base gasket. Fitted the new BMW OEM gasket, replaced the cylinder head and torqued oiled head bolts to 35Nm in 3 stages (= 40Nm on my torque wrench). Ensured that the cylinder was at TDC on the compression stroke (valves closed) before torqueing the head bolts. Tightened exhaust nut. Adjusted inlet tappet to 0.15mm and exhaust tappet to 0.20mm with the cylinder at TDC on the compression stroke, oiled the rocker shafts and refitted the tappet cover. 30 August 2009 0 Hours (Total = 408.75 hours) Started and ran the „bike twice. LHS exhaust header requires quite a bit of work to get all the parts to line up. 31 August 2009 0 Hours (Total = 408.75 hours) Success!! There was no oil leak under the RHS cylinder after a full day. It seems that the root cause of the leak was the corners of the hex cylinder head bolts interfering with the torque readings, or a combination of both reasons. 6 September 2009 1.5 Hours (Total = 410.25 hours) Purchased 10 litres of petrol and filled the fuel tank with about 7 litres. The RHS carb leaked fuel from the float chamber cover as soon as the fuel cock was opened. Removed float chamber cover from RHS carb, removed pivot pin from float lever, removed needle, and cleaned dirt out of seat. Replaced pivot pin and checked and adjusted float lever height (22mm - +4mm). Replaced float chamber cover and confirmed that the needle and seat are working satisfactorily – no more leaks. Started the „bike and ran it for a short while, then noticed a drop of oil on the paving under the LHS cylinder head, and a film of oil under the cylinder head mating face. Removed slide from LHS carburettor, LHS tappet cover and cylinder head. Rotated the engine to ensure that the LHS cylinder was at TDC on the compression stroke (both valves closed and valve pushrods loose when rotated). 24 December 2013 Rev 1.1 77 Allan‟s BMW R50/2 Restoration (Abridged) There was some blackish sediment in the tappet cover. Oil was again present on both sides of the Uli‟s gasket around the oil return hole indicating a failure to seal properly. Chamfered all 4 cylinder head bolt hexagons in the lathe. The spotfacing on the rocker shaft supports/towers has receded causing the corners of the hex heads to catch on the spotfacing. This may also have prevented the bolts from reaching the correct torque. Fitted the new BMW OEM gasket, replaced the cylinder head and torqued oiled head bolts to 35Nm in 3 stages (= 40Nm on my torque wrench). Ensured that the cylinder was at TDC on the compression stroke (valves closed) before torqueing the head bolts. Tightened exhaust nut. Adjusted inlet tappet to 0.15mm and exhaust tappet to 0.20mm with the cylinder at TDC on the compression stroke, oiled the rocker shafts and refitted the tappet cover. Started the „bike and ran it again for a short while without problems. 7 September 2009 0.0 Hours (Total = 410.25 hours) Phoned Jan Cornel re exhaust headers, etc Jan says it is better to purchase exhaust headers from overseas because the local people cannot make the tight bends correctly. Jan also said the gear lever can be bent upwards (and outwards), either by hand (in 2nd gear), or in the vice, to clear the LHS exhaust pipe. Checked the „bike for oil leaks – none at this stage! 24 December 2013 Rev 1.1 78 Allan‟s BMW R50/2 Restoration (Abridged) 4 October 2009 0.0 Hours (Total = 410.25 hours) Went to CMC. Hennie van Zyl will check if has any generator covers lying around. He thinks he has, but they will all need some welding and repairs. He said he would give me one for gratis. I must phone him later this week. Visited Jan Cornel. He does not have a generator cover, but he will ask Hennie Dormehl if he has one. Also purchased a good steel wheel rim from Jan, as well as the (early 1950 – 1954) handlebar risers. 5 October 2009 0.0 Hours (Total = 410.25 hours) Purchased 2 x M8 x 30 s/steel capscrews, 4 x M8 x 30 s/steel hex screws, 2 x M10 x1 nuts, JKM. 10 October 2009 2.0 Hours (Total = 412.25 hours) Removed old handlebar risers and stainless steel spacer from steering damper knob. Wire-brushed M10 x 1 threads on the new risers from Jan Cornel (for the early 1950 – 1954 „bikes), then cleaned them up with a die nut. Fitted the new handlebar risers from Jan Cornel using new mild steel nuts (M10 x 1). Turned raised letters off M8 x 30 s/steel bolt heads and polished them on the buff wheel. Fitted polished bolts to handlebar clamps. The new handlebar risers result in the handlebar touching the steering damper knob. 15 October 2009 0.0 Hours (Total = 412.25 hours) Melville Price called from Queenstown. He saw my advert in Kickstart magazine for handlebar risers. He has a spare set off a 1958 „bike, he will swap for taillight chrome bezel, or taillight bulb holder. His risers need chroming. 18 October 2009 0.5 Hours (Total = 412.75 hours) Bent gearlever (outwards) to clear exhaust pipe. Tried to synchronise carburettor throttles by adjusting cable lengths to result in simultaneous movement of slides. Started and ran ‟bike for short periods. Collected 2 x mirrors from Jan Cornel, also „bike registration procedure. Jan will try to find used taillight chrome bezel for me to swap with Melville in Queenstown for R50/2 handlebar risers. 19 October 2009 0.0 Hours (Total = 412.75 hours) Jan Cornel called to inform me to fit sturdy 10mm diameter washers between the nuts for fitting the mirrors. I will use stainless steel washers. Jan also confirmed that he has managed to find me a taillight chrome bezel (from his friend) that he will let me have. The chrome bezel has a slight dent in it and will be delivered to Jan on Tuesday evening. I phoned Melville Price in Queenstown to inform him that I have sourced a chrome bezel for him and that I would like to swap it for his risers. I requested him to take a photo of his risers and e-mail to me, which he did. 24 December 2013 Rev 1.1 79 Allan‟s BMW R50/2 Restoration (Abridged) 25 October 2009 0.5 Hours (Total = 413.25 hours) Removed generator cover and removed advance mechanism from magneto rotor spindle. Earthed the points with a fly lead to prevent firing. Measured runout on magneto rotor spindle with dial test indicator = < 0.03mm (~1 thou”). The head of the Allen capscrew that retains the advance mechanism on the magneto rotor spindle has a much larger runout, but this is not due to the capscrew. Measured concentricity of the capscrew shank and head in the lathe = very good. Replaced advance mechanism on magneto rotor spindle and replaced generator cover. Adjusted both idle speed screws to 1 turn in. Checked tyre pressures: front = 170kPa, rear = 160kPa (suspect slow leak in rear tube) 1 November 2009 0.0 Hours (Total = 413.25 hours) Visited Jan Cornel. Jan gave me a taillight rim he obtained from his friend in quite good condition = gratis. He also lent me some ignition points to try on my „bike. Sent e-mail to Melville with pictures of the taillight rim. 6 November 2009 0.0 Hours (Total = 413.25 hours) Melville confirmed he is happy with the taillight trim ring, but he wants me to have it re-chromed when I have the risers re-chromed – he said he will pay. Arranged with Melville to deliver the risers to East London for collection on Saturday 12 November 2009 0.0 Hours (Total = 413.25 hours) Collected handlebar risers (ex Melville Price). 15 November 2009 0.0 Hours (Total = 413.25 hours) Melville Price called with contact details for Powerflow in Durban. He was quoted R1300-00 + VAT for a set of polished stainless steel headers, excludes the manifold nuts. 19 November 2009 0.0 Hours (Total = 413.25 hours) Sanna undertook to phone me re Delivered parts to African Electroplating for re-chroming. completion date (2 weeks) and price. o 2 x handlebar risers o 2 x riser clamp bolts o 2 x M10 x 1 nuts (to be zinc/cad plated only) o 2 x M8 x 1 nuts (to be zinc/cad plated only) o 1 x taillight rim (for Melville Price) o 3 x valve pushrod tubes 24 December 2013 Rev 1.1 80 Allan‟s BMW R50/2 Restoration (Abridged) 22 November 2009 0.5 Hours (Total = 413.75 hours) Loosened handlebar riser nuts. Removed battery, charged battery (6.48V no load) for a short while, cut a rubber base for the battery, replaced battery on new rubber base. Top triple plate will need to be resprayed. 7 December 2009 0.0 Hours (Total = 413.75 hours) Gave Piet B cash for procurement of spares from Uli‟s. Delivery is expected today in Munich and Piet says he should deliver to me on Friday 11 December. African Electroplating called to inform my parts are ready for collection. 8 December 2009 0.0 Hours (Total = 413.75 hours) Collected re-chromed parts from African Electroplating. Note that all the parts were re-chromed, even the nuts. Estimate that taillight rim re-chroming = R80-00 12 December 2009 1.0 Hours (Total = 414.75 hours) Removed steering damper, steering column nut, and removed top triple plate. Scraped all layers of paint from triple plate, sanded flat with production paper, wiped with lacquer thinners and coated with Duram Metcote NS5 etch primer. Flatted with 400 grit water paper. Removed top engine stay (bracket), as well as fuel tank mounting bracket. Flatted both with 400 grit water paper. 14 December 2009 1.0 Hours (Total = 415.75 hours) Beadblasted and prepped old Bosch horn. Cut new paper gaskets. Turned rusted parts in lathe. Sprayed horn components with grey lacquer primer. Sprayed Black Limo topcoat on horn components. Assembled horn using s/steel screws. Tested old Bosch horn – draws a lot of current with very little sound! 15 December 2009 0.0 Hours (Total = 415.75 hours) Piet B delivered spares from Uli‟s (missing 2 x M7x0.75, 9mm AF nuts for carb air screws). 16 December 2009 4.5 Hours (Total = 420.25 hours) Fabricated 2 x M7x0.75, 9mm AF nuts for carb air screws using 10mm hex stainless steel. Milled 0.5mm off each flat of 10mm hex s/steel bar. Drilled 6.3mm hole, tapped M7 x 0.75, parted-off 3.5mm thick. Faced & chamfered edges. Removed old nuts from carbs and fitted new nuts. Spray-painted top triple plate, upper engine mounting bracket and lower fuel tank bracket with 2K filler primer (4:1 mix with hardener and a little thinners = 40mL + 10mL + 5mL). Let dry for an hour and then flatted with 400 grit water paper. Set regulator on compressor to 300kPa, used gravity feed spraygun. 24 December 2013 Rev 1.1 81 Allan‟s BMW R50/2 Restoration (Abridged) Spray-painted top triple plate, upper engine mounting bracket and lower fuel tank bracket with 2K Black topcoat (2:1 mix with hardener and a little thinners = 30mL + 15mL + 5mL). Set regulator on compressor to 200kPa, used gravity feed spraygun. Let Black topcoat dry for 2 hours and then flatted with 2000 grit water paper, and polished with Wynns Restore and Rally car wax. Refitted fuel tank lower bracket and top engine mounting bracket. Removed old handlebar risers, and fitted newly chromed risers. Refitted top triple plate, handlebar risers loosely to avoid damaging paint on triple plate. 17 December 2009 0.5 Hours (Total = 420.75 hours) Removed handlebar and risers from triple plate. Tightened 36mm AF nut on steering head to clamp on triple plate. Tightened 19mm AF nuts clamping top plate to forks. Refitted handlebar & risers to triple plate. Tightened 17mm AF nuts clamping risers to triple plate. Refitted steering damper and fitted split pin. Adjusted angle of handlebar as well as perches. 23 December 2009 0.0 Hours (Total = 420.75 hours) Visited Jan Cornel. Purchased a new 6V horn from Jan. 24 December 2009 3.5 Hours (Total = 424.25 hours) Fitted new 6V horn using s/steel screw & nut. Tested = OK. Flatted paint on frame with 2000 grit water paper and polished to shine. Fabricated 2 x spark plug extensions (for shorting out plugs when tuning), using 2 x 44mm lengths of 6mm AF hex plated mild steel, with one end turned and threaded M4 for about 10mm, and the other end drilled and tapped M4. Fabricated wheel hub pin spanner, using 4 x M6 x20 capscrews on 44mm diameter circle, turned down to 4mm dia on the ends, steel plate 8mm thick, bored 13mm diameter and turned OD = 60mm. Welded 22mm AF nut on the steel plate. Sprayed grey primer undercoat followed by a coat of machinery grey spraypaint. Supplied with galvanised M12 bolt, nut and 2 x washers. 27 December 2009 0.5 Hours (Total = 424.75 hours) Reset idle speed screws on both carbs = 1 turn in. Adjusted cable length on LHS carb to result in almost simultaneous lifting of carb slides. Started bike and ran for a few minutes only. 24 December 2013 Rev 1.1 82 Allan‟s BMW R50/2 Restoration (Abridged) 28 December 2009 0.5 Hours (Total = 425.25 hours) Fabricated hollow drift for adjusting seating of valve pushrod tubes from 20mm dia conduit. Cut a length (170mm) conduit, slit the tube for a length of 45mm and cut half the circumference at 60 deg. Deburred all cut edges. 10 February 2010 2.0 Hours (Total = 427.25 hours) Took one tappet cover to Aerotig (Charlie Hamer) to weld one fin. Fettled welding, used milling machine, die grinder, file and scraper. Bead blasted tappet cover. 3 March 2010 0.0 Hours (Total = 427.25 hours) Telephoned Krish at Powerflow in Durban. He confirmed s/steel headers = R1300 + VAT, plus postage or shipping to me. They do not deal with other branches. Procedure = place order, they manufacture, when ready for shipping they provide invoice. Effect payment and they will ship/post. Manufacture takes up to 2 weeks. 7 March 2010 2.0 Hours (Total = 429.25 hours) Purchased 2 x 18” and 2 x 19” rim tapes from CMC (ex Errol Cowan estate). Fabricated 2 x s/steel (304) flat washers for front axle. OD = 25mm, ID = 14.3mm, 3.5mm thick, chamfered, deburred and polished on the buffing wheel. Fabricated 3 x 22mm hex nuts (M14x1.5) for front & rear axles. Milled a section of 25mm Φ 304 s/steel bar to 22mm hex and sawed off 5 pieces 9mm thick. Faced the flat sides in the lathe to a nominal 8.5mm, centre drilled, drilled 5mm pilot hole, then 8mm, then 12.5mm (tapping size for M14x1.5). Countersunk the bores and chamfered the corners. Tapped holes M14x1.5 using the lathe initially to align the tap, then in the bench vice. Deburred and flatted all faces on 400 grit water paper. Polished on the buffing wheel. Replaced both old axle nuts with the new s/steel nuts, fitted new s/steel washer on front axle. 13 March 2010 1.0 Hours (Total = 430.25 hours) Fabricated s/steel (304) flat washer for rear axle. OD = 32mm, ID = 14.3mm, 4.0mm thick, chamfered, deburred and polished on the buffing wheel. Removed old rear axle flat washer and replaced with the new s/steel washer. Started bike and ran it for short while. Bike would not idle and LHS did not appear to be running as well as the RHS. RHS cylinder head hotter than LHS. Removed both carburettors and checked for blockages. The idle jet on the LHS carburettor was blocked. Checked float levels and replaced carburettors. 14 March 2010 0.0 Hours (Total = 430.25 hours) Started „bike on second kick, ran beautifully! Idles well. Both cylinders getting equally hot. 24 December 2013 Rev 1.1 83 Allan‟s BMW R50/2 Restoration (Abridged) 27 March 2010 0.0 Hours (Total = 430.25 hours) Visited Jan Cornel. Jan has the following /2 spares available: o R50 engine case, very good condition o Rear swing arm and driveshaft, good o Separate driveshaft, good o Final drive, case cracked – needs welding o Tappet covers, new o Gearbox spares (except kickstart gears) 10 April 2010 1.0 Hours (Total = 431.25 hours) Fabricated T-handle pin spanner for rear swing arm adjusters. 3 May 2010 0.0 Hours (Total = 431.25 hours) Telephonically ordered a set of s/steel exhaust headers from Powerflow in Durban (Krish Naicker). Takes about 2 weeks from date of order. Followed up with an e-mail to pflowbikes@hotmail.com. 8 May 2010 0.5 Hours (Total = 431.75 hours) Removed bench seat, and refitted seat with side brackets between the rear mudguard and the mounting points on the rear suspension towers. Seat is now firmly attached and follows the contours of the mudguard more closely for a better visual effect. Attempted (unsuccessfully) to set carburettors. The LHS mixture adjustment is effective, but adjustment of the mixture screw on the RHS does not result in much difference. This is possibly due to a restriction in the idle jet, or the #35 idle jets need to be replaced with #40 jets. 10 May 2010 1.0 Hours (Total = 432.75 hours) Removed RHS carb and unscrewed idle jet. Removed blockage from idle jet, and replaced carb. Tried to set carbs again, but still the RHS idle air screw does not seem to have much effect. This could be because the LHS carb is still too “dominant” and the idle speed adjusting screw needs to be turned out on the LHS carb. Tried again to set the carbs. Achieved much success by adjusting the throttle cable length on the RHS carb with the engine running on part throttle. This resulted in a marked increase in speed and much smoother running (less vibration). 14 May 2010 0.0 Hours (Total = 432.75 hours) Visited Roly Tilman and obtained another carb float and an idle stop screw. Replaced float and idle stop screw on RHS carburettor. Noted that the idle stop screw is the same length as the old one. 24 December 2013 Rev 1.1 84 Allan‟s BMW R50/2 Restoration (Abridged) 27 May 2010 0.0 Hours (Total = 432.75 hours) Collected s/steel Powerflow headers from Post Office. 28 May 2010 2.0 Hours (Total = 434.75 hours) Removed old headers and trial fitted new s/steel headers. Cut 6mm off each front pipe, and 12mm off pipes that fit into the silencers, using bandsaw. Cut 6mm off balance tube pipe. Slotted the pipes that fit into the silencers with a hacksaw – they are 36mm diameter and the silencers are made to fit 35mm diameter pipes. Managed to fit headers so that the cylinder head joints do not leak – by removing the silencers and fitting the head joint first and tightening the nuts hand tight before fitting the silencers. 9 June 2010 1.0 Hours (Total = 435.75 hours) Removed RHS carb again and unscrewed idle jet. Removed blockage from idle jet. Checked that the idle fuel passage into the body of the carb was clear. Removed idle mixture screw and tinned the thread lightly with solder to improve the fit in the carb body. Replaced the idle mixture screw 2 turns out. Cleaned deposit out of float chamber, lightly sanded sides of float chamber. Re-assembled and refitted carb. 23 June 2010 3.0 Hours (Total = 438.75 hours) Fabricated one spoke retainer using 16mm round brass rod. Drilled centre hole 4mm, then turned spigot 7.3mm diameter. Milled 10.5mm square and parted off to 3.2mm thick (square). Faced square face in the lathe (to 3mm thick) and countersunk centre hole using 7mm drillbit. Placed new s/steel spoke in the retainer, held retainer in the bench vice and tapped spoke head down into the countersink to form the retaining slots. Started wheelbuilding. Inserted all spoke retainers, new s/steel spokes and new nipples. 24 December 2013 Rev 1.1 85 Allan‟s BMW R50/2 Restoration (Abridged) 4 – 6 July 2010 6.0 Hours (Total = 444.75 hours) Fabricated wheel trueing/balancing stand using 25mm square tubing and 20mm square tubing, welded together. Design is largely based on a commercial wheel balancing stand from Rod Neff described and reviewed on www.webbikeworld.com. 11-12 July 2010 0.0 Hours (Total = 444.75 hours) Removed battery and charged it for 7.5 hours. Initial open circuit voltage = 5.28V, final voltage = 6.29V (after a rest period). Note that when new, the battery charged to 6.76V after 5 hours at 0.8A. 6 August 2010 0.0 Hours (Total = 444.75 hours) Craig Patterson called from Bloemfontein re my advert in Kickstart magazine. He has a (new old stock) generator cover for me, without the captive nuts. He wants to swap for 2 x valve pushrods for R60/2. 7 August 2010 4.0 Hours (Total = 448.75 hours) Phoned Jan Cornel to enquire if he has R60/2 pushrods. He confirmed that he has 4 new pushrods (251mm long, 7mm diameter), and he will sell them to me for R250 each. He also confirmed that he has two hardened perch wedges for me. He also asked me to fabricate 2 x eccentric bushes for him for the gearbox he is restoring for Roly Tilman. Fabricated 2 x eccentric bushes using 20mm diameter silver steel. Faced the end and turned down to 18.5mm diameter for a length of 28mm, then turned down to 15mm diameter by 17.20mm long, chamfered edges. Used 1.5mm parting tool to cut a shallow groove (0.5mm deep) at the head of the bush, slowest direct speed on the lathe. Cut a shallow vee-groove to indicate 18.5mm round collar 2.10mm deep. Used bandsaw to cut off to 25mm long, faced cut end in the lathe to end up with 24.10mm overall length, and 6.90mm length of 18.5mm diameter. Gripped 15mm diameter in the 3-jaw chuck with a piece of 0.8mm shim under one jaw to set eccentric. Centre drilled, drilled right through with 4mm pilot drill and then drilled out to 6.8mm. Used 8mm drill to counterbore 7mm deep the hex end, chamfered edges and started M8 tap using the tailstock drill chuck. Removed work piece from lathe, gripped in bench vice and tapped M8 through. 24 December 2013 Rev 1.1 86 Allan‟s BMW R50/2 Restoration (Abridged) Clamped work piece in drill vice and used pedestal drill with a 90 deg countersink to chamfer hole edges. Clamped work piece in the milling vice with a vee-block and milled a 16mm AF hex on the 18.5mm diameter end about 5mm deep. Replaced work piece in the 3-jaw lathe chuck and chamfered the edges of the hexagon. Checked that a 16mm ring spanner will fit the hex. Polished 15mm diameter bush in the lathe using emery cloth to reduce the diameter to 14.97mm. Coated bushes with liquid soap, heated to cherry red (non-magnetic) and quenched in a bucket of cold water. Polished bush circumference and tempered to blue. Polished bush circumference again and checked 14.97mm diameter with micrometer. Cleaned thread and checked that an M8 bolt screws in easily all the way. Note that the above description has been updated to provide the correct measurements. 10 August 2010 2.0 Hours (Total = 450.75 hours) Visited Jan Cornel. The fabricated eccentric bushes were just too big to fit nicely in the gear selector forks, so I polished the bushes in his lathe with emery cloth wrapped around a file. The final diameter for a smooth fit in the gear selector forks was 14.95mm. It looks like there is sufficient space for the hexagons on the bushes next to the input shaft. If not, Jan can grind the hexagons on his bench grinder. Jan agreed to a straight swap – one eccentric bush for one R60/2 pushrod. Jan also gave me two perch wedges and three spoke plates. 15 August 2010 0.0 Hours (Total = 450.75 hours) Craig Patterson sent me an e-mail confirming that he has posted the engine/generator cover, together with a tracking number. I sent Craig an e-mail stating that I will collect the pushrods from Jan Cornel and will post them later this week. 19 August 2010 0.0 Hours (Total = 450.75 hours) Collected flat generator cover from Post Office. Packaged R60/2 pushrods in a short length of PVC conduit after greasing them. padded envelope and took to Cresta P.O. Sent e-mail to Craig, thanks for cover and advising him of the posting of his pushrods. 24 December 2013 Rev 1.1 Placed in 87 Allan‟s BMW R50/2 Restoration (Abridged) 21 August 2010 3.0 Hours (Total = 453.75 hours) Fabricated 2 x special nuts for new generator front cover, using 16mm Φ stainless steel 304 bar. Cut an 80mm length of s/steel bar using the bandsaw. Gripped bar in 3-jaw chuck, faced cut end and turned down to 14.5mm Φ for circular collar (2,5mm wide), then down to 10mm Φ for 30mm long main body, overall length = 38mm. Turned a 1mm wide recess for the circlip 2mm from the end of the 10mm Φ shank. Centre-drilled deeply and drilled 5mm Φ hole 30mm deep, and threaded M6 x 1. Reversed the bar and gripped newly turned 10mm shank in the 3-jaw chuck to repeat the foregoing procedure, but with support from the tailstock centre. Gripped workpiece in the bench vice and cut in half using hand hacksaw. Chucked individual workpieces in the lathe and faced the cut ends to result in an overall length of 38mm. Removed from lathe and milled 10mm AF hex on ends for 5,5mm deep, resulting in a 14.5mm diameter collar 2.5mm thick between the hex and the 10mm diameter portion. Returned to lathe and chamfered the hex corners and domed the ends. Fitted 10mm external circlips to the grooves. On subsequent nuts, I changed the dimensions to 15.0mm Φ (for 8mm) and 10.5mm Φ (for 30mm). Before cutting the hex in the milling machine, I turned the 15mm Φ portion down to 11.5mm Φ for a length of 5.5mm (less to mill). Circlip grooves are cut so that the circlips rotate easily. Labour = 2 hours. 24 December 2013 Rev 1.1 88 Allan‟s BMW R50/2 Restoration (Abridged) 22 August 2010 1.0 Hours (Total = 454.75 hours) First attempt at bead blasting new generator front cover. Still not working very effectively. I may also have to use sandpaper to smooth roughness on the generator cover before bead blasting again. 24 - 28 August 2010 4.0 Hours (Total = 458.75 hours) Sanded new generator front cover using 80 grit sandpaper and sanding block, as well as rotary sanding pad in Ryobi cordless drill. Bead blasted new generator front cover, washed in soapy water, dried with blast from air duster. Fitted new stainless steel captive nuts and fitted new front cover to engine. 8 September 2010 0.0 Hours (Total = 458.75 hours) Purchased 10 x 10mm external circlips and 10 x 10mm E-clips, JKM. 11 September 2010 0.5 Hours (Total = 459.25 hours) Removed fabricated perch wedges and fitted OEM wedges (from Jan Cornel). 26 September 2010 0.25 Hours (Total = 459.5 hours) Started bike, 3rd kick. Revs well, idles. Rode bike in 1st gear along driveway. Need to adjust front brakes. Touched up chips in paintwork with brush-applied Duco Black Limo. 27 September 2010 0.5 Hours (Total = 460 hours) Painted fixed hex on front swing arm spindle with Duram Metcote NS5 etch primer, 2K primer and 2K black enamel, using a brush. 1 October 2010 1.5 Hours (Total = 461.5 hours) Fabricated a reducing bush for front wheel spindle using an 80mm length of 20mm OD galvanised steel conduit, bored out to 17mm ID. 24 December 2013 Rev 1.1 89 Allan‟s BMW R50/2 Restoration (Abridged) Fabricated an inner “top hat” bush from 30mm OD BMS. Faced end and turned 30mm OD, then turned 25mm OD for a length of 8.5mm. Centre drilled and progressively drilled out to 19mm ID before using a boring tool to finish the ID to 20mm. Cut off to 11mm length in the bench vise, fitted in 3-jaw chuck and faced the cut end to result in a “brim” thickness of 1.5mm, chamfered all sharp edges and reversed in the 3-jaw chuck to face the smaller end to result in an overall length of 10mm. Flatted “wedding band” spacer ring on emery cloth to adjust the bearing preload. Cleaned SKF and FAG bearings in petrol and oiled using H32 oil. These bearings are in perfect condition. Fitted all parts to the spare spindle, using a tubular spacer to provide thrust on the bearings. Fitted spindle and bearing stack in wheel to be trued, and clamped spindle in wheel truing/balancing stand. The rim requires extensive truing to meet specification! 2 October 2010 1.0 Hours (Total = 462.5 hours) Fabricated another spoke spanner using 16mm Φ EN8 (the previous spanner made from 13mm hex MS broke!). 6 October 2010 0.5 Hours (Total = 463 hours) Removed front brake lever and rotated it on the splines to result in an angle closer to 90 degrees when the brake hand lever is applied. The distance between the lower parts of the arms is now closer to the 16.5cm quoted by Duane Ausherman. Hopefully, this will improve the effectiveness of the front brake. 10 October 2010 0.5 Hours (Total = 463.5 hours) Adjusted front brake cam anticlockwise to take up some slack in operating the brake shoes. Adjusted brake Bowden cable free play. 24 December 2013 Rev 1.1 90 Allan‟s BMW R50/2 Restoration (Abridged) 13 October 2010 1.0 Hours (Total = 464.5 hours) Took newly spoked wheel to Jan Cornel for trueing. There is a “dent” in the rim on one side. Jan tried to hammer it out with a deadblow rubber mallet, but with no success. He said the rim should be fine on the rear wheel of the motorcycle. He also checked the runout on the brake drum and said it was fine. Bearings appear to be correctly adjusted. 16 October 2010 0.5 Hours (Total = 465 hours) Milled flats on newly fabricated spoke wrench. Jan Cornel has similar spoke wrenches with handles twice as long. Fabricated four stainless steel washers (two for spares).for carb floats: OD = 7mm, ID = 2.5mm, thickness = 1.5mm. Fitted new stainless steel washers to my BMW R50/2 carb float pins. Fabricated 8 more stainless steel carb float washers for Jan Cornel. 23 October 2010 0.0 Hours (Total = 465 hours Replaced short length of fuel hose between inline filter and float chamber to cure a fuel leak. Tickled carbs and slowly moved kickstart lever twice to turn motor over. Kicked once and the motor started and idled perfectly. Rode motorcycle up and down the road twice. Gear lever catching on LHS exhaust header. Tapped LHS exhaust header pipes inwards with a rubber mallet, tightened exhaust manifold nuts. Rode motorcycle up and down the road twice more. Gear lever not catching on LHS exhaust header anymore. Gearbox and clutch action are perfect! 26 October 2010 0.0 Hours (Total = 465 hours) Mike Lester gave me a new National 6V 35/35W headlamp globe. (Lamp fitted is 25/25W) 30 October 2010 0.5 Hours (Total = 465.5 hours) Removed all the new s/steel spokes and nipples from the bent/buckled rim xx November 2010 1.5 Hours (Total = 467 hours) Fabricated a bending brake for the steel wheel rim using a thick wooden plank and some tough angle iron. Cut 2 x curved strips from pine plank to use inside the rim when using the bending brake. Bolted bent rim to the plank and pulled the rim over to the appropriate side to straighten the rim – in 3 places. Some success. 1 January 2011 2.5 Hours (Total = 469.5 hours) Fabricated 2 off vacuum take-off stubs from 7mm diameter brass rod. Turned down to 6mm diameter, centre-drilled and drilled 1.5mm right through. Drilled 3mm diameter for approx 8mm and tapped M3.5 x 0.7. Chamfered inner and outer edges. Reversed in the 3-jaw chuck and faced to length = 18mm. Chamfered edge and threaded M6 x 1 for 6mm using the tailstock die holder. Chamfered inside edges. 24 December 2013 Rev 1.1 91 Allan‟s BMW R50/2 Restoration (Abridged) Cut 2 x M3.5 screws to 6mm length and turned down brass washers to suit. Fitted red fibre washers. Removed carburettors, mounted them on an angle plate and drilled through mounting flange with 1.5mm drill, followed by a 5mm drill for about 6mm. Tapped hole M6 x 1 using a bottoming tap. Used Loctite Threadlocker 243 on brass vacuum stubs and screwed them into the carburettor mounting flanges (using the blanking screw as a driver). Let set for about 30 minutes. Refitted carburettors to motorcycle. 2 January 2011 3.0 Hours (Total = 472.5 hours) Tried, unsuccessfully, to adjust carburettors using the differential manometer. The RHS cylinder always showed more vacuum. Removed spark plugs and carried out compression test (using 2 different gauges): LHS = 5 Bar Gunson (6 Bar Dixco) RHS = 7 Bar Gunson (8 Bar Dixco) Compression is low and unbalanced. It could be low because the rings have not yet seated, or because the valves are not sealing. There is also a possibility that the cylinder head gaskets are still not sealing properly due to incorrect torque on the head bolts. Removed valve covers – Black deposit at the bottom of both covers, like soot/carbon. Check-tightened cylinder head bolts using a 14mm ring/flat spanner. It felt as if the RHS bolts were slightly looser than the LHS bolts. Check-tightened the cylinder base nuts with a 17mm ring/flat spanner. Some seemed a bit loose. Checked and adjusted valve tappet clearances again. Initially, I could not get the LHS at the point where the pushrods were loose, so I checked the RHS first, then turned the engine 180 degrees, and “miraculously” the LHS pushrods were loose (I cant explain why). Repeated the compression test (cold) with the Gunson gauge: LHS = 7 Bar RHS = 7 Bar Cleaned and refitted the valve covers, spark plugs, timing hole rubber plug. Note that at 1700m above sea level, the compression pressure reduces to 0.853 of the quoted specs. For the R50/2, at 1700m amsl, the pressure should read 7 – 8 bar. 8 January 2011 0.5 Hours (Total = 473 hours) Removed front brake lever on brake drum and replaced it shifted by one spline. 15 January 2011 1.0 Hours (Total = 474 hours) Removed RHS carb and idle jet. Cleaned out idle jet and idle air screw. Replaced idle air screw 2 turns out from fully seated. Checked float lever height = 22mm. Flatted carb mounting face on 320 water paper on plate glass. Replaced carb. Set idle speed screw just touching slide. 24 December 2013 Rev 1.1 92 Allan‟s BMW R50/2 Restoration (Abridged) 31 January 2011 2.0 Hours (Total = 476 hours) Loaded bike on trailer (borrowed from Zane) and delivered it to Jan Cornel. Jan spent just over 2 hours on my bike: o The compression does differ, but nothing to be concerned about. o Jan checked the ignition timing with his timing light – the differential timing is well within spec. (I think the timing is just a touch retarded). He also says the mechanical advance seems a bit slow. o He removed the carb float chamber covers and said there was not enough fuel in the chambers. He removed the small s/steel washers on top of the floats and replaced them with much larger washers. He thinks the floats should be 11g on the lever top carbs and not 7g. He says I could try 2 washers on top of each float to improve the pickup from idle. o He says I must set the tappets 0.2mm (inlet) and 0.25mm (exhaust) (0.05mm more than spec). This appears to be satisfactory for local climatic conditions. o We bent the tab in the headlight switch unit a touch to get the engine cutout to work. o I cut a small shim using 0.010” brass, folded double and inserted over cutout switch tab. o Removed generator cover and checked the mechanical advance unit – appears to be OK. o Jan says I must bend the gear lever some more to clear the exhaust pipe. o He also says I must take some 40 grit sandpaper and take off the high spots on the front brake shoes. o Jan checked the idle speed with an inductive pickup rev counter – seems to be idling at around 750 rpm. o Jan says the clutch cable appears to be a bit tight – needs to be loosened a bit. o LHS carb leaking fuel a bit from screw plugs. o Jan removed the fuel hoses and filters and replaced with new plastic hoses. o While there I looked at another bike – gap between front swingarm and cover = 2 x mine. 1 February 2011 0.0 Hours (Total = 476 hours Researched lever top carb info (Bing manual, Vech site, Uli‟s, Roland Slabon, etc) Floats for lever top carbs = 7 grams. Only carbs for BMW R26s and R27s use 11 gram floats. Small washers/spacers on top of the floats are only required when using soft-tip float needles. My float needles are solid/hard tipped. The spacer will have the effect of reducing the amount of fuel in the float chamber, in the same way that bending the float lever outwards reduces the fuel level. To get more fuel into the chamber, remove the spacers and bend the float lever upwards another mm. Jan fabricated a stepped rod that he fits through the float lever to check the float lever height. On my carbs, the float levers were about 1mm too high (using his gauge). 2 February 2011 2.0 Hours (Total = 478 hours Removed tappet covers and re-torqued cylinder head bolts (40Nm on my torque wrench – reads 5Nm too high) Adjusted tappet clearances to 0.2mm (inlet) and 0.25mm (exhaust). Oiled the valve rocker shaft holes and replaced tappet covers. Bike started on the first kick, idles well, revs fine (perhaps a bit slow), no noise from tappets, and cuts out when the ignition switch is pulled, as it should! Checked ignition timing dynamically with my timing light – the one line (of differential timing) was below the timing mark on the crank case, and the other line and “S” mark were even lower at idle speed. 24 December 2013 Rev 1.1 93 Allan‟s BMW R50/2 Restoration (Abridged) Removed generator cover and mechanical advance unit. Adjusted points gap to 0.45mm to advance the timing slightly. Adjusted spring tension on mechanical advance unit – reduced tension. Noted that the springs are of heavier gauge than those on the worn unit loaned to me by Jan Cornel. Replaced mechanical advance unit and checked timing dynamically again. This time the lower line and “S” mark are on the timing mark on the crank case, and the upper differential mark is above them. I think it is acceptable for a touch more timing advance at this altitude. Replaced generator cover and rubber plug for the timing hole. Bike starts on first kick, idles well. Pumped tyres 200kPa. Rode bike around the block – a bit rough and sluggish, but OK. Need to check and adjust steering head bearings and/or front swing arm bearing preload. Brakes still disappointing, and gear lever still needs to be bent upwards to clear exhaust pipe. 5 February 2011 1.0 Hours (Total = 479 hours) Fabricated a float lever height gauge using Φ 4.8mm rod. Turned down to Φ 3.8mm for about 16mm, then turned down to Φ 2.8mm for a length of 10mm. Then adjusted the Φ 2.8mm portion to result in a length of about 5mm for the Φ 3.8mm portion. Adjusted float lever heights on both carbs using the new float lever height gauge. Works very well, since it takes the guess-work out of using a rule and trying to keep everything at right angles. 6 February 2011 0.5 Hours (Total = 479.5 hours) Visited Jan Cornel after CMC visit. Jan says my bike‟s advance mechanism is correct. The springs are too weak on the repaired unit. However, my unit may need 11mm springs (currently they are 9mm long), as indicated on the Slash2 forum. Jan could not explain to me the principles of adjusting the advance unit spring tensions. Jan is very happy with the repair work I performed on the worn out advance mechanism. He reckons, with the correct springs, it should last many miles. Replaced mechanical advance unit and generator cover on my bike, started the bike, and it idled and revved fine. The main 15A fuse blew when trying to replace the generator cover – confirming the necessity to disconnect the power when removing/replacing the cover! 13 February 2011 0.0 Hours (Total = 479.5 hours) Started bike easily, and rode it around the suburb. Still a bit slow to rev, and something loose on the front end – could be steering head bearings or front swing arm. Front brake still pathetic, rear brake “pulsing”. Tightened both carb plug screws. 14 February 2011 0.0 Hours (Total = 479.5 hours) Bought new 14mm ring/flat spanner (Kennedy) from ExecuPawn. 24 December 2013 Rev 1.1 94 Allan‟s BMW R50/2 Restoration (Abridged) 22 February 2011 1.0 Hours (Total = 480.5 hours) Fabricated 2 x stainless steel domed 13mm AF nuts for valve covers to dimensions from Melville Price. Chucked 13mm hex s/steel bar, faced the end, centre drilled, and drilled tapping size (6.8mm) for M8 thread, 21mm deep. Countersunk for 2mm with 8mm drill bit and chamfered inside edge. Tapped M8 with spiral flute tap. Turned down hex to Φ 12mm for a distance of 12mm. Chamfered edges. Removed from chuck, cut off 25mm length, and reversed in the lathe chuck. Faced the end to achieve 12mm long hex portion, domed the end using the chamfer tool, a file and emery cloth. Polished on the electric buffing wheel. Removed the 2 commercial M8 dome nuts from the valve covers, as well as the spring washers. Fitted B8 s/steel wavy washers and the new fabricated s/steel domed nuts to the valve covers. Fabricated 2 more dome nuts for Melville Price. 25 February 2011 0.0 Hours (Total = 480.5 hours) Purchased 2 x M10 copper washers, and 2 x M14 copper washers, JKM. 27 February 2011 0.5 Hours (Total = 481 hours) Started bike first kick, rode bike around the suburb. Noticed that there is play in the steering head. Placed bike on centre stand and raised front end with a trestle under the front of the engine. The play in the steering head bearings was seen and felt when moving the swing arm forwards and backwards. Removed handlebar riser nuts and detached handlebar from top yoke. Removed yoke bolts and removed steering damper (note that the bottom plate on the steering damper falls off!). Removed 36mm AF nut, and lifted off the top yoke. Tightened the 41mm AF nut on the steering head at least half a turn and felt for play in the steering head bearings, and checking that the wheel moves easily from side to side. Replaced top yoke and fitted the chromed bolts. Refitted the 36mm AF nut on the steering head and tightened it securely with a ring/flat spanner. Refitted the handlebar risers in the top yoke and tightened the nuts securely. Refitted the steering damper. Checked that the front wheel still moves easily from side to side. Rode the bike around the suburb again, and confirmed that there is no more play in the steering head bearings. Parked bike. 2 March 2011 0.0 Hours (Total = 481 hours) Bought 200mm x 80mm x 4mm MS plate from Fleet Steel in Strijdom Park to fabricate steering head spanner 36/41mm. 4 March 2011 0.0 Hours (Total = 481 hours) Bought two oil seals = 65 x 85 x 10, 30 x 42 x7 (Nitrile) for final drive, BMG. 7 March 2011 0.0 Hours (Total = 481 hours) Bought 431 (EN57) stainless steel, Φ 20mm x 260mm and Φ 25mm x 430mm from Diversified Alloys in Stormill to turn axles. 24 December 2013 Rev 1.1 95 Allan‟s BMW R50/2 Restoration (Abridged) 9 March 2011 0.0 Hours (Total = 481 hours) Fabricated 36/41mm steering head spanner using 4mm MS plate (3 hours) 10 March 2011 0.0 Hours (Total = 481 hours) Bought oil seal 28 x 47 x 7 Nitrile for final drive, BMG. 11 March 2011 0.5 Hours (Total = 481.5 hours) Replaced front suspension bolts with M10 stainless steel bolts, washers and nuts (used A4 nuts with CopaSlip). Fitted cable ties to tyre pump and frame. 12 March 2011 0.0 Hours (Total = 481.5 hours) Started bike first kick, rode bike around the suburb. 14 March 2011 0.5 Hours (Total = 482 hours) Bought stainless steel hex bolt M12 x 45 and nut, JKM Replaced LHS rear suspension bolt with M12 stainless steel bolt, washers and nut (with CopaSlip). Note that RHS rear suspension bolt is fine thread fitting into final drive housing (to be fabricated). 17 March 2011 3.0 Hours (Total = 485 hours) Milled 8 x stainless steel hex nuts M10, 17mm AF down to 14mm AF. Removed M10 stainless steel hex nuts from cylinder bases and replaced them with the 14mm AF nuts. Ground 14mm Kennedy ring/flat spanner to fit in the confined space around the cylinder bases. 26 March 2011 0.5 Hours (Total = 485.5 hours) Aligned front and rear wheels using a length of 25mm square tubing lifted up on bricks. Measured wheelbase (used carpenter square): o RHS = 1425mm o LHS = 1405mm o Spec = 1415mm 11 April 2011 0.5 Hours (Total = 486 hours) Collected BVK/SOA forms from Randburg Licencing Office for registration of a “rebuild”. Completed forms, scanned forms and receipts 12 April 2011 0.5 Hours (Total = 486.5 hours) Took completed BVK/SOA forms to Linden SAPS for sworn affidavit. 24 December 2013 Rev 1.1 96 Allan‟s BMW R50/2 Restoration (Abridged) 13 April 2011 2.5 Hours (Total = 489 hours) Took completed forms to Randburg Licencing Office. They told me to take the completed forms to Langlaagte Testing Station (at weighbridge) for Police Clearance (before 11h00). Langlaagte Testing Station (4) told me (at 11h00) to return tomorrow with the bike. They only “work” from 07h30 to 11h00! They first entered the engine number into the computer and checked for something or other (didn‟t tell me). Need proof of residence (+ 2 copies), ID (+ 2 copies), originals (+ 2 copies) for Langlaagte TS. Removed paint from frame numbers on the steering head. 15 April 2011 3.5 Hours (Total = 492.5 hours) Loaded bike on Zane‟s bike trailer and drove to Langlaagte Testing Station (at weighbridge) for Police Clearance (09h30). Queued at window 4, and handed completed BVK/SOA forms to them. They took forms and copy of my ID and completed Part 1 of RPI form. I then waited for my number to be called. When they called my number, they returned the forms to me and I drove into the vehicle queue where the SAPS completed Part 2 of the RPI form (frame and engine number, make and model of vehicle), and told me to take the bike to the weighbridge at Randburg Testing Station to be weighed, before handing the forms back to Randburg Licencing Office. Departed Langlaagte at 11h30 and drove to Randburg Testing Station, where they informed me that they did not weigh bikes since the licence fee is a flat rate for bikes!. They said I must take the completed forms back to Randburg Licencing office. Unloaded the trailer at home, scanned the completed RPI and returned to Randburg Licencing Office where the system was offline and I was told to return on Monday. 20 April 2011 1.0 Hours (Total = 493.5 hours) Took forms to Randburg Licence Office. Completed parts A and C of form RLV (Request to Register & Licence Motor Vehicle). They made 2 copies of ALL the forms. They checked on Natis system that engine and chassis numbers do not exist. They then send the 2 copies to Pretoria for the details to be entered on the system. Call after 2 weeks to confirm that details have been entered on Natis. 25 April 2011 0.0 Hours (Total = 493.5 hours) Started bike first kick, rode bike around the suburb. Removed centre stand, tried to bend LHS leg inwards to clear silencer. Not successful. Closed the ends of the legs from 175mm inside measurement to 170mm inside measurement, but it probably bent the RHS leg further in. Inserted M10 s/steel nut between LHS silencer and mounting – still not enough for centre stand to clear. RHS of centre stand needs to have a 5mm plate welded underneath to get the bike to stand more or less perpendicular. 8 May 2011 0.0 Hours (Total = 493.5 hours) Started bike first kick, rode bike around the suburb. 24 December 2013 Rev 1.1 97 Allan‟s BMW R50/2 Restoration (Abridged) 15 May 2011 0.0 Hours (Total = 493.5 hours) Bought 1”BSW Britool socket (3/4” drive) from Piston Ring Club to fabricate pin wrench for final drive pinion removal. 16 May 2011 3.0 Hours (Total = 496.5 hours) Turned down OD of 1”BSW Britool socket from 60mm to 57.5mm, using brazed tip lathe tool – very tough metal! Hacksawed slots in the end of the socket to suit slotted ring in final drive. Tools Fabricated for BMW R50/2 Final Drive Pin Wrench Fabricated from 1” BSW Britool Socket 24 December 2013 Rev 1.1 98 Allan‟s BMW R50/2 Restoration (Abridged) 20 May 2011 0.0 Hours (Total = 496.5 hours) Returned 27:8 final drive to Jan Cornel (he needed it for spares to repair a client‟s diff). 22 May 2011 1.0 Hours (Total = 497.5 hours) Removed centre stand again and bent the RHS leg in the vice to clear the exhaust pipe. Sanded tool marks on centre stand. Mixed some 2K black paint and hardener and brush-painted the centre stand. Replaced centre stand – note that the stand has been modified. Threaded bushes (M10) have been welded to the stand, and the holes in the frame are too small for the standard steel bushes. Started bike first kick and rode it around the block again. 29 May 2011 0.0 Hours (Total = 497.5 hours) Tightened front swing arm spindle nut (24mm spanner), as well as rear swing arm dome nuts (36mm). Started bike first kick and rode bike around the block twice. 12 July 2011 0.0 Hours (Total = 497.5 hours) Started bike first kick and rode bike around the block twice. Clutch grabs on pull away, not smooth take up. Centre stand rattling against exhaust when up. 23 July 2011 1. 2. 3. 4. 1.0 Hours (Total = 498.5 hours) Removed air filter assembly and battery. Cleaned air filter housing. Checked battery voltage = 5.26V. Trickle-charged battery for 3 hours. Voltage = 6.30V. Replaced battery and air filter assembly. 1 August 2011 1.0 Hours (Total = 499.5 hours) 1. Phone Randburg Licence Office – bike has finally been entered on Natis system. 2. Went to Randburg Licence Office and was issued with a Request for Police Clearance (RPC) form, and told to take the bike back to Langlaagte Testing Grounds for SAPS clearance and to obtain a roadworthy certificate (RWC). 12 August 2011 4.0 Hours (Total = 503.5 hours) 1. Fitted rear view mirror on RHS handlebar. 2. Placed bike on Zane‟s trailer and went to Langlaagte Testing Grounds for SAPS clearance, from 09h00 to 12h00. Had to make a copy of the original RPI form (R3-00) on site. All the SAPS did was to take a photo of the frame number. Then I had to wait for the printed SAPS clearance form. 3. Drove to Randburg Testing Grounds and obtained Roadworthy Certificate = R180, 1 hour. Had to start the bike and turn on lights and brake light. 4. Returned bike to storage and placed battery on trickle charge. 24 December 2013 Rev 1.1 99 Allan‟s BMW R50/2 Restoration (Abridged) 13 August 2011 1. 2. 3. 4. 5. 6. 1.5 Hours (Total = 505 hours) Disconnected battery & tack-welded 5mm plate under RHS leg of centre stand. Placed bike on axle stands and removed centre stand. Welded plate on centre stand and dressed the welds. Painted the work with Duram Metcote NS5 self-etching primer, let dry. Mixed some Black 2K paint and touched up centre stand, let dry. Replaced centre stand & reconnected battery. 04 September 2011 1. Went to CMC and visited Jan Cornel Jan lent me 2 x 120 main jets to try in my bike. Jan asked me to make 2 more pairs of gearbox selector eccentric bushes 2. Started bike first kick and rode it around the suburb a few times. 10 September 2011 0.5 Hours (Total = 505.5 hours) 1. Removed carbs and fitted 120 main jets. 2. Applied Hylomar to carb base gaskets and refitted carbs 3. Started bike and rode it around the suburb. It feels like there is a definite improvement in responsiveness with the new 120 main jets. 11 October 2011 0.5 Hours (Total = 506.0 hours) 1. Fitted M5 Helicoil to Mike Lester‟s R60/2 carb. Carb is fitted with 125 main jet for lever top carbs. 2. Mike Lester rode my bike around the suburb – the following comments apply: Clutch is a problem – grabbing. Could be flywheel runout or requires new parts. Gearbox “clonks” more than his R60/2 – ensure that oil in gearbox is SAE40 (correct). Rear brake pulsates but works well. Front brake has too much “spring” – looks like a cable problem. Try replacing the cable. Performance seems to be fine. He says I must remove the fuel tank and he will improve the finish on it (gratis). 3. Replaced front brake cable with thicker Uli‟s cable – moved front brake lever out one notch again. 14 October 2011 1. Pulled in clutch lever on handlebars and observed flywheel moving slightly through the timing inspection hole. This may be due to a “loose fitting” crank rear bearing, and could be the cause of the clutch grabbing. 27 October 2011 1.0 Hours (Total = 507.0 hours) 1. Tried to register and licence the bike at Randburg Licencing Office. I was informed that: The NATIS entry had expired after 21 days The RWC had expired after 60 days 2. I was told to make another copy of ALL the previously submitted documentation and to resubmit for the NATIS entry to be recaptured. 3. Returned home and made another copy of all the documentation. 4. Returned to Randburg Licencing Office and resubmitted the copy of all documentation. I was told it should only take a few days. 24 December 2013 Rev 1.1 100 Allan‟s BMW R50/2 Restoration (Abridged) 2 November 2011 1. Randburg Licencing Office telephonically confirmed that the NATIS entry had been approved. I was advised to register the bike on the following day. 3 November 2011 1.0 Hours (Total = 508.0 hours) 1. Randburg Licencing Office took all the ORIGINAL documents including the blue form application for registration. 2. I paid the cashier R180 for the registration certificate and R120 for the licence. However, he would not give me the licence disc until a new RWC has been submitted. 13 November 2011 1.0 Hours (Total = 509.0 hours) 1. 2. 3. 4. 5. Removed old clutch cable. Oiled new clutch cable from Uli‟s. Filed slots in cable adjusters to fit the new thicker cable. Fitted new clutch cable from Uli‟s. Rode the bike around the suburb. Clutch still grabs and shudders on take up, but feels better with the new cable. Front brakes definitely feel better. 6. I cannot locate any confirmation that I measured the thickness of the clutch friction plate before refitting, or the wear on the clutch cover plate. What are the specs for the /5 clutch friction plate thickness? 15 November 2011 1.0 Hours (Total = 510.0 hours) 1. Trailered the bike to Randburg Testing station where they issued another RWC = R180 (only checked brake light, hooter and headlight functioning). 2. Submitted RWC with licence application form to Randburg Licencing Office where they issued a valid licence and disc (no extra charge). 3 December 2011 1. 2. 3. 4. 0.25 Hours (Total = 510.25 hours) Bought Sterling licence disc holder, Main Reef Midas (R14) Fitted licence disc holder to LHS rear mudguard stay bolt. Placed valid licence disc in holder. Rode bike around the block twice. Clutch is a bit better and front brakes feel more “solid”. 11 December 2011 1. Started bike first kick. Rode bike around the block twice. 2. The clutch was still “grabby”, and I heard a rattle when I let the clutch out to ease the bike forward in 1st gear from a dead stop. I also removed the rubber stop in the timing hole and observed the flywheel as I activated the clutch. The flywheel moves very slightly axially when the clutch is activated. The rattle could be due to any of the following: Clutch cover plate mounting bolts loose - unlikely. Flywheel loose - unlikely. Clutch friction linings loose. Clutch friction disk splines worn. Loose bolts on the driveshaft universal joint. Play in rear crank bearing or seatings. Play in gearbox input shaft bearing or seatings, or too much axial play of input shaft. 24 December 2013 Rev 1.1 101 Allan‟s BMW R50/2 Restoration (Abridged) 28 January 2012 1. Collected a set of clutch parts from Rob Dercksen: Diaphragm spring (heavy duty) Pressure plate - fairly smooth surface Friction disc, with good lining, very bad splines! Pressure ring, working face ground flat, to be used with spacer washers & 9mm clutch Pressure ring with raised edge to replace spacer washers – also reground. This is only for use with 7mm thick clutch plates. 2. Rob did not give me the spacer washers = 4mm thick or the slotted screws for the clutch assembly, or a usable clutch pushrod. 3. Rob asked me to make 16 clutch pushrods from silver steel – he lent me a broken pushrod and a thrust bearing assembly as a pattern. He said Hennie van Zyl recommended that grooves be turned to accommodate an o-ring rather than a reduced section for the felt ring. 4. Measured the sample clutch thrust rod: Overall length = 203mm (my existing clutch pushrod is only 195mm long) Diameter = 7.5mm Thrust bearing end reduced to 6mm diameter for a length of 18mm Need to order 4000mm of silver steel to fabricate 17 pushrods 5. Measured the thickness of the flat pressure ring = 5.97mm (clutch cover plate). 30 January 2012 1. Returned clutch friction plate with worn splines to Rob Dercksen – swapped it for another clutch friction plate in very good condition (with Peter). 2. Measured clutch friction plate thickness = 8.5mm (very good) 3. Obtained quotes for silver steel from Metals Centre, JKM and Sanderson Special Steels: JKM have 3 x 1m in stock of 8mm Φ = R90.07/m excl VAT Metals Centre don‟t have stock of 8mm Φ = R65/m excl VAT, 4 days to order (don‟t stock 7.5mm diameter) Sanderson can supply 1m or 2m lengths of 7.5mm Φ silver steel at R38/m excl VAT, and will deliver. 4. Ordered 2 x 2m lengths of 7.5mm Φ silver steel from Sanderson, paid by EFT = R173.28 5. Jan Cornel does not think that the clutch pushrod needs to be hardened – however, I may harden the ends a bit! 4 February 2012 0.75 hour (Total = 511.0 hours) 1. Sanded rust off clutch pressure plate. 2. Cleaned “new” clutch friction plate with petrol and BH32 and water. Dried friction plate with compressed air, and put it in the sun to dry completely. 3. Measured clutch friction plate thickness = 8.5mm (very good), width = 28mm and outer diameter = 180mm. Number of splines = 10. 4. Measured OD of felt oil seal fitted to sample clutch pushrod = 8mm 5. Purchased 20 off 6 x 1 O-rings from BMG (R14) – they look too thin and they do not fit tightly on a 6mm diameter rod. I will have to use smaller 5 x 2 O-rings 6. Measured ID of BMW R80/7 gearbox hollow input shaft = 9mm. However, the clutch pushrod is 8mm diameter. I am guessing that the /2 gearbox hollow input shaft has a diameter of 8.5mm max to accommodate the 7.5mm diameter pushrod. 7. Placed a 5 x 2 O-ring on a 6mm diameter rod and measured OD = 9.3mm. This will easily be compressed to 8.4mm OD (10% squeeze). 8. Measured height of diaphragm spring = 17mm 24 December 2013 Rev 1.1 102 Allan‟s BMW R50/2 Restoration (Abridged) 5 February 2012 2.0 hours (Total = 513.0 hours) 1. Fabricated 2 x 304 stainless steel washers for headlight mounting. OD = 30mm, ID = 8.5mm, 3mm thick. Chamfered and polished on the buffing wheel. Hennie van Zyl mentioned at CMC that he would like a pair of these washers in s/steel. 2. Removed existing pitted and chromed headlight mounting washers and replaced them with the new stainless steel washers. 3. Fabricated 1 x stainless steel washer for front axle OD = 32mm, ID = 14.3mm, 4mm thick. Chamfered and polished on the buffing wheel. 4. Removed 25mm washer from front axle and replaced with new 32mm stainless steel washer. 9 February 2012 1.0 hour (Total = 514 hours) 1. Fabricated one clutch pushrod using the 7.5mm diameter silver steel. Made a single 2mm wide groove and fitted 5x2 Nitrile O-ring – as a sample. 2. Noted that the broken clutch pushrod sample supplied by Rob Dercksen has 2 different diameters – the longer portion is 7.5mm and the rear portion is 8.2mm. 24 December 2013 Rev 1.1 103 Allan‟s BMW R50/2 Restoration (Abridged) 11 February 2012 2.0 hours 1. Visited Rob Dercksen and discussed the sample clutch pushrod. He says it is fine, but he would like 2 o-rings fitted – no problem. He says I must make all 16 clutch pushrods 205mm long. 2. Fabricated 8 more clutch pushrods, and fitted two 5x2 o-rings to each pushrod. 3. Unfortunately, I left the washer part of the clutch thrust bearing assembly at Rob‟s place! 4. I did get a sample oil seal for the clutch pushrod piston at Rob‟s. 12 February 2012 2.0 hours 1. Fabricated 8 more clutch pushrods. Ran out of 5x2 o-rings. 2. Need to purchase 35 off 5x2 o-rings from BMG. 3. Fabricated 2 more 304 stainless steel washers for headlight mounting for Hennie van Zyl. OD = 30mm, ID = 8.5mm, 3mm thick. Chamfered and polished on the buffing wheel. 4. Started bike first kick 5. Rode bike around the suburb – clutch not that vicious. 13 February 2012 0.0 hours 1. Purchased 35 off 5x2 o-rings from BMG = R10-81. 2. Fitted 5x2 o-rings to 8 clutch pushrods. 18 February 2012 1. 2. 3. 4. 0.5 hours Delivered 16 clutch pushrods to Rob Dercksen. Collected one clutch thrust washer from Rob Dercksen. Six of the new clutch pushrods do not fit the clutch thrust washer. Returned home with 6 clutch pushrods and applied emery cloth to the pushrods until the thrust washer fitted. 1 April 2012 0.0 hours 1. Visited CMC. 2. Fitted a single BMW 37 – 42 mm Jubilee Clip (hose clamp) to each carb inlet tube. 3. Started bike first kick and rode bike around the suburb for 30 minutes. 6 May 2012 0.0 hours 1. Visited CMC. Rob Dercksen was also there and he asked me to fabricate 30x mild steel clutch spacers for him. Spacer dimensions are OD = 16mm, ID = 8.5mm, thickness = 3.97mm. 2. Rode bike around the suburb for 30 minutes. 3. Fabricated 15 x clutch spacers on the lathe using leaded FCMS – took me about 1 hour. 12 May 2012 0.0 hours 1. Delivered 30 x clutch spacers to Rob Dercksen – no charge. 27 May 2012 0.0 hours 1. Pumped tyres from 1.5 bar to 2 bar (front) and 2.1 bar (rear) 2. Started bike first kick and rode bike around the suburb for 30 minutes. 3. Trickle-charged battery (4.78V - 6.38V for 3 hours. 24 December 2013 Rev 1.1 104 Allan‟s BMW R50/2 Restoration (Abridged) 12 July 2012 0.5 hours 1. Purchased M8x1 x 20 cap screws (10 off) from President Bolt & Tool in Fordsburg. 2. Turned 45 deg chamfer on inside edge of cap screws for clutch bolts. 17 August 2012 1. 0.0 hours Neil Darling of Optimum Clutch Systems recommended that I wash the new clutch plate (from Rob Dercksen) in thinners before using it, to remove any oil. He says the woven facing material is very good! 09 September 2012 1. 2. 3. 0.0 hours Checked tyre pressures – both around 2 bar. Started bike. Initially there were some rattles from the centre stand on the exhaust silencers, but this cleared up soon. Most likely as a result of shifting the exhaust system to the right to clear the gear lever. Rode bike around the suburb for 30 minutes. Gear change much improved, especially if making slow, deliberate changes. 4 October 2012 1. 0.0 hours Renewed licence = R192 at Cresta Post Office. 22 November 2012 1. 0.0 hours Purchased 8x hardened steel flat washers (M10) for cylinder head mounting studs = R8-15 from Northern Bolt, Midrand. 6 February 2013 1. 0.0 hours Purchased 6V 4.5 Ahr AGM battery from Current Automation = R68 27 May 2013 1. 0.0 hours Bought plastic box 160 x 96 x 67 = R81 from Communica for AGM 6V battery. 1 June 2013 1. 2. 3. 4. 5. 6. 7. 8. 9. 1.0 hours Removed 6V lead acid battery from motorcycle – measured voltage = 4.29V. Topped up battery with de-ionised water and placed battery on charge for a number of hours. Fitted plastic box for AGM battery with two M6 nickel-plated brass screws and nuts as terminals for the battery. Made up short leads fitted with 6.5mm round terminals at one end and female spade terminals at the other end. Soldered wires to crimp terminals. Fitted 6V 4.5Ahr AGM battery into plastic box, connected spade terminals on short leads to the battery terminals. Cut strips of Styrofoam to wedge battery into plastic box and closed lid with screws provided. Measured open circuit battery voltage = 6.65V. Fitted new AGM battery in plastic box into motorcycle frame and connected battery leads. Checked that all lights work with new battery. Rode „bike around the suburb for 10 minutes – no problems! 24 December 2013 Rev 1.1 105 Allan‟s BMW R50/2 Restoration (Abridged) 24 August 2013 1. 2. 3. 0.5 hours Loosened handlebar riser nuts and moved handlebar risers to the rear pair of holes. Tightened riser nuts. Checked tyre pressures: Front = 230kPa, Rear = 250kPa Rode „bike around the suburb. Definite improvement in riding position. My left wrist is no longer strained. 24 September 2013 1. 2. 3. 4. 5. 6. 7. 2.0 hours Removed old front engine mounting stud (280mm long). Fabricated a new front engine mounting stud using 12mm Φ 304 stainless steel, 295mm long, threaded M12 x 1.5 using a single point tool in the lathe. Cleaned up the threads using an M12 x 1.5 HSS die. Greased and fitted the new stainless steel front engine mounting stud. Removed old rear engine mounting stud (315mm long). Fabricated a new rear engine mounting stud using 12mm Φ 304 stainless steel, 330mm long, threaded M12 x 1.5 using a single point tool in the lathe. Greased and fitted the new stainless steel rear engine mounting stud with new galvanised Nylock nuts. Checked engine oil level = OK and rode bike around the suburb. 24 December 2013 Rev 1.1 106 Allan‟s BMW R50/2 Restoration (Abridged) 29 September 2013 1. 2. 3. 4. 5. 0.5 hours Drained (old, stale) fuel from tank. Removed tank mounting bolts and fuel crossover pipe. Removed fuel tank, removed fuel cock, removed tools from tool compartment, removed knee pads, and removed tank badges. Left one key for tool compartment in the lock. Straightened and fettled the spare top yoke plate (ex-Melville) BMW R50/2 Contents of Tool Kit 30 September 2013 1. 2. 0.0 hours Delivered fuel tank and top yoke (ex-Melville) to Mike Lester for spray painting. Mike previously indicated he wasn‟t happy with the clear coat on the tank and offered to redo it. Placed fuel cock in petrol to keep cork wet – too late!!. 18 October 2013 1. 0.0 hours Collected fuel tank and top yoke from Mike Lester. 19 October 2013 1. 2. 3. 4. 5. 1.0 hours Fitted BMW badges and knee pads to fuel tank, placed tools in tool compartment. Applied Autoglym polish to fuel tank. Fitted fuel tank to the bike – added a second rubber washer between the tank and the mounting bracket. Re-fitted fuel cock and filled the tank with about 7 litres of petrol. Started bike. 24 December 2013 Rev 1.1 107 Allan‟s BMW R50/2 Restoration (Abridged) 2 November 2013 1. 2. 0.0 hours Started bike first kick and rode it around the suburb. Fuel petcock leaks when in the “on” position – all over my left shoe! Looks like I will need to replace the cork lining again. 8 November 2013 1. 2. 3. 4. 5. 0.5 hours Purchased number plate (BN 58 MM GP) = R100. Mogale City Licensing Office issued me with a duplicate licence at no charge in order to purchase the number plate. Fitted the new number plate to the bracket using 4.8mm rivets. Fitted new licence disc. Started bike – fuel dribbles freely from the petcock spindle in the “on” position. Also noticed some oil on the rear gearbox shelf – one of the oil seals is leaking! 9 November 2013 1. 2. 3. 4. 5. 6. 7. 8. 9. 10. 1.0 hours Drained fuel from tank and removed fuel petcock. Cut away the three small crimped edges and dismantled the fuel petcock – cork lining was damaged. Cut a paper template for the cork and marked the positions of the holes from the petcock body. Cut a new piece of 3mm thick cork (26mm x 50mm) and used the paper as a template to cut the 4 holes using a ¼” hole punch. Cut the butting edges of the cork at an angle, applied some silicone grease and fitted the cork lining into the body of the petcock. Ensured that the holes in the cork lining were open and clear (using a 5mm drill bit) before refitting the spindle in the petcock. Refitted the fuel petcock to the fuel tank and filled the tank with the fuel previously removed. Confirmed that the fuel petcock does not leak in any position and that the fuel passes freely through the petcock in both “on” positions. Adjusted clutch cable. Checked engine oil level = ok 10 November 2013 1. 2. 3. 4. 5. 6. 7. 0.0 hours Rode bike around the suburb – longest trip to date. No fuel leaks at all. Clutch action appears a bit smoother and the clutch appears to release more fully. Seating position quite comfortable and no discomfort on wrists from leaning on handlebars. Experienced a little instability when riding at 35 – 40mph – wheel and tyre related, or swing arm bearings, or even steering head bearing related. Nonetheless, a very satisfying ride! Adjusted idle speed screws slightly to increase idle speed when hot. Engine casing hot, gearbox casing less hot and final drive about the same temperature as the gearbox. 24 December 2013 Rev 1.1 108 Allan‟s BMW R50/2 Restoration (Abridged) DEFECTS (BEFORE): 1. 2. 3. 4. 5. 6. 7. 8. 9. 10. 11. 12. 13. 14. 15. 16. 17. 18. 19. 20. 21. 22. 23. 24. 25. 26. 27. 28. 29. 30. 31. 32. 33. 34. 35. 36. 37. 38. 39. 40. 41. 42. 43. Frame and engine numbers do not match. Front wheel steel rim (British) narrower than BMW rim (bent spokes). Missing hinged piece for rear mudguard. Both front and rear mudguards had been “chopped” – front portion welded on front mudguard. Missing front mudguard stay. Missing tail light. Missing top engine mounting plate. Missing lower fuel tank bracket. Missing mounting bracket for dual seat. All chrome-electroplated parts were either rusting or flaking. Brake linings shot. Rusted components, including engine and gearbox internal, brake drums, etc. Piston rings badly worn Conrod small end bushes loose and badly worn Excessive lateral play in LHS conrod big end (crank webs need to be pressed closer). Valve guides badly worn, especially exhaust valve guides. Excessive axial/end play in valve rocker arms. Spotfacing on valve rocker arm supports worn, allowing headbolts to bind on hex. Fins broken on valve covers and cylinder heads. All engine and gearbox oil seals hardened through heat and age. All frame and wheel oil seals hard through age. Incorrect handlebar and rubber handgrips. Incorrect handlebar risers (BMW R68). Fuel tap cork lining shot. Fuel cap gasket perished. Carburettor parts missing – eg idle mixture screw assembly. Main jets were 105 instead of 120 (for lever-top carbs). Supplied with one incorrect carb air tube (for R60/2) No passenger (pillion) foot rests All rubber parts shot, including bushes, tank knee pads, footrest rubbers, etc. Incorrect size Yokohama tyres and tubes fitted. No gearbox cover gasket, and no shims on shafts. Excessive axial play on input shaft. Gearbox selector forks not adjusted centrally (require bending) Gearbox selector fork for 3rd/4th gear tips worn. Centre stand brackets have been modified – stand won‟t come all the way up. Oil pump gears are worn. Two valve pushrods have ends that have started cracking – placed at camshaft end. Speedometer drive gears damaged, but should be workable. RHS carburettor float chamber pitted, but appears usable. Camshaft and crankshaft noses have been filed. Chromed hubcaps and aircleaner dome not standard – should be painted silver. Domed generator cover too close to Earle‟s Fork – replaced with older flat cover Bowden cables supplied for clutch and front brake too thin 24 December 2013 Rev 1.1 109 Allan‟s BMW R50/2 Restoration (Abridged) IMPROVEMENTS: 1. 2. 3. 4. 5. 6. 7. 8. 9. 10. 11. 12. 13. Fitted brass vacuum take-off stubs on carburettors to aid synchronisation using the differential manometer. Stainless steel fasteners Stainless steel spokes and nipples Stainless steel exhaust headers and silencers Stainless steel cable end caps Some stainless steel fabricated parts, speedo cable gland, brake swivel pins, etc Fused (15A) battery positive lead Fitted 6V 4.5Ahr AGM battery Sump cover bolts replaced with stainless steel studs. Sump cover reinforced with flat bar Eccentric bushes, hardened and tempered silver steel, for gear selector forks. Used Viton double lip oil seals on engine and gearbox. Taper roller steering head bearings fitted. KNOWN DEFECTS (AFTER): 1. 2. 3. 4. 5. 6. 7. 8. 9. 10. 11. 12. 13. 14. 15. 16. 17. 18. 19. Frame and engine numbers do not match. Rear main crank bearing seated on crank with RT20G anaerobic retainer – did not set! Gearbox selector fork for 3rd/4th gear tips worn – need to be hard-faced and reground. Gearbox input and output shaft bearing seats in gear case could be tighter. Excessive lateral play in LHS conrod big end (crank webs need to be pressed closer). RHS exhaust valve guide is different – fabricated from PB1 bronze by me. LHS exhaust valve guide (Uli‟s) has been knurled and refitted by me. Centre stand brackets have been modified. Oil pump gears are worn. Two valve pushrods have ends that have started cracking – placed at camshaft end. Spotfacing on rocker shaft supports has receded. Chamfered hex on headbolts to compensate. Flywheel lateral play 0.1mm too much. Flywheel should have been trued in the lathe and balanced. Speedometer drive gears damaged, but working. Differential ignition timing < 6mm between marks One gearbox cover M6 stud that I replaced appears to be stripped again! Chromed hubcaps and aircleaner dome not standard – should be painted silver. Clutch “grabbing”. Frame/forks slightly out of true. 24 December 2013 Rev 1.1 110 Allan‟s BMW R50/2 Restoration (Abridged) PARTS FABRICATED Part Number 32 72 2072217 35 21 4044266 32 72 2072221 46 51 4034227 11 81 4034282 16 11 4080248 16 11 4080194 21 52 1020112 21 52 1080122 23 51 1056124 07 11 9913425 52 53 9034110 31 41 1231201-4 33 53 3064268 13 72 0043118 13 11 0039156 07 11 9940396 11 11 0001184 11 13 007156 51 14 6040110 46 52 4028218 36 31 4038243 13 11 0042146 16 11 4080288 24 December 2013 Description Qty Date Pivot screws for hand levers (stainless steel) 2 14 Oct 07 Bush for clutch hand lever pivot (EN1A Pb) 1 14 Oct 07 Bush for rear brake bell crank (EN1A Pb) 1 20 Oct 07 5/16” BSW cable adjuster for clutch lever 1 27 Oct 07 Engine mounting spacer (EN1A Pb) 1 28 Oct 07 Engine top hanger bracket (2,5mm MS plate) 1 31 Oct 07 Rubber spacers for fuel tank lower mounting 4 31 Oct 07 Petrol tank lower bracket (2,5mm MS plate) 1 03 Nov 07 Cap screw M6 (plated) for clutch lever, modified 1 03 Nov 07 Compression spring for clutch lever 1 04 Nov 07 Cotter pin for kick start lever (EN1A Pb) 1 07 Nov 07 Welded stop on RHS frame for centre stand 1 11 Nov 07 Screw M6 x 10 for breather filter 1 Sandblasted mudguards, seat frame, headlight 13 Nov 07 mounting brackets, centre stand, petrol tank lid Brazed cracked headlight mounting brackets 2 14 Nov 07 Fabricated side mounting bracket for seat 1 15 Nov 07 Welded bracket on seat frame for side mounting 1 17 Nov 07 Spacer shim under steering yoke 1 1 x M5 and 1 x M4 electrical terminal screws 2 8 Dec 07 Cut Cardan flange – swing arm gasket = paper 2 9 Dec 07 Cut gasket for air filter housing, 2.5mm cork 1 22 Dec 07 Float chamber screws M5 (stainless steel) 4 01 Jan 08 Stainless steel pivot pin for foot brake bell crank 1 01 Jan 08 M6 studs for rear crank bearing housing 5 02 Jan 08 Cut oil sump gasket, 2.5mm cork 1 03 Jan 08 Turned stainless steel 25mm diameter washers 8 05 Jan 08 Bead blasted cylinder heads, tappet covers, front 10 Jan 08 engine cover, slingers, sump (bottle of Rum!) Cut Nitrile gaskets (1mm) for BMW tank roundels 2 13 Jan 08 Clamping ring for sump, 16 x 3 flat bar 1 26 Jan 08 Another spring for centre stand 1 30 Jan 08 Top hat spacer, front wheel bearing LHS (BMS). 1 9 Feb 08 25mm Φ seal surface, 20mm Φ bore, 30mm Φ collar, collar = 1.5mm thick, total height = 14mm Re-upholstered dual seat 1 12 Feb 08 Lock for fuel tank toolbox lid 1 17 Feb 08 Carb mounting flange gasket (cut paper) 4 23 Feb 08 Rubber seal for tank tool box (weather strip) 1 4 Mar 08 Charlie Hamer Tig-welded broken fins on one Lot 20 Mar 08 cylinder head and tappet cover. Also arc welded front mudguard Machined welded cooling fins Lot 20 Mar 08 Bead blasted cyl head, tappet covers again Lot 26 Mar 08 Stainless steel M6 x 20 sump studs 12 31 Mar 08 5/16” BSW studs to M6 for Roly tappet cover 2 31 Mar 08 Rev 1.1 Cost R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R5-00 R0-00 R0-00 R0-00 R15-00 R0-00 R105-00 R0-00 R6-00 R5-70 R0-00 R513-00 R0-00 R0-00 R0-00 R150-00 R0-00 R0-00 R0-00 R0-00 111 Allan‟s BMW R50/2 Restoration (Abridged) PARTS FABRICATED (2) Part Number 34 11 2060182 11 21 0016268 11 11 0002172 11 41 0052527 16 12 4084110 16 12 4084109 11 41 0052527 07 11 9922093 11 12 0021816 23 21 1030116 23 21 1231658 23 11 1030174 07 11 9913227 07 11 9922036 07 11 9913625 07 11 9922082 07 11 9913444 07 11 9922054 31 41 2000295 23 22 1030176 21 52 1020112 23 22 1030176 07 11 9923412 07 11 9923412 23 11 1338646 07 11 9903214 13 11 0042146 32 72 2072223 23 31 1066186 23 21 1020164 24 December 2013 Description Qty Date Inner pressed sleeve, sheet steel extension Lot 12 Apr 08 pieces, hinge, brackets with M8 threads for rear mudguard Sand blasted three parts of rear mudguard ex- Lot 15 Apr 08 Roly Tilman (2 bottles red wine, 1 bottle Scotch – Rian Emerich) Front brake swivel pins (s/steel) 2 24 Apr 08 Spacer washer for crankshaft = 47mm OD x 1 29 Apr 08 35mm ID x 3,61mm thick (front) M4 screw, s/steel, slotted for tail light 1 10 May 08 Cut timing gear cover gasket (Flexoid 0,4mm) 1 17 May 08 Cut cork gasket for oil pump pickup/strainer 1 17 May 08 Red fibre gasket for fuel cock (19mm x 15mm) 1 1 Jun 08 Fibre gasket for fuel cock (21mm x 17,5mm) 1 2 Jun 08 Flexoid 1,5mm gasket for oil pump pickup/strainer 1 5 Jun 08 Turned dome nuts M8 x 1 stainless steel (303) for 4 28 Jun 08 drive shaft tube mounting studs Turned exhaust valve guide (PB1 bronze) 1 6 July 08 Steel shim washer 1mm thick between cam gear 1 18 Jul 08 and wavy spring washer for engine breather disc S/steel spacer for steering damper knob (to 1 16 Aug 08 replace mild steel fabrication from previous owner) Welded M8 stud on rear mudguard 1 30 Aug 08 Turned speedo cable clamp screw (M6), s/steel 1 20 Sep 08 with breather hole M5 x 10 s/steel hex screw, washer, nut, polished, 2 21 Sep 08 for front mudguard M8 x 20 s/steel hex screw, washers, nut, polished, 2 21 Sep 08 for front mudguard M6 x 16 s/steel hex screw, washers, nut, polished, 4 21 Sep 08 for rear mudguard Turned steering damper bolt, s/steel, M8 1 23 Sep 08 Turned clutch cable bushing, s/steel 1 25 Sep 08 M6 cap screw for clutch lever & Nylock nut 1 25 Sep 08 Speedo cable drive bushing, s/steel polished 1 25 Sep 08 M8 castellated s/steel nuts for steering damper 2 4 Oct 08 M8 castellated s/steel nut for rear brake bell crank 1 4 Oct 08 Exhaust header stubs for cross over tube 2 19 Oct 08 Charlie Hamer welded gearbox casing (gearlever) 1 23 Oct 08 Cut gearbox lid gasket, 0.4mm Velumoid 1 9 Nov 08 Stud M6 x 25 galv, waisted, for gearbox cover 2 9 Nov 08 Tufnol carb flange gasket, heat-resistant 2 15 Nov 08 Perch wedge, silver steel. 18mm long 2 15 Nov 08 Steel washer 8mm for gear selector for cap 2 22 Nov 08 screws Stop washer (gearbox input shaft), OD = 25, ID = 2 29 Nov 08 15, t =1.11mm (Not used) Rev 1.1 Cost R0-00 R0-00 R0-00 R0-00 R0-00 R3-00 R9-00 R50-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R50-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 112 Allan‟s BMW R50/2 Restoration (Abridged) PARTS FABRICATED (3) Part Number 23 21 1020216 23 31 1230086 23 31 1066162 23 11 1338646 23 21 1020164 23 21 1230969 23 21 1231655 46 51 4034227 12 13 8004120 13 11 1251395 23 11 1030174 13 21 2072370 36 31 4038243 61 21 8042109 07 11 9988505 34 11 2072444 23 41 1066286 07 11 9921605 23 21 1030168 34 11 2060178 11 14 0002191 32 72 2072221 13 11 0039184 07 11 9931089 07 11 9922155 36 31 3007378 36 31 3004168 36 31 4038173 11 11 0002195 24 December 2013 Description Qty Date Shim (gearbox input shaft), OD = 45, ID = 15mm, 1 29 Nov 08 t = 1.17mm, with joggle Turned eccentric bushes for gear selector forks 2 11 Dec 08 (hardened and tempered silver steel) Cut gearbox lid gasket, 0.4mm Flexoid 1 13 Dec 08 Stop washer (gearbox input shaft), OD = 20.75mm 1 15 Dec 08 ID = 15, t =1.75mm Shim (lay shaft) = 0.60mm x 40mm OD 1 16 Dec 08 Shim (output shaft) = 0.63mm x 47mm OD 1 16 Dec 08 Turned engine mounting spacer (Aluminium) 2 21 Dec 08 2BA screw for sparkplug wire terminal (Magneto) 1 26 Dec 08 Float lever tab, soldered on 1 28 Dec 08 Turned speedo cable clamp screw (M6), s/steel 1 6 Jan 09 with 1.5mm Φ breather hole Throttle cables: free length = 110mm 2 9 Jan 09 Outer = 900mm Inner = 1022mm Cork liner (3.2mm) for fuel petcock 1 11 Jan 09 Top hat spacer for rear wheel bearing LHS (BMS). 1 24 Jan 09 25mm Φ seal surface, 20mm Φ bore, 30mm Φ collar, collar 1.5mm thick, total height = 14mm Rubber pad - battery 1 1 Feb 09 Nipple holder, brass (front brake cable) 1 7 Feb 09 Guide sleeve, s/steel (front brake cable) 1 7 Feb 09 Washer 8mm ID, s/steel (front brake adjuster) 1 8 Feb 09 Nut, M8 x 1 (13mm AF hex), s/steel (front brake 1 8 Feb 09 adjuster) Flat washer (behind gearbox output shaft castle 1 nut), 15mm ID Front brake cable adjusting nut, s/steel, 10mm AF 1 7 Apr 09 hex, M6 x 1 Generator cover nut M6, 10mm AF hex, s/steel, 2 18 Apr 09 overall length = 28mm Knurled locknut for clutch cable adjuster, s/steel 1 26 Jul 09 M8 x 30 s/steel hex screws, polished heads, for 2 10 Oct 09 new (incorrect) handlebar risers (ex Jan Cornel) M7 x 0.75, 9mm AF s/steel nuts for idle air screw 2 16 Dec 09 Aerotig (Charlie Hamer) welded one fin on tappet 10 Feb 10 cover Flat washer 304 s/steel 25mm OD, 14.3mm ID, 2 7 Mar 10 3.5mm thick, chamfered and polished (front axle) Front & rear axle nuts, 22mm hex 304 s/steel, 3 7 Mar 10 M14x1.5, chamfered and polished Flat washer 304 s/steel 32mm OD, 14.3mm ID, 1 13 Mar 10 4.0mm thick, chamfered and polished (rear axle) Spoke retainer, brass 1 23 Jun 10 Generator cover nut M6, 10mm AF hex, s/steel, 2 21 Aug 10 overall length = 38mm Rev 1.1 Cost R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R10-00 R0-00 R0-00 R0-00 R0-00 R0-00 R10-00 R0-00 R10-00 R0-00 R0-00 R0-00 R0-00 R35-00 R0-00 R0-00 R0-00 R0-00 R0-00 113 Allan‟s BMW R50/2 Restoration (Abridged) PARTS FABRICATED (4) Part Number 36 31 4038241 36 31 2060174 13 11 1252179 11 12 0023160 11 11 0001104 61 31 8 050 134 07 11 9931089 21 52 1 080 176 21 21 0 070 511 21 21 1 231 463 11 81 4 034 216 46 51 4 034 210 24 December 2013 Description Qty Date Top hat spacer for front wheel bearing RHS 1 1 Oct 10 (BMS). 25mm Φ oil seal surface, 20mm Φ bore, 30mm Φ collar, collar 1.5mm thick, total length = 10mm Reducing bush for front wheel bearings set – for 1 1 Oct 10 use on wheel truing/balancing stand Washer, stainless steel 7mm OD, 2.5mm ID, t = 2 16 Oct 10 1.5mm for carb floats Carb vacuum take-off stubs, brass 6mm dia 2 1 Jan 11 Nuts, M8 s/steel polished, SW13, valve cover 2 22 Feb 11 Hex nuts, M10 s/steel 14mm AF, cylinder bases 8 17 Mar 11 Flat washer, 304 s/steel, OD = 30mm, ID = 2 5 Feb 12 8.5mm, 3mm thick, polished, headlight mounting Flat washer 304 s/steel 32mm OD, 14.3mm ID, 1 5 Feb 12 4mm thick, chamfered and polished (front axle) Clutch thrust rod, 205mm long. 7.5mm diameter, 1 12 Feb 12 silver steel, 5x2 O-rings Clutch spacer, 4mm thick 6 Apr 12 Allen CS clutch screw M8x1 x 20 6 12 Jul 12 Battery box for AGM battery 1 1 Jun 13 Front engine mounting stud, 295mm 304 s/steel 1 24 Sep 13 Rear engine mounting stud, 330mm 304 s/steel 1 24 Sep 13 Rev 1.1 Cost R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R10-00 R0-00 R22-38 R81-00 R25-00 R25-00 114 Allan‟s BMW R50/2 Restoration (Abridged) PARTS PROCURED Part Number 36 31 4038258 36 31 4038230 07 11 9985005 07 11 9985010 07 11 9914053 07 11 9922121 26 11 3038225 46 71 1235428 23 41 1232116 16 11 1230263 11 61 0043161 61 21 8042138 46 53 4034150 11 11 0001106 13 11 0042149 13 11 0039274 13 11 0039181-5 13 11 0042126 13 11 0039527 13 11 0039168 13 11 1251394 13 11 0042150 32 72 1230868 13 72 0043524 52 53 9034111 11 14 0002197 11 14 1256562 23 51 1006135 31 41 2000331 23 11 1006124 36 31 4038258 36 31 4038230 07 11 9985005 31 42 2000000 16 11 4080187/9 11 11 0001122 24 December 2013 Description Qty Oil seal TC 25 x 38 x 7 (wheel hubs) Nitrile Oil seal TC 25 x 35 x 7 (front hub) Nitrile 30203 taper roller bearing (swing arms) 30204 taper roller bearing (wheel hubs) M8 x 1 bolts for petrol tank mounting M10 x 1 nuts for front suspension mounting M8 x 50 s/steel bolt for brake bell crank M8 x 75 s/steel bolt for gearbox mounting M12 x 1.5 Nylock nuts for engine mountings M8 x 40 s/steel bolts Rubber sleeve for drive shaft (Hypoid oil) Foot peg rubbers Gear lever rubber sleeve Nitrile gasket for petrol cap Sleeve for carb air pipe on carb side Rubber strap for battery Passenger foot rests Rubber plug for timing hole O-ring for carb slide covers Jet Needles #46-255 for carbs, new Air regulating screw, complete, used Small gasket for idle jet plug screw Slide stop screw & spring, used Slide spring (8mm dia x 70mm long), used Float needle, new Gasket for float cover, new Magura hand grip R/H, new Air filter element, used Front seat mounting bracket (used) Oil seal 20 x 32 x 7 (gen journal) Viton Oil seal 25 x 35 x 7 (magneto hub) Viton Oil seal 17 x 28 x 7 (kickstart, Nitrile 2 lip) Oil seal 22 x 40 x 8(10) (swing arms, Nitrile) Oil seal 15 x 24 x 7 (gear lever, Nitrile 2 lip) Oil seal 25 x 38 x 7 (wheel hubs, Nitrile) Oil seal 25 x 35 x 7 (wheel hubs, Nitrile) M10 x 35 s/steel bolts & nuts (centre stand) M10 s/steel nuts (cylinders) SW17 30203 taper roller bearing (swing arms) 51W/34W taper roller bearings (steer hub) Tank knee pads 6207 crank bearing, NTN 6203 camshaft bearing, Rollway 6004 generator bearing, KBC Oil seal 52 x 72 x 10 (crank rear, Viton) 1 1 2 4 2 4 1 1 4 R8-50 R8-50 R40-00 R120-00 R2-95 R3-40 R34-00 4 1 2 1 1 2 1 2 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 4 1 1 1 2 8 2 2 2 2 2 1 1 R14-20 R70-00 R60-00 R15-00 R15-00 R40-00 R30-00 R80-00 R10-00 R1-00 R140-00 R20-00 R4-00 R12-00 R5-00 R45-00 R8-00 R50-00 R40-00 R20-00 R28-73 R55-03 R6-81 R32-54 R6-59 R8-14 R7-16 Rev 1.1 Cost Supplier Tvl Bearings Tvl Bearings Tvl Bearings Tvl Bearings JKM JKM Bolt & Nut Bolt & Nut R14-47 JKM R78-00 R280-00 R450-00 R76-86 R30-64 R16-43 R70-70 JKM CMC CMC Jan Cornel CMC CMC CMC CMC CMC CMC Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Invicta Invicta Invicta Invicta Invicta Invicta Invicta JKM JKM Invicta Ed Korn = $32 Jan Cornel Invicta Invicta Invicta Invicta 115 Allan‟s BMW R50/2 Restoration (Abridged) PARTS PROCURED (2) Part Number 07 12 9948811 11 61 0043163 61 13 8080160 31 41 2000324 61 13 8070196 33 53 3054296 12 12 8036163 36 31 4001004 36 31 4038258 62 12 8080115 23 11 3038513 23 11 1006179 31 41 2054234 16 12 4084120 16 12 1233520 32 72 1230407 11 11 0033163 11 11 0010161 11 12 0022118 11 12 0023025 11 25 1256483 11 24 0017150 11 21 0016132 11 21 0016130 11 12 0021804 07 11 9985005 07 11 9913457 07 11 9922054 07 11 9911605 07 11 9921606 07 11 9913439 07 11 9922054 24 December 2013 Description Qty S42/9 hose clamps for carb air pipes 3 Gasket for air pipe on transmission housing 2 Rubber sleeve for speedo cable 1 Rubber plug for holes on front swing arm 2 Grommet for headlamp shell 1 Silent blocs for rear suspension (OD = 25mm 2 ID = 12mm, L = 20mm) D-shaped grommet for top of motor (elec) 1 HT cable for spark plugs 1m MS strips for sump, 16 x 3mm thick (3m) 1 Wavy washers, s/steel for rear brng housing 5 Tyres, new 3.50 x 18 Metzeler ME22 2 Tube 3.50 x 18 (King Tube) 1 Oil seal 25 x 38 x 7 Nitrile (rear wheel) 1 Rubber O-ring for speedometer 1 Oil seal 30 x 40 x 7 (g/box input, Viton) 1 Oil seal 36 x 54 x 7 (g/box output, Nitrile) 1 Silent bloc front (OD=22, ID=10, L=16mm) 4 Side stand 1 Rubber beading for tail light fitting 1 Rubber stop for centre stand 1 Rear mudguard for R68, R51/3 (gave to Roly 1 Tilman in exchange for parts) Top nut for Everbest fuel cock (used) 1 Fuel cock fibre gasket, new (returned to Jan) 1 Magura hand grip L/H, new 1 Valve pushrod tube rubber seal, new 4 Cylinder base gasket, 0.5mm Aluminium 2 Cylinder head gasket, new = spare 2 Tappet cover gasket, new 2 Set of piston rings, 1st oversize (68,5mm) 2 Conrod bushing 20mm, new 2 Woodruff key for flywheel, new 1 Lock/spring washer for rear crank bearing 1 Valve guides, standard size, new 4 Total for the above parts from Jan Cornel: 30203 taper roller bearing (swing arms) M6 x 15 s/steel hex screw, washers, nut for front mudguard M8 x 16 s/steel hex screw, washer, nut, for rear mudguard M6 x 16 s/steel hex screw, washers, nut, for rear mudguard Rev 1.1 2 2 Cost R2-00 R40-00 R15-00 R30-00 R10-00 R50-00 Supplier CMC CMC CMC CMC CMC CMC R10-00 R8-00 R18-00 R0-00 R650-00 R50-00 R8-00 R0-00 R38.51 R21-49 R100-00 R25-00 R10-00 R20-00 R650-00 CMC Blitz Fleet Steel Stock Mosskays Mosskays Bearing Man Stock Bearing Man Bearing Man CMC CMC CMC CMC CMC E1.68 E0.25 E5.62 E13.68 E5.04 E8.06 E6.38 E32.72 E12.78 E1.28 E1.51 E26.20 R1700-00 Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel Jan Cornel R78-00 Invicta (BMG) R0-00 Stock 1 R0-00 Stock 2 R0-00 Stock 116 Allan‟s BMW R50/2 Restoration (Abridged) PARTS PROCURED (3) Part Number 13 11 1252178 13 11 0042111 23 51 4034257 11 34 0026110 61 32 8048185 12 12 8002172 61 31 8048165 46 61 5090116 07 11 9919216 07 11 9912455 46 62 5096122 11 11 0002172 11 34 1251472 11 61 0043175 11 11 0001106 63 12 8050157 62 12 8080180 18 11 4090110 12 31 8002106 36 31 4038217 24 December 2013 Description Qty Float guide pins for carbs 2 Rubber sleeve for throttle cable at carb 2 Kick start rubber bumper 1 Inner valve spring 2 Valve spring set (2 x outer, 2 x inner) 1 Ignition switch cover slide 1 Spring, ignition advance, 9mm 1 Brake light switch 1 Front fender brace 18” 1 Drain plug driveshaft 14mm hex, M10x1 1 Speedo chrome bezel VDO 1 HiLo switch chrome universal dim/bright 1 Idle jet slotted #40 = spare 2 TOTAL incl VAT & shipping from Uli‟s: M8 x 30 s/steel hex screw, washers, nut, for 2 rear mudguard 12 x M6 x 25 s/steel bolts, 12 x M6 s/steel Lot Nylock nuts, 6 x M8 s/steel Nylock nuts, 4 x M8 x 30 s/steel bolts & nuts Rear mudguard, tail light, used, complete 1 Timing gear cover gasket 1 Exhaust valve (1126), new, plus 2 Bracket hardware for kickstart rubber, new 1 Carb air pipe (RHS), used 1 Grommet for speedo cable at headlamp 1 Rubber plug for timing hole 1 Rubber plugs for mudguard holes 2 Rubber washer 30mm OD at headlight 4 Courier charge pro rata for Bill Speight parts 1 Seal ring headlight lens, new 1 Rubber boot for throttle cables on perch, new 1 Speedo cable, new 1 Exhaust nut, new 1 Generator brushes, new 2 Reinforced rubber fuel hose (ID = 6mm) new 1m Bushing for ignition key, used 1 Alloy wheel, complete, used 1 Steel wheel rim 2.15 x 18” chrome plated 1 (Stamped 245 1 64 410 41), used, rusted Rev 1.1 Cost E3.60 E3.00 E8.90 E5.80 E12.00 E2.92 E1.70 E5.95 E23.15 E2.56 E15.70 E11.19 E5.24 E110-00 R0-00 Supplier Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Uli‟s Paid to P. Beukes Stock R47-10 JKM R1200 John Wightman R5-00 CMC R678-00 Uli‟s (P Beukes) R20-00 R10-00 R10-00 R 8-00 R 8-00 R15-00 E1-50 E2-20 E13-40 E10-25 E5-00 R15-00 R0-00 R0-00 R0-00 CMC Bill Speight Bill Speight Bill Speight Bill Speight Speed Services Uli‟s (1007) Uli‟s (30037) Uli‟s (1016) Uli‟s (9016) Uli‟s (1019) ProAuto Rubber Jan Cornel Roly Tilman Roly Tilman 117 Allan‟s BMW R50/2 Restoration (Abridged) PARTS PROCURED (4) Part Number 61 13 8070232 18 12 4090087 18 12 4090088 07 11 9963470 07 11 9981214 07 11 9981219 07 11 9981408 07 11 9981416 07 11 9982409 07 11 9951461 07 11 9934100 18 11 4090073 32 71 2072129 26 11 3038225 36 31 4038230 13 72 0043536 36 31 4001004 36 32 4038195 07 12 9948830 07 12 9948839 36 31 4038222 36 32 4038195 12 31 8030106 12 12 8002172 12 12 1353604 13 72 1250389 11 12 0022118 36 31 4038217 07 11 9912455 51 16 2072296 12 11 9058248 32 71 2072306 71 11 9090070 21 52 2072321 61 33 8046030 24 December 2013 Description Qty Cost Cable clips, used 2 R0-00 Exhaust silencer s/steel (RHS), new 1 R700-00 Exhaust silencer s/steel (LHS), new 1 R700-00 Rubber boots for plug caps, new 2 R2-00 Exhaust copper crush gaskets 35x41x2.5 2 R20-00 Gearbox bearing 6203 C3 SKF 1 R26-31 Gearbox bearing 6204 C3 SKF 2 R61-61 Gearbox bearing 6302 C3 SKF 1 R30-84 Gearbox bearing 6303 C3 SKF 1 R34-82 Gearbox bearing 3203 B TVH C3 FAG 1 R140-00 Woodruff key 4 x 6.5mm, g/box output shaft 1 R3-81 17 x 1 mm external circlip, g/box output shaft 2 R0-55 Exhaust headers, fabricated & electroplated 2 R500-00 Handle bar, used but newly electroplated 1 R250-00 M12 x 30 s/steel bolt, passenger foot rests 2 R15-00 Cork gasket material 3.2mm for fuel petcock 1 R82-00 In-line fuel filters 2 R30-00 6V 3W lamp for parking light 1 R8-00 Battery (B49-6), 6V 8Ahr, new 1 R160-00 Rubber sleeve for drive shaft (Hypoid oil) 1 R75-00 Oil seal TC 25 x 35 x 6, Nitrile 2 R10-00 O-ring for air filter element (6 x 55mm) 1 R30-00 Inner tube 3.50” x 18” 1 R111-00 Rim tape 18” 1 A70/9 hose clamp, used 1 R0-00 A90/9 hose clamp, used 1 R0-00 New front brake bonded linings (4mm thick) Lot R100-00 and drum skimmed 140mm x M4 chromed spokes, with nipples, 70 R1470Uli‟s part #6044 00 New rear brake bonded linings (4mm thick) Lot R162-00 and drum skimmed Rim tape, 18” new 1 R16-00 Condensor (Echlin EP258), new 1 R25-00 Spring, ignition advance, 9mm 1 R0-00 Spark plug caps, NGK LZFH, new 2 R0-00 Air filter element, BMW OEM Purolator 1042 1 R396-22 Cylinder head gasket, BMW OEM, new 2 R65-00 Steel wheel rim 2.15 x 18” chrome plated 1 R300-00 (Stamped 245 1 64 410 41), used, buckled S/Steel M8 x 30 bolts for handlebar risers 6 R26-20 Rear view mirrors (Taiwan), new 2 R140-00 Ignition point set, new 1 R0-00 Handlebar risers, used 2 R0-00 Tyre pump (E20 x R11.08) 1 R220-00 Clutch cable (E7.20 x R11.08) 1 R80-00 Horn 6V, chrome, new 1 R220-00 Rev 1.1 Supplier Roly Tilman Jeff Talbot Jeff Talbot Blitz Jan Cornel SKF SKF SKF SKF Bearing & Belting JKM JKM CMC Jan Cornel JKM Wizard Midas Randburg M/Cycle Randburg M/Cycle Jan Cornel CMC/Bill Speight BMG BMG Randburg M/Cycle House of BM House of BM Hercules Brake & Clutch Uli‟s (via R&S) CBF, Strijdom Park Randburg M/Cycle Blitz Motor Spares Jan Cornel NGK Spark Plugs Northside M/c Northside M/c Jan Cornel JKM Jan Cornel Jan Cornel Melville Price P Beukes (Uli‟s) P Beukes (Uli‟s) Jan Cornel 118 Allan‟s BMW R50/2 Restoration (Abridged) PARTS PROCURED (5) Part Number 36 32 4038195 18 11 4090073 18 11 4090074 18 11 4090248 13 11 0039527 13 11 0039187 36 31 4038173 32 72 2072223 11 14 0002177/8 07 11 9978006 07 11 9963086 07 11 9963242 33 12 3004337 33 12 3004343 33 12 3038257 07 11 9933642 13 11 0039187 13 11 1251395 13 11 0039181 34 11 2072345 13 11 0 039 241 21 21 0 070 182 21 21 0 070 166 21 21 0 070 060 21 21 0 070 157 21 21 0 070 149 24 December 2013 Description M8 x 20 s/steel hex screw, nut, washer, spring washer, for horn mounting Rim tape, 18”, new Exhaust pipe L, 304 s/steel, new Exhaust pipe R, 304 s/steel, new Exhaust balance tube, 304 s/steel, new Idle stop screw & spring (used) Float 7g (used) Spoke retainer, brass (new) Perch wedge, hardened (used) Engine/generator cover, flat (NOS) External circlip, 10mm 6V 35/35W headlamp globe, new Copper washer for M10 plugs Copper washer for M14 plugs Oil seal 30 x 42 x 7 (final drive), Nitrile Oil seal 65 x 85 x 10 (final drive), Nitrile 20mm x 230 mm 431 s/steel for front axle 25mm x 430mm 431 s/steel for rear axle Oil seal 28 x 47 x 7 (final drive), Nitrile Piston pin circlip C20 Float 7gr Float lever, new version Mixture regulation screw, long Brake cable, new Carb main jet 120 Licence disc holder, Sterling Clutch diaphragm spring, heavy duty, used Clutch pressure plate, used Clutch friction disc, 8.5mm thick, used Clutch pressure ring, flat (only for use with 9mm clutch friction plate), to be used with 511 hardened spacer washers, used Clutch pressure ring, stepped (only for use with 7mm clutch friction plate), used Through-hardened steel flat washer, cylinder head studs CSB GP645, 6V 4.5Ahr AGM battery Plastic box 160x96x67 for battery Rev 1.1 Qty 1 Cost Supplier R0-00 Stock 3 1 1 1 1 1 3 2 1 2 1 2 2 1 1 1 1 1 4 1 1 1 1 2 1 1 R15-00 CMC R1544-70 Powerflow Powerflow Powerflow R0-00 Roly Tilman R0-00 Roly Tilman R0-00 Jan Cornel R0-00 Jan Cornel R0-00 Craig Patterson R0-35 JKM R0-00 Mike Lester R5-00 JKM R4-55 JKM R6-76 BMG R15-89 BMG R35-00 Diversified Alloys R65-00 Diversified Alloys R15-00 BMG E5.00 Uli‟s 14202 E23.50 Uli‟s 8049 E1.75 Uli‟s 51395 E5.80 Uli„s 18049s E8.10 Uli‟s 5055 R0-00 Jan Cornel swap R14-00 Main Reef Midas R0-00 Rob Dercksen 1 1 1 R0-00 Rob Dercksen R0-00 Rob Dercksen R0-00 Rob Dercksen 1 R0-00 Rob Dercksen 8 R8-50 Northern Bolt 1 1 R68-00 Current Autom‟n R81-00 Communica 119 Allan‟s BMW R50/2 Restoration (Abridged) STAINLESS STEEL PARTS Part Number 07 11 9913625 07 11 9922082 13 11 0039156 07 11 9940396 31 41 2000345 34 11 2060182 07 11 9922093 07 11 9913227 07 11 9922036 07 11 9913625 07 11 9922082 07 11 9913444 07 11 9922054 31 41 2000295 23 22 1030176 23 22 1030176 07 11 9923412 07 11 9923412 23 11 1030174 34 11 2072444 23 41 1066286 07 11 9921605 34 11 2060178 11 14 0002191 32 72 2072221 13 11 0039184 07 11 9931089 07 11 9922155 36 31 3007378 36 31 3004168 07 11 9912505 07 11 9912551 07 11 9912620 07 11 9922110 07 11 9932070 07 11 9912455 07 11 9931065 24 December 2013 Description M8 x 20 hex screw, nut, washer, spring washer, for horn mounting Screws M5 x 16, carb float chamber Pivot pin for foot brake bell crank (304) Flat washer 25mm OD, 10.5mm ID bevelled polished, shock mounting, fork yoke plate M6 x 20 studs, engine sump cover Front brake swivel pins (304), polished M4 screw, slotted for tail light Dome nuts M8 x 1 (303) for drive shaft tube mounting studs, polished (special) M5 x 10 hex screw, washer, nut, polished, for front mudguard M8 x 20 hex screw, washers, nut, polished, for front mudguard M6 x 16 hex screw, washers, nut, polished, for rear mudguard Steering damper bolt, M8 (special) Clutch cable bushing, polished Speedo cable drive bushing, polished M8 castellated nuts for steering damper M8 castellated nut for rear brake bell crank Speedo cable clamp hex screw (M6x20), with 1.5mm Φ breather hole, polished Guide sleeve, front brake cable Washer 8mm ID, front brake adjuster Nut M8x1 (13mm hex), front brake adjuster Front brake cable adjusting nut, 10mm AF hex, M6 x 1 (special) Generator cover nut M6, 10mm AF hex, 28mm long, s/steel Knurled locknut for clutch cable adjuster M7 x 0.75, 9mm AF nuts for idle air screw Flat washer s/steel 25mm OD, 14.3mm ID, 3.5mm thick, chamfered polished (front axle) Front & rear axle nuts, 22mm hex 304 s/steel, M14x1.5, chamfered and polished Flat washer s/steel 32mm OD, 14.3mm ID, 4.0mm thick, chamfered polished (rear axle) Hex bolt M8 x 50 for brake bell crank Hex bolt M8 x 75 for gearbox mounting Hex bolt M10 x 35 & nuts (centre stand) Hex nut M10 (cylinders) SW17 Wavy washer B6, crank rear b/ring housing M8 x 30 hex screw for rear mudguard stay Flat washer 8.4 for rear mudguard & stay Rev 1.1 Qty 1 Cost Supplier R0-00 Stock 4 1 8 R0-00 Fabricated R0-00 Fabricated R0-00 Fabricated 12 2 1 4 R0-00 R0-00 R0-00 R9-00 2 R0-00 Fabricated 2 R0-00 Fabricated 4 R0-00 Fabricated 1 1 1 2 1 1 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 1 1 1 1 R0-00 R0-00 R10-00 R10-00 Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Stock Fabricated Fabricated Fabricated 2 R0-00 Fabricated 1 2 2 R0-00 Fabricated R0-00 Fabricated R0-00 Fabricated 3 R0-00 Fabricated 1 R0-00 Fabricated 1 1 2 8 5 2 4 R34-00 Bolt & Nut Bolt & Nut JKM JKM R0-00 Stock R0-00 Stock R0-00 Stock 120 Allan‟s BMW R50/2 Restoration (Abridged) STAINLESS STEEL PARTS (2) Part Number 46 62 5096152 46 62 5096152 07 11 9913457 07 11 9922054 07 11 9911605 07 11 9921606 07 11 9913439 07 11 9922054 07 11 9913891 07 11 9936246 11 11 0002195 13 11 1252179 11 12 0023160 07 11 9932094 07 11 9914345 07 11 9914347 07 11 9922110 07 11 9933109 07 11 9914625 07 11 9921626 11 11 0001104 61 31 8050134 07 11 9931089 11 81 4034216 46 51 4034210 24 December 2013 Description M8 dome nuts for rear mudguard & stay M8 dome nuts for top engine mounting M6 x 15 hex screw, washers, nut for front mudguard M8 x 16 hex screw, washer, nut, for rear mudguard M6x16 hex screw, washers, nut, rear mudguard 12 x M6 x 25 bolts, 12 x M6 Nylock nuts, 6 x M8 Nylock nuts, 4 x M8 x 30 bolts & nuts Hex bolt M12 x 30, passenger foot rests Lock washer 12.5mm, passenger footrests Generator cover nut M6, 10mm AF hex, s/steel, overall length = 38mm Washer, stainless steel 7mm OD, 2.5mm ID, t = 1.5mm, carb floats Hex nut, 13mm AF, s/steel M8, valve covers B8 wavy washers, valve covers Hex bolt M10 x 45mm, front shock upper Hex bolt M10 x 50mm, front shock lower Hex nut M10, A4, front shock mounting Lock washer 10mm, front shock mounting Hex bolt M12 x 45mm, rear shock mounting Hex nut M12, A2, rear shock mounting Hex nut, M10 s/steel 14mm AF, cylinder base Flat washer, OD = 30mm, ID = 8.5mm, 3mm thick, bevelled, polished, headlight mounting Flat washer 32mm OD, 14.3mm ID, 4mm thick, chamfered and polished (front axle) Front engine mounting stud, 295mm s/steel Rear engine mounting stud, 330mm s/steel Rev 1.1 Qty 4 2 2 Cost Supplier R0-00 Stock R0-00 Stock R0-00 Stock 1 R0-00 Stock 2 R0-00 Stock Lot R47-10 JKM 2 2 2 R15-00 JKM R0-00 Stock R0-00 Fabricated 2 R0-00 Fabricated 2 2 2 2 4 4 1 1 8 2 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R7-65 R2-75 R0-00 R0-00 1 R0-00 Fabricated 1 1 R25-00 Fabricated R25-00 Fabricated Fabricated Stock Stock Stock Stock Stock JKM JKM Fabricated Fabricated 121 Allan‟s BMW R50/2 Restoration (Abridged) TOOLS PROCURED Part Number Matra 442 Matra 338/1 Description Qty Matra R1/7 BMG valve guide reamer 7K7 1 C/pin-spanner for exhaust clamps 1 Multi spanner 1 Heyco flat spanner 10/11 1 Heyco flat spanner 12/13 1 Walter flat spanner 10/13 1 V 5030 Magneto/generator extractor M8 bolt (HT) 1 Swing arm bearing extractor 1 Matra 292 Flywheel clamp & multi-tool 1 Gedore 41mm socket ¾” drive 1 ¾” to ½” converter for 41mm socket 1 Set metric tube spanners (Fragram) 1 Matra 534 M8 x 1 x 30mm bolts for flywheel removal (HT) 3 Tommy bar for toolkit 1 5127 Mild steel drift for valve guide replacement 1 Inclined block for cyl head valve guide work 1 Matra 530a Aluminium drift to set valve pushrod tubes 1 V 5035 Wood support for conrod & piston 2 W 5039 Pressure cylinder to refit crank shaft gear 1 Matra 311 Flywheel puller using M16 x 1,5 x 40mm bolt & 1 nut, 2 x M10 x 1 x 25 HT bolts, 12mm plate Wheel tube (wheel bearing removal and fit) 1 W 5038 Pressure bush (pipe) 1 V 5040 Pressure bush (pipe) 1 Pliers (Hapewe) 1 Tyre levers Magura 2 Plug spanner 1 Reversible screwdriver 1 Plug spanner 1 Feeler gauge 1 Matra 494/3 Gearbox output flange castellated nut driver 1 Angle iron vise-mounting bracket for gearbox 1 Matra 501 Puller for flange on gearbox output shaft 1 Matra 500 Gearbox output flange clamp/stay 1 Spoke wrench, using 16mm Φ EN8 1 Points setting tool 1 Spark plug extensions (for shorting out plugs) 2 Matra 517 Heavy duty wheel hub pin spanner (36 3 650) 1 111 600 Pushrod tube hollow drift 1 Matra 529 Clutch centring arbour 1 Matra 513 T-handle pin spanner (rear swing arm adjuster) 1 Wheel trueing/balancing stand 1 Carb float lever height gauge 1 71119090123 Spanner 36/41mm, steering head 1 Spanner 14mm ring/flat, ground & bent 1 506a Pin wrench, final drive pinion removal 1 6V constant voltage battery charger (AGM) 1 Gearbox cover, milled flat 1 24 December 2013 Rev 1.1 Cost R0-00 R0-00 R0-00 R10-00 R10-00 R10-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R16-00 Supplier Al Gibson Jimmy D*** Zane Mannell Piston Ring Club Piston Ring Club Piston Ring Club Fabricated/JKM Fabricated Fabricated Piston Ring Tool Shop Just Tools JKM Stock Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated (JKM) R0-00 R0-00 R0-00 R20-00 R0-00 R10-00 R11-40 R11-40 R16-79 R10-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R0-00 R8-50 R13-00 R60-00 R0-00 R0-00 Fabricated Fabricated Fabricated Piston Ring Swap Stock Piston Ring Swap Autozone Autozone Unnic Midas Fabricated/Makro Stock/Fabricated Zane Mannell Stock/Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fabricated Fleet St ExecuPawn Fabricated Fabricated Fabricated R0-00 R0-00 R50-00 R70-00 R20-00 122 Allan‟s BMW R50/2 Restoration (Abridged) NOTES 1. 2. 3. 4. 5. 6. 7. 8. 9. 10. 11. 12. 13. 14. 15. 16. 17. 18. 19. 20. 21. 22. 23. 24. 25. 26. Brake pedal stops against foot peg rubber – confirmed by Jan Cornel. Clymer workshop manual only - (there is no Haynes manual for an R50/2). Found a Chilton‟s Repair & Tune-Up Guide at “Bike Hospital”. Neutral indicator provides a short to earth (when in neutral) Use 3 x M8 x 1 bolts and nuts to remove clutch Clutch plate = F&S, pressure plate = BMW part for /5, spring diaphragm looks new. Clutch push rod appears to have been shortened to 195mm (original length could be 205mm). There is also a sleeve fitted to the clutch push rod at the thrust bearing end. Gearbox bell housing webs have been ground to clear bolts on later clutch/pressure plate. Exhaust thread on cylinder heads = M45 x 2 Improved steering head bearing = SSW055 or MCI 51W & 34W taper roller bearings (34 x 51 x 12mm). Note: The /5 taper roller bearings cannot be used! Pistons = 1st oversize = 68.42mm, clearance spec = 0.08mm. Markings on piston crown = 68.42, Sp 0.08, Vorn, C1, Made in Germany, 150E 059. Markings inside piston = 1275, 068079, 4.2 (all cast into the inside wall of the piston) no manufacturer. Rule-of-thumb for piston ring end gaps is 0.004” to 0.005” per inch of bore for air-cooled engines (0.1mm to 0.125mm per 25.4mm of bore). The BMW spec is 0.25mm to 0.4mm, compared with the rule of thumb of 0.27mm to 0.34mm for a bore of 68,5mm. Jan Cornel confirmed making M6 studs for sump cover is preferable to M6 bolts. Done. Al Gibson says use Caustic Soda to remove muck from slingers. Suitable tyres = Metzeler ME22 3.50 x 18; Michelin Macadam 50 100/90 x 18; Bridgestone S11 100/90 x 18, Yokohama 100/90 x 18; Cheng Shin Hi Max C906 100/90 x 18 Metzeler ME22 tread depth = 6mm when new. Shidawei Rubber say Nitrile better for fuel resistance than Neoprene. Smear a thin layer of silicon grease inside tube portion of pushrod tube rubbers when fitting. Al Gibson says Phosphor Bronze is not a good idea for exhaust valve guides – he has had cases where the material burns away to a chalky substance. He says use Aluminium Bronze for valve guides - exhausts need a bit more clearance than inlets (he thinks 2.5 thou for exhausts). Blueprint Engineering quoted me R1400 incl VAT for 2 x cylinder head recon. They make their own valve guides from phosphor bronze. They send out rocker tip grinding to Camtech Set carbs leaner for high compression R50S pistons. Note that to remove wheel bearings, use the Duane Ausherman method – insert axle from the “wrong” direction, use a pipe spacer and tighten the axle nut to contain the bearing assembly as a unit. Then tap the entire bearing assembly out of the hub using a rubber mallet or nylon hammer. The same pipe spacers are used to set the preload. To refit the bearings, place the axle through the bearing assemble from the correct direction, fit the pipe spacer and tighten the axle nut (nipped). Tap the entire bearing assembly back into the hub from the “threaded” end, taking care to ensure that the axle is straight. Peter Posniak says hydrochloric acid will remove chrome plating, then sand or wire brush to remove the nickel layer. Mark Bell of Pratley‟s advised Pratley Quickset White for ceramic, but maximum temp is still only 100 – 120 deg C. Craig Harmse of Chemence confirmed RT20G = high temperature retainer. New piston rings from Uli‟s were NOT marked “TOP”. The top ring is chromed and the bevel on the inside of the ring faces the TOP of the piston. The second ring appears to be a PLAIN ring. Only one is marked TOP – difficult to say which side is TOP on the other ring. The oil ring is fitted with the bevel/chamfer on the outer edge at the TOP. Uli telephonically confirmed he would post a new second ring to me at their expense. A set of two middle rings (with steps) was received in the post from Uli‟s on 3 April 2008 (Customs clearance = R12-00). Note that the steps face down on the piston. Charlie Hamer of Aero Tig says to weld Aluminium use Tig AC. 24 December 2013 Rev 1.1 123 Allan‟s BMW R50/2 Restoration (Abridged) 27. 28. 29. 30. 31. 32. 33. 34. 35. 36. 37. 38. 39. 40. 41. 42. 43. 44. New valve guides are 43mm long vs 50mm for the old guides. Length from top of guide to top of circlip = 8,5mm (new) and 15,9mm (old). Jan Cornel says the 43mm long guides are fine. Also, the next time guides need to be replaced use the next oversize OD = 13,15mm or larger. Jan Cornel also recommended light knurling of loose valve guide to fit oversize hole. Preferable to use straight knurling. Mike Lester confirmed tubular rear mudguard stays are 12mm diameter thin wall tubing with 4mm thick plate (shaped) welded to ends. He suggested screws instead of rivets to attach the stays to the mudguard – peen the ends of screws beyond the nuts. Mike Lester provided dimensions of front brake cable swivels = 10mm diameter, with 4mm wide groove to result in 5mm diameter step, and 1mm wide end piece. Hole through swivel to suit brake cable adjuster = 6,2mm diameter, length through yoke = 15,5mm. Battery = Yuasa B38-6A 13 Ahr, 6V (L x W x H=119 x 83 x 161mm = 411/16“ x 3¼” x 65/16”). My battery = MS B49-6, 8 Ahr (Maan Shyang) from Battery Centre. Rotate front brake adjuster anticlockwise to reduce free play (rotate clockwise to increase play between leading brake shoe and drum) For refitting, Jan heats crankshaft gear on a metal plate with oxy-acetylene flame until it just starts to change colour. Mark Huggett (slash2 Group) says ACM (acrylic rubber) or FKM (Fluoride rubber) material is used in applications with hypoid oil due to their high chemical and temperature resistance. NBR (Nitrile) seals are only hypoid resistant to 80 deg C and harden when exposed to hypoid oils. NBR is also not suitable for the rear crank main seal due to the high temperature experienced (in excess of 120 deg C) – he recommends the KACO silicon seal for this application. Mark Huggett also says use 6207 bearings with massive aluminium or brass cages made out of 2 halves riveted together (BMW part # 07 11 9 981 245) or with Pertinax cages. The rear bearing can exceed 120 deg C. Most modern standard 6207 bearings use a thin steel cage which is spot welded together and cannot carry the load (DIN625) in the BMW motors. At one stage BMW specified nylon cages (TN), but these are no longer available. Do not use bearings with modern glass fibre reinforced polyamide cages which are only suitable up to 80 deg C. Plastic cages become hard and brittle at 120 deg C and also fail with time. Ron Cichowski (slash2 Group) says the connection between the crank and the flywheel is supposed to be assembled clean and dry. It is a locking taper and transmits the torque of the engine to the transmission. The Woodruff key is only used to locate the timing marks correctly and there must be a clearance between the top of the key and the flywheel taper keyway to prevent runout of the flywheel lateral face. Note that the keyway in the flywheel taper will NOT push the Woodruff key into alignment – the key must be correctly seated in its slot first. BMW Service Bulletin 5/66 (234) states that for the later rotating valves, the exhaust valve guides must be counterbored 8mm diameter for a distance of 5mm on the port side to prevent seizing of valves. BMW Service Bulletin 12/59 (166) says heat cylinder head to 356 deg F (180 deg C) to remove old valve guides. BMW Service Bulletin 8/67 (258) states that the flywheel mounting screw must be tightened to 159 + 14.5ft.lbs (22 + 2mkp) = 225 - 230Nm. Bronze valve guides should be reamed dry. Use a THIN layer of Hylomar on both sides of the cylinder base gasket. Install cylinder head and tappet cover gaskets DRY. Ron Cichowski of the Slash2 Group recommends cutting a clearance slot in the rubber pushrod tube seals purchased from Uli‟s in order to ensure that the oil splash hole from the engine casing to the pushrod tubes is clear. Use a Dremel-type tool with a fresh coarse sanding drum on medium speed to cut a half-moon shape at an angle to encourage oil flow into the pushrod tubes, and hence into the valve covers. Require colder spark plugs for increased compression ratio. NGK B8ES is colder than NGK B7ES. Specs for BMW R50S say use Bosch W240T1 (= NGK B7ES) for running in and thereafter use Bosch W260T1 (= NGK B8ES) 24 December 2013 Rev 1.1 124 Allan‟s BMW R50/2 Restoration (Abridged) 45. 46. 47. 48. 49. 50. 51. 52. 53. 54. 55. 56. 57. 58. 59. 60. 61. 62. 63. 64. Spark plug equivalents: Bosch W240T2 = Bosch W4CC = NGK B8ES/BP7ES Bosch W260T2 = Bosch W3CC = NGK B8ES/BP8ES (colder than W4CC and B7ES) Jan Cornel confirmed NGK B7ES is the correct plug for the R50/2. He says it also works well in the R69S. He said the BP7ES range did not exist before 1968, so extended insulator plugs not required. Jan Cornel says use SAE 40 oil in engine and gearbox, but use SAE 90 oil in final drive. Need to be careful to use GL4 and NOT GL5 which attacks brass components. All gearbox bearings should be increased clearance C3 with pressed steel cages. Gearbox output flange taper joint to be fitted with clean, dry mating surfaces. The key is no longer required. Fit a 15mm ID flat washer behind the castellated nut. Jan Cornel showed me how to bend gear selector forks – clamp both fork ends in the vice and use a long ½” socket extension bar hooked over the single lever end – the barrel projection fits through the hole in the female end. I should have checked and corrected gearshift shaft axial end-play. Brake shoes can be bonded with 4mm thick friction material, also the clutch friction disk. Generator electrical terminal screws are M5. Magneto electrical terminal screws are M4.5 (~ 2BA). Jan Cornel gave me the following Bowden control cable specs: Throttle = 910mm (outer), 1030mm (inner) incl nipples Clutch = 1060mm (outer), 1340mm (inner) Brake = 1095mm (outer), 1300mm (inner) Craig Vechorik on the Slash2 Group confirmed the following throttle cable lengths for low (Euro) handlebars: 13 21 2072370 = outer = 911mm overall length = 1028mm 13 21 2072370F = outer = 904mm overall length = 1026mm Based on the above and my BMW, I fabricated cables as follows: Outer sheath = 900mm inner = 1022mm (incl nipples) free length = 110mm Note free length is usually measured from cable end cap to inside edge of nipple. This is the length of travel of the cable inner. Throttle nipple = 3.2mm Φ x 6mm L Carb nipple = 3.2mm Φ x 6.5mm L End caps = 6.35mm OD x 5mm ID (for 8.5mm) x 10mm long with 2.0mm hole in closed end. Wheel rims are measured across the inside of the rim where the tyre bead seats – for the R50/2, the rim size is 2.15” x 18”: Spoke size for R50/2 = 140mm x 3.5mm (M4), qty = 40 per wheel. Note that the spoke diameter is measured over the rolled thread – this is a greater diameter than the spoke. BMW M4 spokes measure 3.5mm over the body of the spoke. Mark Huggett says “an M4 spoke is a 3.5mm wire with rolled thread giving a diameter of 3.75mm or M4”. Wheel offset spec= 6.0mm – 6.5mm on the brake drum side. Most of the original supplied spokes and nipples are marked with a 4-leaf clover = “Berg Union”. In Uli‟s terminology, the spokes for my wheels are “double crossed”, 140mm x 3.5mm (#6044) for steel chromed spokes and nipples Carb idle air screw thread = M7 x 0.75 Use 25 x 38 x 6mm double lip Nitrile seals for inner wheel hubs Top hat spacers for wheel axles have different dimensions for LHS and RHS. The LHS top hat spacer = 14mm long/wide and the RHS spacer = 10mm long/wide. 24 December 2013 Rev 1.1 125 Allan‟s BMW R50/2 Restoration (Abridged) 65. 66. 67. 68. 69. 70. 71. 72. 73. 74. 75. 76. 77. 78. 79. 80. 81. 82. 83. 84. 85. 86. 87. Set static ignition timing in accordance with guidelines from Craig Vechorik. First, align the “S” mark on the flywheel with the mark on the crankcase. Then ensure that the mark on the magneto rotor aligns with the mark on the magneto body when the magneto body is in the middle of its adjustment range – this is the “abrisz” or e-point. The important thing to note is that the static ignition timing is set by rotating the contact breaker points base plate, and NOT the magneto body, while the flywheel “S” mark is aligned with the mark on the crankcase. Connect a test lamp and suitable battery across the ignition points (first disconnect the wire to the magneto coil). The test lamp must extinguish as the “S” mark aligns with the crankcase mark when the engine is rotated. Rotate the contact breaker points base plate clockwise to advance the ignition timing and counter-clockwise to retard the ignition timing (note that the centrifugal advance mechanism will need to be removed to rotate the points base plate). The points gap can also be increased to advance the ignition timing (anywhere between 0.4 and 0.5mm = OK). Final ignition timing is set dynamically using a timing light (powered by a separate 12V battery). Increase the engine revs slowly while viewing the marks on the circumference of the flywheel. At about midrange (3800 rpm), the “F” mark on the periphery of the flywheel must align with the mark on the crankcase. The timing should not advance any further as the engine speed is increased. The limit spring on the centrifugal advance mechanism can be adjusted to ensure that the timing does not advance beyond the “F” mark. The limit for differential timing between the two cylinders is 2 degrees = 4mm on the flywheel circumference with a flywheel diameter of 220mm. Duane Ausherman says it will not make much difference if the differential timing is up to about 8mm = 4 degrees. Beyond this limit, it will be necessary to tap the nose of the magneto rotor and centrifugal advance mechanism with a hammer to alter the alignment on the taper fit between the magneto rotor and the camshaft. OT = “oberer totpunkt” = TDC. This mark is used when setting valve clearances. S = “spätzündung” = minimum advance spark = static/low rpm timing (“retarded ignition”) F = “frühzündung” = spark advanced = dynamic timing („advanced ignition”) Spark plug caps supplied with my „bike were BERU, 5k ohm. Mark Huggett says the original spark plug caps are 1k ohm “BERU” Craig Vechorik says use only spark plug caps with zero resistance. Both centrifugal advance springs appear to be the same length = 9mm. (May need to be 11mm) Bowden OEM cable adjusting screws are plated brass, threaded M7 x 1 (my non-OEM clutch cable screw is 5/16” BSW) OEM mirrors = Albert or Bumm, OEM fuel tank cap = BLAU New BMW OEM cylinder head gaskets = Victor Reinz, AFM 200, 1.00mm thick with no steel reinforcing ring. Engine oil temperature = 80 – 90 deg C on a hot day (says Gawie Nienaber) R50S and R69S barrel fins are round, and cylinder heads have 6 bolts holding them down. Jan Cornel says I can use washers under the cylinder head bolts (instead of turning down the rocker stands) Jan Cornel also showed me it may be necessary to drill (ream) out the cylinder head holes for the bolts – they can close up on the bolts – using a 10mm drillbit or reamer. Duane Ausherman says use normal grease in wheel bearings, not the stringy grease for car wheel bearings. Use paper from Corn Flake packets as gaskets for the horn diaphragm. Jeff Talbot says do not use stainless steel for exhaust headers – they do not carry the heat away from the cylinder head as well as mild steel. Use thick wall mild steel tubing for more effective heat conduction. New style piston pin snap ring has loops = 07 11 9933643 (Jan says use old style snap rings) Jan Cornel says use Nitrile oil seals except for engine main crank seal = Viton. How to set carb float levels? See Bing carb manual and Service Bulletin 257b. Set lever at 22mm from cover surface when resting on needle. Set tab so that lever moves another 4mm when fully open. New main jet = 120 (up from 105) in 1967/8 for R50/2. 24 December 2013 Rev 1.1 126 Allan‟s BMW R50/2 Restoration (Abridged) LESSONS LEARNT 1. 2. 3. 4. 5. 6. 7. 8. 9. 10. 11. Do NOT re-chrome wheel spokes and nipples. The hydrochloric acid used to clean the old parts dissolves the zinc in the brass nipples (leaving soft copper in the threaded portion), as well as reduces the diameter of the spoke where it has eaten the rust away. Do NOT take motorcycle engineering work to an automotive engineering works – they are NOT geared up to machine motorcycle engines. Do NOT use bearings with modern glass fibre reinforced polyamide cages (which are only suitable up to 80° C) in motorcycle engines and gearboxes. Plastic cages become hard and brittle at 120° C and also fail with time. Do NOT use cheap studding to fabricate new studs for engine and gearbox casings. Rather fabricate new studs from suitable high tensile bolts. Do NOT bead blast aluminium parts with an air pressure higher than 300kPa. Do NOT have motorcycle brake drums skimmed by shops that have not been recommended. Do NOT re-use old piston pin wire clips (snap rings) Do NOT fit resistor suppressed spark plug caps, or resistance/suppressed HT leads. DO check the crankshaft for truth / alignment. DO check valve spring installed heights. DO check that pistons and conrods weigh the same. 24 December 2013 Rev 1.1 127 Allan‟s BMW R50/2 Restoration (Abridged) LINKS 1. http://www.snafu.org/restore 2. http://www.benchmarkworks.com 3. http://www.w6rec.com/duane/bmw 4. http://www.bmbikes.co.uk 5. http://www.bmwbike.com 6. http://www.bingcarburetor.com 7. http://home.insightbb.com/~aatherton 8. http://www.beemergarage.com 9. http://bmwdean.home.att.net/ 10. http://autos.groups.yahoo.com/group/slash2 11. http://www.cycleworks.net 12. http://vintagebmw.org/forums 13. http://tonyfoale.com 14. http://agwalker.com/wheelbuilding.html 15. http://www.tyreman.co.za 16. http://www.classicmotorcycleclub.co.za 17. http://www.pomc.co.za 18. http://www.savva.org.za 19. http://vmcc.net 20. http://www.pistonring.co.za 21. http://www.startline.co.za 22. http://www.mosskays.co.za 23. http://www.ulismotorradladen.de 24. http://www.motorrad-stemler.de 25. http://www.motobins.co.uk 26. http://www.airheads.org 27. http://www.largiader.com 28. http://www.bluemooncycle.com 29. http://darryl.crafty-fox.com/motorcycles 30. http://www.motorcycle.com 31. http://www.barringtonmotorworks.com 32. http://www.maxbmw.com 33. http://www.hobbyist.nl 34. http://www.meyer-bikes.de 35. http://www.motoren-israel.de 36. http://www.boxup.eu 37. http://www.rabenbauer.com 24 December 2013 Rev 1.1 Marco Hyman‟s log of restoring R69S Craig Vechorik of Bench Mark Works Duane Ausherman‟s BMW site Phil Hawksley‟s BM Bikes Mark Huggett‟s online BMW parts (Swiss) Bing Carb site in USA Allan Atherton‟s R69 buying experience John Lacko‟s Beemer Garage Jeff Dean‟s BMW site Slash 2 forum Ed Korn‟s BMW tools & parts Vintage BMW Club Tony Foale‟s technical site Lonnie Walker‟s site for /2 wheel building TyreMan, Boksburg Classic Motorcycle Club Pretoria Old Motor Club SA Veteran & Vintage Association The Vintage Motorcycle Club (UK) Piston Ring Club Startline Online Motorcycle Spares Mosskays accessories Uli‟s online BMW spares (Germany) Motorrad Stemler bike spares (Germany) Moto-bins online BMW parts (UK) Airheads BMW website Anton Largiader‟s BMW bike website Vintage BMW bike parts Darryl Richman‟s BMW bike website Motorcycle website Barrington Motor Works, Vintage BMW Max BMW The Hobbyist online Spares (Holland) S Meyer Online BMW parts, Germany Motoren Israel BMW parts, Germany Reiner Winter Online BMW parts M Rabenbauer BMW parts, Germany 128 Allan‟s BMW R50/2 Restoration (Abridged) REFERENCES 1. 2. 3. 4. 5. 6. 7. 8. 9. 10. “How to Restore Your BMW Motorcycle Twins 1950 –1969”, Roland Slabon, Motorbooks International, 1994. “Chilton’s BMW Motorcycle Repair & Tune-Up Guide R50, R50S, R60, R69S, R50/5, R60/5, & R75/5 Models through 1972”, Chilton Book Company, 1973 “Understanding and Maintaining the BMW/2 Electrical System”, Doug Rinckes with contributions from Kees van der Heiden, 2002 “Clymer BMW 500 & 600cc Twins 1955 – 1969 Service Repair Performance”, Mike Bishop, Clymer Publications, 1978 “Building BMW/2 Wheels”, Lonnie Walker, http://agwalker.com/wheelbuilding.html Factory Manuals & Service Bulletins Website of Craig Vechorik = www.benchmarkworks.com Website of Duane Ausherman = www.w6rec.com Website of Cycleworks (ex Ed Korn) = www.cycleworks.net Yahoo Groups Slash2 Forum = http://autos.groups.yahoo.com/group/slash2 24 December 2013 Rev 1.1 129 Allan‟s BMW R50/2 Restoration (Abridged) RECORD OF EXPENDITURE DATE 11 Oct 07 14 Oct 07 14 Oct 07 14 Oct 07 21 Oct 07 23 Oct 07 29 Oct 07 2 Nov 07 4 Nov 07 5 Nov 07 6 Nov 07 10 Nov 07 18 Nov 07 2 Dec 07 5 Dec 07 8 Dec 07 12 Dec 07 12 Dec 07 12 Dec 07 19 Dec 07 20 Dec 07 20 Dec 07 02 Jan 08 03 Jan 08 06 Jan 08 08 Jan 08 10 Jan 08 10 Jan 08 10 Jan 08 13 Jan 08 15 Jan 08 30 Jan 08 5 Feb 08 6 Feb 08 DESCRIPTION BMW R50 m/cycle as scrap or spares M6 and M8 chrome dome nuts Aerosol primer and metallic silver Lacquer thinners 5 litres Heyco flat spanners 10/11, 12/13 4 x 30204 and 2 x 30203 bearings, 1x oil seal = TC 25 x 38 x 7, 1 x oil seal = TC 25 x 35 x 7 4 x M8 x 1 x 30 bolts for petrol tank bracket 4 x M12 x 1,5 Nylock nuts, 2 x M10 x 1 bright nuts, 4 x M8 x 40 s/steel bolts CD of R50/R60 Workshop Manual 2 x M8 x 75 s/steel, 2 x M8 x 50 s/steel, 2 x M8 x 40 s/steel, 2 x M8 x 1 x 30 HT, 4 x M10 x 1 nuts Autosol metal polish 1L MS primer, 1L 2K black gloss, 1L 2k hardener, 5L thinners 500mL Duram Metcote NS5 etch primer (red) and Dulux Black Limo spray paint BMW rubber parts Various new & used BMW parts Emery cloth and water paper Various oil seals Bolts & nuts 1L Black Gloss 2K, 1/2L 2K hardener, wet/dry sand paper (1500 and 2000) 30203 bearings for front swing arm Hylomar gasket compound & cork for gaskets 6V 25W/25W lamp Tank knee pads Engine enamel Black Gloss spraypaint Various rubber parts & spares Spark plug leads, 1m 6203, 6004 and 6207 bearings & crank seal Bead blasting (Red Heart Rum) Steel strip and plate 51W/34W taper roller steering head bearings & Bing carb manual 1/2L silver 2K, 1/2L clear 2K, 1/2L MS primer 2 x springs (for centre stand) 2 x Metzeler ME22 3.50 x 18 tyres 5L Shell Rotella Tx SAE40 oil SUBTOTAL: 24 December 2013 AMOUNT R7000-00 R18-00 R59-00 R60-00 R20-00 R177-00 SELLER Jimmy D****** Builder‟s Express Builder‟s Express Builder‟s Express Piston Ring Club Tvl Bearings R11-15 JKM R30-00 JKM R50-00 CMC (Bob Harpin) R34-00 Bolt & Nut (KDP) R49-00 Unnic Midas R345-00 Randburg Automotive Paints R63-90 Builders Express R375-00 R350-00 R38-65 R145-00 R34-00 R167-00 R78-00 R167-00 R18-00 R450-00 R30-00 R150-00 R8-00 R194-63 R105-00 R45-75 R404-00 CMC Jan Cornel Builders Express Invicta JKM Randburg Automotive Paints Invicta Blitz Motor Spares Randburg Motorcycles Jan Cornel Mica Hardware CMC Blitz Motor Spares Invicta Zane‟s contact Fleet Steel R Alexander (Ed Korn) R180-05 R11-40 R650-00 R108-30 Randburg Auto Paints Starco Springs Mosskays Midas R11626-83 Rev 1.1 130 Allan‟s BMW R50/2 Restoration (Abridged) RECORD OF EXPENDITURE (2) DATE 7 Feb 08 12 Feb 08 14 Feb 08 18 Feb 08 1 Mar 08 2 Mar 08 4 Mar 08 12 Mar 08 20 Mar 08 22 Mar 08 26 Mar 08 12 Apr 08 12 Apr 08 19 Apr 08 3 May 08 17 May 08 1 Jun 08 2 Jun 08 4 Jun 08 18 Jun 08 18 Jun 08 1 Jul 08 28 Jul 08 3 Aug 08 25 Aug 08 5 Sep 08 8 Sep 08 15 Sep 08 21 Sep 08 21 Sep 08 21 Sep 08 29 Sep 08 12 Oct 08 21 Oct 08 23 Oct 08 2 Nov 08 7 Nov 08 14 Nov 08 25 Nov 08 7 Dec 08 15 Dec 08 6 Jan 09 8 Jan 09 11 Jan 09 DESCRIPTION Inner tube 3.50 x 18 (King Tube) Re-upholster dual bench seat Oil seals 24x35x7, 25x38x7, Nitrile Oil seals 30 x 40 x 7, 36 x 54 x 7 Viton & Nitrile RT20G High Temp Retainer (50mL) Mudguard, silent blocs, side stand Spares from Uli‟s Spares from Uli‟s = E110 (E1 = ZAR13) Welded fins on tappet cover and cylinder head Small tin body filler S/Steel bolts & nuts 1m of M6 s/steel studding Medium emery cloth 1kg Formula 40 body filler, 1m P60 sandpaper Rear mudguard, tail lamp, luggage carrier complete Flexoid 0,4mm gasket paper (1m x 1m) Timing cover gasket 2 x Red fibre gaskets 13mm hex s/steel to fabricate nuts (500mm) Cut valve seats M16 x 1,5 and M10 X 1 bolts Bronze Bar PB1, 19mm diameter x 200mm 2 x exhaust valves and kickstart rubber h/ware RHS carburetor air pipe Rubber parts from Bill Speight incl Courier Re-chroming of some parts Parts from Uli‟s = E40.00 (E1 = R11.50) Spraypainting & pinstriping (my 2K paint) Reinforced rubber fuel hose (1m) Plug Spanner Pliers (Hapewe Germany) Plug spanner, screwdriver, Black silicon Exhaust silencers, s/steel, pair ½ L Black, ½ L Clear 2K paint Weld gearbox casing around gear lever Gear lever rubber sleeve, exhaust crush gasket Gearbox bearings (x 5) Gearbox 3203 bearing 17 x 1 circlip and 4 x 6.5 Woodruff key (g/box) Fabricated and electroplated exhaust headers Handlebar, used but electroplated M12 x 30 S/steel bolts, x 2 Hylomar (for Jan Cornel) Cork gasket material 3.2mm (for fuel petcock) 6V 3W lamp and in-line fuel filters SUBTOTAL: 24 December 2013 Rev 1.1 AMOUNT R50-00 R513-00 R15-00 R60-00 R68-00 R705-00 R1700-00 R1430-00 R150-00 R35-00 R47-10 R28-00 R7-99 R76-00 R1200-00 SELLER Mosskays Classic Auto Trimmers Bearing Man Bearing Man Chemence CMC Jan Cornel Uli‟s (R&S) Paid Euro Aerotig (Chas Hamer) Autoquip JKM Builders Warehouse Builders Warehouse Randburg Auto Paints John W****** R28-50 R5-00 R5-00 R60-00 R150-00 R16-00 R148-20 R678-00 R20-00 R51-00 R385-00 R460-00 R1600-00 R15-00 R10-00 R20-00 R36-50 R1400-00 R140-00 R50-00 R35-00 R154-00 R140-00 R4-40 R500-00 R250-00 R15-00 R142-50 R82-00 R38-00 R24351-02 Unnic Midas CMC Lazer Hydraulics Metals Centre J.B Engineering JKM Gold Circle Metals P. Beukes (Uli‟s) CMC Bill Speight African Electroplating Uli‟s Mike Lester Piston Ring Swap Piston Ring Swap Piston Ring Swap Autozone Jeff Talbot Randburg Auto Paints Chas Hamer Aerotig Jan Cornel SKF Bearing & Belting Supp JKM CMC Jan Cornel JKM Blitz Autozone Wizard Midas Randburg M/Cycles 12724.19 131 Allan‟s BMW R50/2 Restoration (Abridged) RECORD OF EXPENDITURE (3) DATE 29 Jan 09 29 Jan 09 1 Feb 09 1 Feb 09 3 Feb 09 5 Feb 09 6 Feb 09 20 Feb 09 15 Mar 09 16 Mar 09 28 Mar 09 6 Apr 09 30 Apr 09 27 Aug 09 4 Oct 09 5 Oct 09 18 Oct 09 7 Dec 09 8 Dec 09 22 Dec 09 10 Feb 10 7 Mar 10 21 May 10 19 Aug 10 8 Sep 10 14 Feb 11 25 Feb 11 2 Mar 11 4 Mar 11 7 Mar 11 10 Mar 11 14 Mar 11 27 Mar 11 15 May 11 3 Dec 11 12 Jul 12 4 Oct 12 22 Nov 12 8 Nov 13 DESCRIPTION Oil seals 25 x 35 x 7, 25 x 38 x 7 Battery B49-6 6V 3W globe and 2 x cable nipples Front brake reline and skim drum Rubber driveshaft boot Oil seal 25 x 35 x 6 Nitrile (x 2) Inner tube 3.50 x 18”, rim tape O-ring 6mm x 55mm Re-chrome 1 x wheel rim, 40 x spokes & nipples, 2 x hubcaps, 1 x aircleaner dome 70 x new spokes & nipples Bonded linings for rear brake shoes, skim drum Rim tape 3m of 10mm AF hex 303 s/steel bar Condensor Cylinder head gaskets & air filter element Chromed steel wheel rim Stainless steel M8 bolts Mirrors Spares from Uli‟s E30 @ R11.08 Re-chroming of handlebar risers, 3 x valve pushrod tubes (R50), taillight rim Credit for chroming taillight rim Hooter, 6V chrome, new Welded fin on one tappet cover 1 x Rim tape, 18” Stainless steel exhaust headers Postage on EconoParcel to Craig Patterson 10mm external circlips and E-clips Spanner, Kennedy 14mm ring/flat M10 and M14 copper washers 4mm plate for steering head spanner Oil seals, final drive 431 S/steel bar for axles Oil seal, 28 x 47 x 7, Nitrile, final drive Hex bolt M12 x 45, nut, s/steel, rear shock mtg Spares from Uli‟s (E40.40 x R9.868) Socket 1” BSW to fabricate pin spanner Licence disc holder M8x1 x 20 cap screw (clutch mounting) Renewed licence for 2012/13 Hardened washers for cyl head mount AGM 6V battery Plastic box 160x96x67 Number plate AMOUNT R24-00 R160-00 R10-00 R100-00 R75-00 R10-00 R111-00 R30-00 R1100-00 TOTAL TO DATE: R32428-00 Approx 24 December 2013 Rev 1.1 SELLER Main Reef Midas Jan Cornel Jan Cornel Jan Cornel/Hercules CMC BMG/Zane Randburg M/Cycles BMG Sheffield Electroplating R1460-00 R162-00 R16-00 R110-00 R25-00 R462-00 R300-00 R26-20 R140-00 R332-00 R302-10 Uli‟s (via R&S) CBF, Strijdom Pk Randburg M/Cycles KMG Blitz Motor Spares Northside M/Cycles Jan Cornel JKM Jan Cornel Piet Beukes (Uli‟s) African Electroplating -R80-00 R220-00 R35-00 R5-00 R1544-70 R18-15 R4-20 R13-00 R9-55 R8-50 R22-65 R100-00 R15-00 R10-40 R398.67 R60-00 R14-00 R22-38 R192-00 R8-50 R68-00 R81-00 R100-00 Melville Price Jan Cornel Aerotig(Charlie Hamer) CMC Powerflow Durban SAPO JKM ExecuPawn JKM Fleet Steel BMG Diversified Alloys BMG JKM Uli‟s Piston Ring Main Reef Midas President Bolt Cresta PO Northern Bolt Current Automation Communica 132