Electrical failure and crash into ocean, United Air Lines
Transcription
Electrical failure and crash into ocean, United Air Lines
Electrical failure and crash into ocean, United Air Lines, Inc., Boeing 72722C, N7434U, near Los Angeles, California, January 18, 1969 Micro-summary: This Boeing 727 crashed into the Pacific shortly after experiencing an electrical failure on takeoff. Event Date: 1969-01-18 at 1821 PST Investigative Body: National Transportation Safety Board (NTSB), USA Investigative Body's Web Site: http://www.ntsb.gov/ Cautions: 1. Accident reports can be and sometimes are revised. Be sure to consult the investigative agency for the latest version before basing anything significant on content (e.g., thesis, research, etc). 2. Readers are advised that each report is a glimpse of events at specific points in time. While broad themes permeate the causal events leading up to crashes, and we can learn from those, the specific regulatory and technological environments can and do change. Your company's flight operations manual is the final authority as to the safe operation of your aircraft! 3. Reports may or may not represent reality. Many many non-scientific factors go into an investigation, including the magnitude of the event, the experience of the investigator, the political climate, relationship with the regulatory authority, technological and recovery capabilities, etc. It is recommended that the reader review all reports analytically. Even a "bad" report can be a very useful launching point for learning. 4. Contact us before reproducing or redistributing a report from this anthology. Individual countries have very differing views on copyright! We can advise you on the steps to follow. Aircraft Accident Reports on DVD, Copyright © 2006 by Flight Simulation Systems, LLC All rights reserved. www.fss.aero . TOOTED AIR LIMES. I N C BOEING 727- 22C. N7434U MEAE LOS ANGELES. CALIFORNIA JANUARY 18. 1969 TABLE OF COMTEMTS ......................... .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. ................... ................... . . .. ... ... ... ... ... ... ... ... ... ... ... ... ... ... ... ... ... ... ... ... ................... ................ .................... ...................... . . . . . . .. .. ... ... ... ... ... ... ... ... ... ... ... ... ... .. .. .. .. .. .. .. .. .. .. .. .. .. .. . . . . . . . . . . . . . . . . . .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. ..................... ............... ................. ......................... . . . . .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. . . . . . . . . .. .. .. .. .. .. .. .. .. .. . . Synopsis ProbableCause Investigation History of t h e Flight I n j u r i e s t o Persons Damage t o Aircraft Other Damage Crew Information Aircraft Information Meteorological Information Aids t o Navigation Communications Aerodrome and Ground F a c i l i t i e s Flight Recorders ( a ) Flight Data Recorder (b) Cockpit Voice Recorder Wreckage Fire Survival Aspects Tests and Research Other Pertinent Information Analysis and Conclusions Analysis Conclusions ( a ) Findings (b) Probable Cause Recommendations and Corrective Measures Appendices A. Investigation and Hearing 1 Investigation Hearing 2 3 Preliminary Reports B Crew Information C t Transcript of t h e Cockpit Voice Recorder Attachment . Page 1 1 2 2 h 4 4 4 4 6 7 7 8 9 9 9 10 11 11 11 12 16 16 28 28 29 30 F i l e No. l-CCOb NATIONAL TRANSFOBTATION SAFETY BOARD DEPAETMEIW OF 'ERAMSFORTATION AIRCRAFT ACCIDEHT REPORT UHITED AIR LIMES, INC. BOECTG 727-22C, ~ 7 4 3 4 ~ HEAE LOS AMGELES, CALIFORNIA JANUARY 18, 1969 SYNOPSIS United Air Lines, Inc., Flight 266, a Boeing 727-22C, B7434U, crashed i n t o Santa Monica Bay, approximately 11.3 miles west of t h e Los Angeles International Airport, at 1821 P.s.t. on January 18, 1969. The a i r c r a f t was destroyed and t h e s i x crewmembers and 32 passengers on board were all f a t a l l y injured. Flight 266 departed from Los Angeles Airport at 1817 P.s.t., and 2 minutes l a t e r reported t o Departure Control t h a t they had experienced a f i r e warning on t h e No. 1 engine and wished t o return. This was t h e last communication with t h e f l i g h t . The secondary o r transponder t a r g e t disappeared from t h e radarscope immediately following t h e above transmission. Thereafter, movement of t h e primary t a r g e t indicated t h e a i r c r a f t continued t o track a s t r a i g h t course on t h e last assigned heading of 270 f o r approximately a minute and a half, a f t e r which t h e a i r c r a f t commenced, a l e f t turn. The t a r g e t then disappeared from t h e radarscope. The Los Angeles weather report i n e f f e c t at t h e time of t h e accident indicated TOO f e e t scattered, measured c e i l i n g 1,000 f e e t broken, 2,000 f e e t overcast, v i s i b i l i t y 3 miles i n l i g h t r a i n and fog. The Board determines t h a t t h e probable cause of t h i s accident was l o s s of a t t i t u d e orientation during a night, instrument departure i n which all a t t i t u d e instruments were disabled by l o s s of e l e c t r i c a l power. The Board has been unable t o determine ( a ) why a l l generator power was l o s t o r (b) why t h e standby e l e c t r i c a l power system e i t h e r was not a c t i v a t e d o r f a i l e d t o function. Safety Board recommendations designed t o prevent t h e occurrence of similar accidents a r e s e t f o r t h i n d e t a i l i n section 3 of t h i s report. These recommendations prjmarily involve measures directed toward assuring ( a ) t h a t t h e standby e l e c t r i c a l power system w i l l be e f f e c t i v e l y activated, e i t h e r automatically o r by t h e crew, i n t h e event of t h e l o s s of all generators, and ( b ) t h a t t h e crew w i l l have available a t t i t u d e indicator instruments following disruption of e l e c t r i c a l power. 1. INVESTIGATION 1.1 History of t h e Flight United Air Lines, Inc. ( W ) , Flight 266 was a regularly scheduled passenger and cargo f l i g h t from Los Angeles, California, t o Milwaukee, Wisconsin, with an en route stop a t Denver, Colorado. N7434U, a Boeing 727-22C, which was u t i l i z e d f o r t h i s f l i g h t on January 18, 1969, a r r i v e d i n Los Angeles from Denver a t about 1530 I/ on t h a t date. - While B7434U was on t h e ground at Los Angeles, a routine en route inspection was performed by a UAL mechanic who found t h e a i r c r a f t t o be serviceable and noticed nothing unusual. This check consists b a s i c a l l y of an i n t e r i o r and e x t e r i o r visual inspection of t h e a i r c r a f t f o r any condition t h a t might require corrective action. During t h e period t h e airc r a f t was on t h e ground, r a i n was f a l l i n g intermittently. However, t h e a i r c r a f t was equipped with a protective canvas shroud designed t o prevent water from dripping i n t o t h e e l e c t r i c a l bay area. As indicated i n t h e logbookJ M7434~had been operating since January 15, 1969, with t h e No. 3 generator inoperative. The second o f f i c e r on board t h e a i r c r a f t during t h e f l i g h t M e d i a t e l y preceding Flight 266 on J a n v 18, 1969, s t a t e d t h a t "inoperative" t a p e had been placed over t h e No. 3 generator CSD (constant speed drive) low-pressure l i g h t , t h e No. 3 generator breaker c i r c u i t open l i g h t , and t h e Do. 3 generator f i e l d relay open l i g h t . He a l s o believed t h a t t a p e was placed adjacent t o t h e No. 3 generator position of t h e AC ( a l t e r n a t i n g current) meters s e l e c t o r switch. The UAL dispatcher, who was responsible f o r dispatching Flight 266, was informed approximately 30 o r 40 minutes before departure that t h e No. 3 genera t o r was inoperative. After r e f e r r a l t o t h e Minimum Equipnent L i s t , which, i n e f f e c t , s t a t e s t h a t t h e a i r c r a f t i s airworthy with only two generators operable provided c e r t a i n procedures a r e followed and e l e c t r i c a l loads a r e monitored during f l i g h t , he approved t h e dispatch. Conversation recorded on t h e cockpit voice recorder p r i o r t o departure indicates t h a t t h e crew was aware that t h e No. 3 generator was inoperative. W procedures prescribe t h a t when only two generators a r e operable, t h e galley power switch and one of t h e two air conditioning packs should be turned off before takeoff. These switches can be turned t o t h e "on" position during climbout when t h e f l a p s have been raised. F l i g h t 266 was scheduled t o depart t h e gate at 1755, but was delayed u n t i l 1807 because of t h e inclement weather and loading problems. The f l i g h t commenced i t s takeoff roll on Runway 24 at approximately 1817. The l o c a l controller i n t h e tower who observed t h e a i r c r a f t during i t s takeoff run, and u n t i l it was 400 o r 500 f e e t i n t h e a i r and about 8,000 f e e t down t h e runway, noticed nothing abnormal. -I/ A l l times herein a r e 'Pacific standard, based on t h e 24-hour clock. A t 1818: 13, F l i g h t 266 contacted Departure Control and w a s i n s t r u c t e d t u r n r i g h t heading two seven zero r e p o r t leaving t h r e e thousand t o 'I. f e e t . " 21 The cockpit voice recorder i n d i c a t e s t h a t , at 1818:30, t h e sound of an engine f i r e warning b e l l was heard i n t h e cockpit. 3/ A t 1819:05, we've had a f i r e warning F l i g h t 266 reported t o Departure Control t h a t on number one engine we shut down we'd l i k e t o come back." This was t h e last communication with F l i g h t 266. Departure Control attempted repeatedly t o contact t h e f l i g h t during t h e time period following t h i s transmission but w a s unsuccessful. .. ". . . The departure c o n t r o l l e r who was handling F l i g h t 266 s t a t e d t h a t t h e Approximately 5 seconds f l i g h t responded t o h i s heading i n s t r u c t i o n of 270'. a f t e r t h e transmission from t h e f l i g h t r e p o r t i n g t h e f i r e warning, t h e seconda r y o r transponder t a r g e t of t h e a i r c r a f t disappeared from t h e radarscope. The movement of t h e primary t a r g e t i n d i c a t e d t h e a i r c r a f t continued t o t r a c k a r e l a t i v e l y s t r a i g h t course on 270° A t 1820:30, when t h e a i r c r a f t w a s about 1 0 miles west of t h e shoreline, t h e . d e p a r t u r e c o n t r o l l e r i n s t r u c t e d t h e f l i g h t t o t u r n r i g h t t o a heading of 060° but again received no reply. A t t h i s point, t h e primary t a r g e t movement i n d i c a t e d t h e a i r c r a f t s t a r t e d a l e f t t u r n , The a f t e r which t h e t a r g e t disappeared from t h e scope within two sweeps.' c o n t r o l l e r a l s o s t a t e d t h a t t h e speed of t a r g e t movement during t h e s e last few sweeps increased g r e a t l y . h/ Appropriate emergency procedures were i n i t i a t e d following t h e disappearance of t h e t a r g e t from t h e radarscope. It w a s l a t e r determined t h a t t h e airc r a f t crashed at approximately 1821 a t a point 11.3 miles west o f t h e a i r p o r t . -51 Two ground witnesses observed an a i r c r a f t t a k i n g o f f from Runway 24 at a time corresponding t o t h e departure of F l i g h t 266. One of t h e s e witnesses, who i d e n t i f i e d t h e a i r c r a f t a s a B-727 based on t h e engine arrangement, noticed nothing unusual about t h e a i r c r a f t as it flew d i r e c t l y over h i s c a r . The o t h e r witness' a t t e n t i o n was a t t r a c t e d by many sparks, reddish i n color, coming from t h e r i g h t s i d e and r e a r engine of t h e a i r c r a f t . She observed t h e a i r c r a f t when it was about 1,000 f e e t high and climbing gradually a t what appeared t o be normal speed. Another ground witness, who w a s l o c a t e d on a h i l l above Faxadise Cove (northwest of t h e impact p o i n t ) , observed an a i r c r a f t over t h e water, t u r n ' "21 - The communications between Los Angeles Departure Control and F l i g h t 266 a r e s e t f o r t h i n f u l l i n t h e Communications s e c t i o n . -31 For a t r a n s c r i p t i o n of t h e recorded crew conversation during t h i s period, see Appendix C. -41 -51 The r a d a r antenna r o t a t e s a t a speed of 1 5 revolutions p e r minute. The approximate f l i g h t p a t h of F l i g h t 266, based on t h e departure c o n t r o l l e r ' s memory c h a r t , i s attached t o t h i s r e p o r t . t o i t s l e f t , and head e a s t back toward t h e a i r p o r t . As t h e plane "descended i n t o a t h i c k fog bank, he heard an explosion and saw a f l a s h of l i g h t . A f o u r t h ground witness w a s d r i v i n g along Malibu Beach i n an e a s t e r l y d i r e c t i o n when h i s son exclaimed "Look, Dad, f i r e . " The man stopped t h e c a r , got out and saw a n a i r c r a f t "on f i r e " which seemed t o be coming from t h e f r o n t of t h e plane. The a i r c r a f t was descending, heading toward t h e a i r p o r t and t h e n it plunged s t r a i g h t down i n t o t h e ocean. This witness a l s o heard s e v e r a l "firecracker" o r "backfire" sounds while t h e plane w a s s t i l l i n t h e a i r . 1.2 I n j u r i e s t o Persons Injuries Crew - Passengers Others Fatal Nonfatal None 1.3 Damage t o A i r c r a f t The a i r c r a f t was destroyed by impact with t h e water. 1.4 Other Damage None. 1.5 Crew Information The crew was properly c e r t i f i c a t e d and q u a l i f i e d t o conduct t h e f l i g h t . The captain had r e c e n t l y completed DC-8 t r a i n i n g and F l i g h t 266 w a s h i s f i r s t f l i g h t i n a E 7 2 7 since December 2, 1968. The second o f f i c e r completed E 7 2 7 t r a n s i t i o n t r a i n i n g on December 19, 1968, and completed h i s l i n e check on January 2, 1969. He had a t o t a l of 40 hours as second o f f i c e r i n t h e E-727, of which at least 18 hours were i n t h e QC model. The o f f i c i a l medical f i l e s o f t h e f l i g h t crewmembers and interviews with r e l a t i v e s revealed no conditions which might have adversely a f f e c t e d t h e crewmembers' f i t n e s s f o r duty. For d e t a i l e d crew information, see Appendix B. 1.6 A i r c r a f t Information 6 ~ 7 4 3 w4 a~s a Boeing Model 727-22C (Qc), -I S/N 19891, with a d a t e of manufacture of September 1, 1968. A standard airworthiness c e r t i f i c a t e w a s issued on September 19, 1968, and t h e a i r c r a f t w a s delivered t o United Air Lines on September 20, 1968. The a i r c r a f t had accumulated 1036: 47 hours operating time s i n c e new, including 217:09 hours s i n c e t h e last maintenance check and 90:01 hours s i n c e t h e last s e r v i c e check. -61 Quick change, cargolpassenger. The a i r c r a f t w a s equipped with t h r e e Pratt & Whitney JT8D-7 engines. Engines No. 2 (SIN 655074) and No. 3 (SIN 655085) had been on t h e a i r c r a f t since new and had accumulated 1037:00 hours. Engine No. 1 (SIN. 654366) was a replacement engine with a t o t a l of 4,505 hours, including 1,021 hours s i n c e heavy maintenance. The a c t u a l gross weight of M7434~at t h e time of t a k e o f f was computed t o be 148,800 pounds, as compared w i t h t h e maximum allowable gross takeoff weight of 156,100 pounds. The c e n t e r of g r a v i t y of t h e a i r c r a f t was calcul a t e d t o have been w i t h i n t h e prescribed limits both at t h e time of t a k e o f f and t h e time of t h e crash. A l l of t h e records exmined during t h e course of t h e i n v e s t i g a t i o n disclosed t h a t t h e a i r c r a f t had been m a i n t a i n e d ' i n accordance with a p p l i c a b l e company and Federal Aviation Administration (FAA) d i r e c t i v e s and procedures. These records were examined with p a r t i c u l a r reference t o t h e f i r e warning and e l e c t r i c a l systems. The records p e r t a i n i n g t o N743kU contained no r e p o r t s of p r i o r f i r e warnings on t h e No. 1 engine o r of any condition t o which t h e f i r e warning experienced on F l i g h t 266 might have been r e l a t e d . With r e s p e c t t o t h e United A i r Lines B-727 f l e e t i n general, a t o t a l o f 73 i n - f l i g h t shutdowns due t o firewarnings was experienced during t h e period from January 1966 through March 1969. Of t h e s e , only 1 0 were " f a l s e " warnings i .e., warnings f o r which t h e r e w a s no i d e n t i f i a b l e cause such as overheat o r f i r e . Most of t h e engine shutdowns i n which no a c t u a l f i r e occurred were due t o overheat r e s u l t i n g from hot, high-pressure engine bleed a i r l e a k i n g i n t o t h e f i r e warning sensor a r e a through f a i l e d o r cracked ducting. -- Research i n t o t h e records concerning t h e f i r e warning system a l s o d i s closed t h a t Boeing Service B u l l e t i n No. 26-15 w a s i s s u e d on May 7, 1968, t o reduce f a l s e f i r e o r overheat i n d i c a t i o n s on a i r p l a n e s using t h e Lindberg engine f i r e d e t e c t o r system" J/ The b u l l e t i n provided f o r options replacement of a sensor element designed t o a c t u a t e warnings at 325' 25' F., with a sensor designed t o a c t u a t e warnings at 375' 25' F.. The system i n s t a l l e d on t h e No. 1 engine on N7434U incorporated t h e 325" 2 5 3'. sensor. . .. / / / With respect t o items of i n t e r e s t i n t h e h i s t o r y of t h e e l e c t r i c a l system on H7434U, t h e No. '3 generator c o n t r o l panel was removed on January 13, 1969, and replaced with panel S/N 163. The l a t t e r panel had been removed frm e i g h t d i f f e r e n t a i r c r a f t f o r varying reasons during t h e period from May 2, 1967, u n t i l December 31, 1968. 8/ Three hours l a t e r , on t h i s same date, t h e crew - -7/ This b u l l e t i n w a s i s s u e d i n connection with t h e B-727-200 s e r i e s a i r c r a f t , which had an engine n a c e l l e temperature t h a t r a n s l i g h t l y higher t h a n e a r l i e r versions. -81 Search o f t h e records a l s o disclosed t h a t Westinghouse Service B u l l e t i n 66-103 (September 1966), which recommended replacement of a s i l i c o n e c o n t r o l l e d r e c t i f i e r i n o r d e r t o prevent nuisance t r i p p i n g o f t h e d i f f e r e n t i a l p r o t e c t i o n c i r c u i t r y , had not been accomplished on panel SIN163. which brought t h e a i r c r a f t i n t o OtHa.re F i e l d reported: "No. 3 generator underexcitation l i g h t on b e f o r e generator connected t o bus. Reset f a u l t but generator f i e l d a f t e r 2 t r i e s s t i l l would not s t a y closed with no load on generator. Disconnected CSD." The c o r r e c t i v e a c t i o n was t o replace t h e No. 3 generator. 91 The generating system apparently passed a l l t h e ground t e s t i n g necessary t o put t h e No. 3 system back i n service. However, 3-112 f l i g h t - h o u r s l a t e r , a crew disconnected t h e newly i n s t a l l e d generator because t h e f i e l d r e l a y would not s t a y closed. The No. 3 generator was t h e n rendered inoperative by ground maintenance personnel and c a r r i e d a s a deferred item i n accordance with t h e Minimum Equipment L i s t . The No. 3 generator was s t i l l being c a r r i e d a s a deferred item 3 days and 42 f l i g h t - h o u r s l a t e r at t h e time o f t h e a c c i d e n t . During t h i s period, t h e a i r c r a f t operated through a t o t a l of 28 s t a t i o n s , 23 of which possessed l i n e maintenance c a p a b i l i t y . The item was not r e p a i r e d during t h i s period because o f t h e exigencies of a v a i l a b l e a i r c r a f t and f l i g h t scheduling. 1.7 Meteorological Information A n extensive a r e a of r a i n , fog, and low cloudiness prevailed along much of t h e C a l i f o r n i a c o a s t l i n e and i n t o c e n t r a l s e c t i o n s of t h e s t a t e i n advance of a f r o n t a l system approaching from t h e P a c i f i c Ocean. The 1900 surface weather c h a r t showed, i n p a r t , a cold f r o n t extending southwestward from near San Francisco i n t o t h e P a c i f i c and a warm f r o n t extending from near San Francisco southwestward along t h e P a c i f i c Coast near Monterey, Santa Maria, and San Nicolas I s l a n d . The o f f i c i a l surface weather observations taken at Los Angeles a t times most immediate t o t h e accident were a s follows: Record s p e c i a l , 700 f e e t s c a t t e r e d , measured 1,000 broken, 2,000 overcast, v i s i b i l i t y 3 miles, l i g h t r a i n , fog, temperature 55' F. dew point 50' F., wind 160° 5 knots, a l t i m e t e r s e t t i n g 29.96 inches. 101 , 1827 - - Special, 800 s c a t t e r e d , measured 2,500 overcast, 4 miles, l i g h t r a i n , fog, temperature 54' F., dew point 49' F., wind 6 knots, a l t i m e t e r s e t t i n g 29.96 inches. la0, The d e p r t u r e c o n t r o l l e r who w a s handling F l i g h t 266 reported t h a t t h e r e were two l a r g e i n t e n s e weather r e t u r n s on t h e radarscope, one of which w a s due -91 The generator which was removed from t h e a i r c r a f t was l a t e r examined i n t h e shop and no discrepancies were found. A t t h e time of departure of F l i g h t 266, t h e 1755 weather observation was being continuously broadcast i n t h e Los Angeles a r e a on frequency 118.6 MHz as p a r t o f t h e Automatic Terminal Information Service (ATIS). west of t h e a i r p o r t and moving eastbound. When t h e primary t a r g e t of t h e f l i g h t disappeared, it w a s j u s t approaching t h e northern edge of t h i s weather return.. The c o n t r o l l e r a l s o r e l a t e d t h a t p i l o t s were generally reporting r a i n showers west of t h e a i r p o r t i n all quadrants. Such reports were cons i s t e n t with ground witness observations. The p i l o t s of Air West Flight 312, which departed from Runway 24 1minute prior t o Flight 266, s t a t e d t h a t t h e i r a i r c r a f t entered t h e overcast at 800 f e e t . After crossing t h e shoreline while climbing through 1,000 t o 1,200 f e e t , t h e f l i g h t encountered complete darkness and t h e r e a f t e r w a s without any reference t o an outside horizon. The f i r s t o f f i c e r on UAL F l i g h t 111, which departed from t h e same runway h minutes a f t e r Flight 266, reported entering an overcast 112 mile o f f t h e coast at an a l t i t u d e of 1,000 t o 1,500 feet . No weather b r i e f i n g was furnished t o t h e crew of F l i g h t 266 by personnel of t h e Weather Bureau o r Flight Service Station, Los Angeles, nor w a s t h e r e a known formal weather b r i e f i n g of t h e crew by company personnel. However, t h e company maintains a self-help weather b r i e f i n g display a t t h e i r Los Angeles f a c i l i t y , which under most circumstances i s t h e method used by crews t o familiarize themselves with current and forecast conditions. 1.8 Aids t o Navigation Ground c e r t i f i c a t i o n checks, which began about 10 minutes a f t e r Flight 266 disappeared from t h e radarscope, indicated t h a t t h e Los Angeles radar, seconda r y radar gear, and radar display equipment were operating within established tolerances. Ground checks a l s o disclosed t h a t t h e back course l o c a l i z e r ( f o r Runway 2 5 ~ )of t h e Instrument Landing System ( f o r Runway 7 ~ was ) operating satisfactorily. A f l i g h t check conducted on January 18, 1969, by t h e FAA indicated t h a t t h e primary and secondary radar were operating s a t i s f a c t o r i l y . A second f l i g h t check w a s conducted on January 21, 1969, t o determine minimum a l t i t u d e coverage between 7 and 15 miles west of Los Angeles Airport. The secondary radar was good a t 500 f e e t i n t h e area, while t h e primary radar w a s good at 700 f e e t and intermittent below 700 f e e t . 1.9 Communications The communications between Flight 266 (UA 266) and Los Angeles Departure Control (DC),as recorded i n t h e Los Angeles Air T r a f f i c Control Tower, were as follows: TIME - SOURCE 1818:13 Vk 266 United two s i x s i x on departure DC United two sixty-six Los Angeles departure control radar contact t u r n r i g h t heading two seven zero r e p o r t leaving t h r e e thousand COCTrEBT Two seven zero Wilco Ah departure United two s i x s i x United two s i x t y s i x go ahead United two s i x t y s i x go ahead We've had a f i r e warning on number one engine we shut down we'd l i k e t o come back United two s i x t y s i x Roger what i s your present altitude United two s i x t y s i x maintain three thousand and say your a l t i t u d e United two s i x t y s i x say your a l t i t u d e maintain t h r e e thousand t h r e e thousand f i v e hundred what's your a l t i t u d e now United two s i x t y s i x i f you hear do not climb above f i v e thousand t r a f f i c twelve o'clock t h r e e miles west-bound l e v e l at f i v e thousand a F a i r c h i l d en route t o Ventura. United two s i x t y s i x ah t u r n r i g h t heading zero s i x zero United two s i x t y s i x i f you hear t u r n r i g h t heading two s i x uh zero s i x zero United two s i x t y s i x i f you hear us squawk two zero zero zero o r zero four zero zero A t 1822:05, United Air Lines F l i g h t 111, a l s o departing from Runway 24, c a l l e d Departure Control and was vectored c l e a r of t r a f f i c we l o s t out west." A t 1822:25, departures were stopped and, at l823:50, Departure Control was informed by United F l i g h t 111 t h a t Flight 266 had not been talking with t h e company. ". . . The f l i g h t check of t h e Los Angeles radar conducted on January 18, 1969, a l s o demonstrated t h a t radio communications on 125.2 MHz, t h e frequency on which Flight 266 was conmrunicating with Departure Control, were s a t i s f a c t o r y i n t h e a r e a west of t h e a i r p o r t . 1.10 Aerodrome and Ground F a c i l i t i e s Not involved i n t h i s accident. 1.11 Flight Recorders (a) F l i g h t Data Recorder The a i r c r a f t w a s equipped with a Fairchild I n d u s t r i a l Products 1423, which was i n s t a l l e d i n t h e r i g h t f l i g h t data recorder, Model 5424, ventral stairway a r e a aft of t h e r e a r pressure bulkhead. The f l i g h t recorder was r e c o v e r e d , s t i l l encased i n i t s housing which had collapsed around t h e recorder. The f l i g h t record medium was readable and showed t h a t all parase t e r s were functioning. SIN A data graph was p l o t t e d t o r e f l e c t two separate time periods. The f i r s t covers t h e period commencing with l i f t - o f f and ending l m i n u t e 34 seconds l a t e r when t h e t r a c e s ceased t h e i r normal appearance and became widely divergent, indicating an e l e c t r i c a l power interruption. This power interruption occurred 5 seconds a f t e r t h e completion of a h-second VHP The transmission from Flight 266 t o LQS Angeles I k p r t u r e Control. second time period commenced at an indeteminate l a t e r time and l a s t e d 15 seconds, during which divergent t r a c e s were recorded f o r all prameters. Examination of t h e data graph reveals that following l i f t - o f f , t h e airc r a f t climbed approximately 2,300 f e e t i n 1 minute 30 seconds at a steady r a t e of climb of about 1,500 f e e t per minute. I n t h e 4 seconds p r i o r t o t h e power interruption, t h e a i r c r a f t descended 50 f e e t . The indicated airspeed t r a c e shows t h a t t h e speed increased s t e a d i l y from 142 knots at l i f t - o f f t o 212 knots l m i n u t e l a t e r . A t t h i s point, t h e airspeed s t a r t e d t o decrease, reaching 203 knots 13 seconds l a t e r , at which point it s t a r t e d t o increase again, reaching 217 knots when power interruption occurred 21 seconds l a t e r . The magnetic heading t r a c e remained on 250' u n t i l 30 seconds a f t e r l i f t - o f f . It then s h i f t e d gradually during t h e next 30 seconds t o 270° where it remained u n t i l power was interrupted 34 seconds l a t e r . The v e r t i c a l acceleration t r a c e recorded e r r a t i c excursions i n t h e period following liftoff which tended t o f l a t t e n out i n t h e f i n a l 1 5 seconds p r i o r t o power interruption. During t h e second period plotted on t h e data graph, when power was restored, t h e i n i t i a l t r a c e indications on all parameters were p a r t i c u l a r l y e r r a t i c . When t h e power w a s again l o s t 1 5 seconds a f t e r being restored, t h e following readings were being reflected: a l t i t u d e 630 f e e t , indicated airspeed 326 knots, heading 2 a 0 , and v e r t i c a l acceleration / 1.75 G t s . (b) Cockpit Voice Recorder The a i r c r a f t was equipped with a United Control cockpit voice re1670, located j u s t forward of t h e aft pressure corder (CVR), Model V-557, SIN The f o i l record contains two a u x i l i a r y binary t r a c e s which r e f l e c t excursions when transmissions a r e made on t h e No. 1 and No. 2 VHP communications system. bulkhead, on t h e right-hand side of t h e a i r c r a f t . The CVE was recoxered almost 6 weeks a f t e r t h e accident. Despite having been immersed i n 1,000 f e e t of sea water during t h i s period, t h e CTK yielded a good tape. covering t h e A t r a n s c r i p t i o n from a recording of t h e tape w a s period following receipt by t h e f l i g h t of takeoff clearance a t 1816: 58. This t r a n s c r i p t i s set f o r t h i n Appendix C. With respect t o t h e recording p r i o r t o t h i s time, all four channels of t h e o r i g i n a l tape were monitored t o determine whether there was any conversation r e l a t i v e t o t h e s t a t u s of t h e a i r c r a f t ' s e l e c t r i c a l generating system, a s well a s other information which might be pertinent t o t h e accident. The only crew conversation noted i n t h i s regard was a reference t o t h e inoperative s t a t u s of t h e No. 3 generator, of which t h e captain was made aware. At The CVR indicates t h a t t h e f i r e warning b e l l sounded a t 1.818:30. 1819:13.5, 5 seconds a f t e r completion of t h e transmission from Flight 266 regarding t h e f i r e warning, CVB operation ceased. A t a l a t e r indeterminate time, t h e CVR resumed operation f o r a period of 9 seconds. When t h e recording terminated a second time, sounds normally associated with impact were not detectable. 1.12 Wreckage The a i r c r a f t crashed i n t o t h e Pacific Ocean a t l a t i t u d e 33' 56' 56" N., and longitude 118' 39' 30" W., o r approximately 11.3 miles from t h e Los Angeles VOR on t h e 260' r a d i a l . The ocean depth at t h i s ~ i n i ts approximately 950 f e e t . The general o r i e n t a t i o n of t h e wreckage path w a s east-west, covering an approximate area 600 f e e t long and kOO f e e t wide. The l a r g e s t sections recovered, including t h e engines, were d i s t r i b u t e d along a r e l a t i v e l y s t r a i g h t l i n e bearing 262O true. Approximately 50 t o 60 percent of t h e bulk of t h e a i r c r a f t was recovered. Components from all major sections were i d e n t i f i e d i n t h e wreckage. The airc r a f t w a s destroyed by t h e impact, with only small fragments remaining from a l l sections. The fragmentation and d i s t o r t i o n were most complete toward t h e nose of t h e a i r c r a f t and t h e right-hand side, and l e s s material from those areas was identified. Conversely, pieces from t h e left-hand, side and aft end were greater i n number, l a r g e r i n size, and l e s s mangled. Evidence i n t h e wreckage indicated t h a t t h e landing gear w a s i n t h e r e t r a c t e d position and t h e wing f l a p s were i n t h e 2 extended position. The No. 2 leading edge slat, t h e only slat section positively identified, was extended at t h e t i n e of impact. !The condition of t h e s m a l l portion of t h e o v e r a l l electrLca1 system which was recovered was not considered t o be pertinent t o t h e accident. None of t h e instruments f r o m t h e f l i g h t panel o r t h e engineer's panel w a s recovered. All t h r e e engines were recovered within a 100-foot c i r c l e i n t h e main wreckage area. The No. 1 engine exhibited only minimal r o t a t i o n a l damage, thus indicating t h a t it was not r o t a t i n g a t impact, which i s consistent with t h e reported crew a c t i o n of shutting down t h e No. 1 engine. There were no engine case penetrations, nor was t h e r e any evidence of overheat conditions present on engine i n t e r i o r o r e x t e r i o r areas. There likewise was no evidence of gross bleed air duct leakage o r rupture. Both No. 2 and No. 3 engines had sustained massive r o t a t i o n a l damage and twisting of low t u r b i n e shafts, indicating high-speed r o t a t i o n at impact. All t h r e e t h r u s t reverser assemblies were found i n t h e forward t h r u s t position. Also recovered were two damaged sensor responders which had been mounted on engines No. 1 and No. 2 and. which constitutedmajor portions of t h e engine f i r e detector systems. These components were subjected t o extensive functional t e s t i n g and were found t o be operating within design specification limits. - 1.13 F i r e One ground witness reported seeing an a i r c r a f t on f i r e plunge i n t o t h e ocean, another saw a f l a s h of l i g h t a s an a i r c r a f t descended i n t o a fog bank, while a t h i r d saw sparks coining from a departing a i r c r a f t . However, t h e r e was no evidence of f i r e on any part of t h e recovered wreckage, including t h e No. 1 engine and 'adjacent structure. 1.14 Survival Aspects The complete destruction and extreme degree of fragmentation of t h e a i r c r a f t , p a r t i c u l a r l y t h e occupiable area, a r e indicative of impact forces far exceeding human tolerance. A p a r t from one severely mutilated body, only body fragments were recovered and only two i d e n t i f i c a t i o n s (both of which were passengers) could be .made. 1.15 Tests and Research An extensive s e r i e s of ground and f l i g h t t e s t s was conducted subsequent t o t h e accident i n an attempt t o shed some l i g h t on t h e e l e c t r i c a l and associated problems experienced by Flight 266. These t e s t s generally showed t h a t during one and two generator operations, t h e a i r c r a f t e l e c t r i c a l system could more than adequately carry t h e design load, provided prescribed procedures were followed. Tests a l s o showed t h a t e l e c t r i c a l outages have no s i g n i f i c a n t adverse e f f e c t on t h e f l i g h t control system. Among t h e more relevant information developed by t h e t e s t s was t h e f a c t t h a t during c e r t a i n extreme overload conditions, s u f f i c i e n t induced e l e c t r i c a l interference may be present on some B-727 a i r c r a f t t o i n h i b i t proper operation of t h e No. 2 time delay c i r c u i t of t h e protection panel. The expected action of t h i s panel during such an overload would be t o t r i p t h e bus t i e breaker, thereby i s o l a t i n g t h e generator and load bus from t h e remainder of t h e e l e c t r i c a l system and clearing t h e overload. However, i f t h e No. 2 time delay c i r c u i t i s disabled by t h e induced interference, t h e No. 1time delay c i r c u i t w i l l continue t o sense t h e overload and, a f t e r 5 t o 9 seconds, w i l l t r i p t h e generator control r e l a y and t h e generator c i r c u i t breaker, thus removing t h e generator from t h e system. Flight t e s t s indicated t h a t , p a r t i c u l a r l y with t h e b a t t e r y switch o f f y t h e generator f i e l d relay would t r i p p r i o r t o t h e bus t i e breaker i n approximately half t h e time under overload conditions. It was a l s o attempted, during t h e t e s t s , t o simulate t h e voltage cond i t i o n r e f l e c t e d on t h e CVR at t h e point when power w a s restored f o r 9 seconds. These t e s t s indicated a low voltage condition of 50 v o l t s a t t h a t time. This power l e v e l was simulated by s t a r t i n g one generator with loading f o r two generators applied. 1.16 Other Pertinent Information ( a ) UAL Einergency o r Abnormal Frocedures Pertinent UAL procedures i n e f f e c t a t t h e time of t h e accident were a s foUows: Engine F i r e If f i r e warning l i g h t illuminates s t e a d i l y and b e l l rings: Phase I .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. .. ............ .............. Additional UAL Items: Engine Fuel Shutoff Valve Switch . . . . . . . ........... ThrustLever Start Lever Essential Bower Selector Engine F i r e Switch Fuel Boost Pump Switches Idle Cut-Off On Operating Generator Pull Close A s Required Blase 11 F i r e Warning l i g h t ON: ........... I f f i r e warning l i g h t remains ON a f t e r 30 seconds: ........... Bottle Transfer Switch .......... Bottle Discharge Switch Bottle Discharge Switch 12/ - Push Transfer Push Engine f i r e and l o s s of all generators a r e emergency procedures, while one generator and two generator operations a r e abnormal procedures. With respect t o emergency proceduresy Phases I and I1 a r e minimum immediate a c t i o n i t e m s , w i t h Phase I being completed before Phase 11. Phase I11 i s accomplished as soon as time permits. Blase I11 Land i f f i r e p e r s i s t s Two Generator Operation 1. Generator Breaker Switches Operative Generators Inoperative Generator ........................ ........ Close Trip 2. Bus Tie Breaker Switches (3) 3. If generators cannot be paralleled, operate generators i s o l a t e d . 4. I f generators cannot be paralleled and inoperative generator i s #1 o r #2: #3 Generator Bus Tie Breaker Switch . . . . .. Inoperative Generator Bus Tie Breaker Switch Remaining Bus Tie Breaker Switch 5. 6. Close, observing manual p a r a l l e l i n g procedure Close Close Trip ...... During takeoff, approach, and landing: Galley Fewer Switch . . . . . . . . . . . . A/C Pack Switches . . . . . . . . . . . . . WOffm u m of one On E l e c t r i c a l Loads . . . . . . . . . . . . . . . Monitor Notes: a. Other loads not required f o r t h e p a r t i c u l a r operating condition should be turned o f f t o l i m i t t h e t o t a l load t o 57 KVA (54 KW). b. Both A/C packs may be operated during Cruise F l i g h t i f necessary, however, one must be turned OET p r i o r t o extending Wing Flaps f o r APPROACH and W I N G . Cargo heat valves should be closed when only one A/C pack i s operating. One Generator Operation 1. Generator Breaker Switches: 3. 4. . . .. .. .. .. .. .. .. .. .. .. Bus Tie Breaker Switches (3) . . . . . . . . . ............. Galley Fewer Switch A/C Pack Switches .............. 5. E l e c t r i c a l Loads Operative Generator Inoperative Generators 2. ............... Close Trip Close Off Both OET, p r i o r t o extending f l a p s Monitor Loss of All Generators Phase I and I1 Any Generator F i e l d Relay Note: ............ Close To permit closing generator f i e l d relay when a d i f f e r e n t i a l f a u l t i s indicated, PULL and RESET t h e associated generator control c i r c u i t breaker o r place b a t t e r y switch OFF then ON. Essential Power Selector ............ To Operating Generator Repeat i f necessary u n t i l e s s e n t i a l power f a i l u r e warning l i g h t remains o f f . Phase I11 Restore system t o normal i f possible. Apart from t h e t h r e e generators, t h e HAL version of t h e B-727 a i r c r a f t a l s o has a standby e l e c t r i c a l power system which can be a c t i v a t e d by pos i t i o n i n g t h e Essential Power Selector Switch t o Standby and turning t h e Battery Switch ON. 3-31 This w i l l provide power f o r t h e captain's gyro horizon, captain's compass, No. 1 VHP receiver, No. 1 VHP transmitter, No. 1 Vm, No. 1 glide slope, radio altimeter, and t h e f i r s t o f f i c e r ' s RMI (remote magnetic i n d i c a t o r ) card. Although t h e action of switching t o t h e standby system i s not included i n t h e "Loss of all Generators" emergency procedure s e t f o r t h above, t h e UAL second o f f i c e r on Flight 266 was instructed during t r a i n i n g t o attempt t o close t h e generator f i e l d r e l a y ( s ) only once before going t o standby. (b) Other Incidents Involving Loss of a l l Generators During t h e months of June and J u l y 1969, t h e r e were t h r e e occasions on which HAL B-727 a i r c r a f t experienced l o s s of a l l t h r e e genera t o r s . The f i r s t of these incidents occurred on June 10, 1969, near San Francisco and involved a i r c r a f t N7411U. When t h e f l i g h t was appreaching t h e San Francisco LQM i n V i s u a l F l i g h t Rules (VFR) conditions, t h e second o f f i c e r noted t h a t h i s background f l i g h t l i g h t s were fluctuating. He t r i p p e d all t h r e e bus t i e breakers t o i s o l a t e t h e generators. He then selected No. 3 on t h e e s s e n t i a l power switch and checked t h e phase l i g h t s . The l e f t l i g h t was steady, t h e r i g h t l i g h t was flashing, and voltage was fluctuating. He switched e s s e n t i a l power t o t h e No. 2 genera t o r and l o s t a l l generator power momentarily, although t h e No. 3 generator f i e l d r e l a y remained closed. The second o f f i c e r switched t o standby power and then r e s e t No. 1 generator f i e l d r e l a y and s e t ese n t i a l power on No. 1 and power was restored. The No. 1 generator breaker was opened, and t h e No. 2 f i e l d r e l a y and t h e No. 2 and No. 1 13/ - The B-727 a l s o has an Auxiliary Power Unit (AFU), but it i s operable only when t h e a i r c r a f t i s on t h e ground. bus t i e breakers were closed. The No. 3 bus s t i l l remained unpowered because No. 3 f i e l d relay had opened. The No. 3 breaker w a s closed, and No. 3 bus t i e l e f t open. A l l power was then normal. After t h e landing, t h e f a u l t panel showed t h e No. 2 generator was underexcited. HAL was unable t o duplicate t h e above sequence of events e i t h e r on t h e ground or i n f l i g h t t e s t s . A number of p a r t s were removed and examined, but t h e reason f o r t h e l o s s of a l l generator power i s s t i l l unknown. The second incident occurred on a touch-and-go landing a t Cheyenne, Wyoming, on a t r a i n i n g f l i g h t on June 26, 1969. The No. 3 engine had been pulled back simulating a two-engine approach. A s t h e t h r o t t l e s were advanced t o t h e takeoff position, t h e i n s t r u c t o r noted t h a t t h e No. 2 or No. 3 EFR gauge did not advance a s rapidly as t h e No. 1 EFR gauge. Accordingly, t h e takeoff was aborted. The crew then noted t h e l o s s of a l l three generators. The No. 2 generator was showing a d i f f e r e n t i a l f a u l t , while No. 1 and No. 3 generators indicated an overvoltage condition. It was l a t e r found t h a t t h e No. 2 generator control panel had a f a u l t y SCR 15/ i n t h e d i f f e r e n t i a l control c i r c u i t ; a f t e r being heated f o r about 45 minutes, it would cause a standing d i f f e r e n t i a l f a u l t t o e x i s t which could not be r e s e t . The No. 1 voltage regulator was found t o modulate a t about 25 v o l t s peak-to-peak, a t about 20 cycles per second, due t o an intermittent open c i r c u i t i n t h e conductor L-1 i n t h e voltage regulator it s e l f . The t h i r d incident occurred at San Francisco on J u l y 18, 1969. After t h e a i r c r a f t turned o f f t h e runway, e s s e n t i a l power was switched from No. 3 generator t o No. 1, t h e No. 1 b u s t i e breaker then t r i p p e d on overexcitation and t h e No. 1 generator breaker was tripped manually. All generator power was l o s t . Essential power was switched t o standby and normal power restored. UAL -was unable t o duplicate t h e above circumstances, e i t h e r on t h e ground o r i n f l i g h t t e s t s . The generator control panels were removed from t h e a i r c r a f t and functionally tested. The incident i s still under investigation. &gine pressure r a t i o . Silicone controlled r e c t i f i e r . 2. 2.1 ANALYSIS AHD CONCLUSIONS Analysis On t h e b a s i s of t h e evidence adduced from t h e wreckage, and t h e recorded crew conversation i n t h e f i n a l moments of f l i g h t , it i s apparent t h a t t h e a i r c r a f t was i n an abnormal a t t i t u d e when it struck t h e water. The l i n d t e d s c a t t e r of t h e wreckage i s indicative of a steep impact angle, while t h e fragmentation p a t t e r n indicates t h a t t h e a i r c r a f t impacted a t a r e l a t i v e l y high r a t e of speed i n a r i g h t wing low, nose low a t t i t u d e . The exclamations of t h e f i r s t o f f i c e r during t h e f i n a l seconds ("Keep it going up you're a thousand f e e t p u l l it up") f u r t h e r demons t r a t e t h a t l o s s of a t t i t u d e o r i e n t a t i o n was experienced p r i o r t o s t r i k i n g t h e water. - - Based upon t h e f a c t t h a t p a r t s of a l l major elements of t h e a i r c r a f t were e i t h e r recovered o r were i d e n t i f i e d by means of t e l e v i s i o n , coupled with t h e f a c t t h a t these p a r t s were a l l located within a relat i v e l y small area on t h e ocean bottom, it can be concluded t h a t t h e a i r c r a f t w a s e s s e n t i a l l y i n t a c t a t impact. The extensive fragmentation of t h e wreckage precluded any determination concerning t h e condition of t h e control system at Impact. However, t h e r e was enough evidence t o conclude t h a t t h e No. 2 and No. 3 engines were capable of producing a s u f f i c i e n t l e v e l of power t o sustain t h e a i r c r a f t i n f l i g h t , despite t h e f a c t t h a t t h e No. 1 engine w a s shut down. I n attempting t o determine t h e f a c t o r s underlying t h e l o s s of attitude reference t h e t h r u s t of t h e investigation was primarily focused on two areas: (1) The circumstances surrounding t h e f i r e warning on t h e No. 1 engine, and (2) The nature of t h e e l e c t r i c a l power problems experienced during t h e f l i g h t , including t h e i r e f f e c t on t h e c a p a b i l i t y of t h e crew t o f l y t h e a i r c r a f t . With respect t o t h e first of these two areas, t h e r e was no evidence of f i r e on any part of t h e recovered wreckage, including t h e No. 1 engine and adjacent structure. It i s d i f f i c u l t t o reconcile t h i s lack of physical evidence of f i r e with ground witness observations of f i r e o r sparks i n f l i g h t . It i s possible, however, t h a t a phenomenon did i n f a c t occur which provided ground witnesses with a view of flames o r t h e appearance of sparks. One such p o s s i b i l i t y would be a t r a n s i e n t compressor stall on one of t h e two operating engines a f t e r t h e a i r c r a f t assumed an unusual f l i g h t a t t i t u d e p r i o r t o impact. One other p o s s i b i l i t y , although remote, i s a t r a n s i e n t compressor o r turbine rub o r t h e ingestion of a small p a r t i c l e by one of t h e two operating engines, which could r e s u l t i n t h e emission of sparks. Such an occurrence would not necessarily i m p a i r t h e operation of t h e engine, nor would evidence of it necessarily be detectable a f t e r impact and t h e r e s u l t a n t massive deformation of engine r o t a t i n g component s . To t h e extent t h a t t h e s e two sources of evidence a r e deemed incons i s t e n t , t h e Board i s of t h e view t h a t physical evidence, o r l a c k thereof, i s more persuasive than t h e observations o f several witnesses on a dark, rainy night. It i s t h e r e f o r e concluded t h a t an i n - f l i g h t engine f i r e did not occur. The remaining possible causes of t h e f i r e warning, once an a c t u a l f i r e i s discounted, a r e an overheat o r a f a l s e warning. The physical evidence derived from t h e wreckage, although negative i n regard t o both of t h e s e p o s s i b i l i t i e s , cannot be considered d e f i n i t i v e . Accordingly, no conclusive reason f o r t h e f i r e warning could be established. Based s o l e l y on t h e past h i s t o r y of f i r e warnings on t h e subject type of engine, t h e most probable cause of t h e f i r e warning was a n overheat condition within t h e engine compartment, which i n t u r n probably r e s u l t e d from a duct leak. Even i f such an assumption were t o be made, 25O F. sensor was however, we do not believe t h e f a c t t h a t a 325O incorporated on t h e No. 1 engine, r a t h e r than a '375O 25' F. sensor, can be considered a causal f a c t o r i n regard t o t h e f i r e warning. The incorporation of t h e higher temperature sensor w a s not mandatory. Furthermore, t h e higher temperature sensor merely delays t h e a c t i v a t i o n of t h e f i r e warning, it does not reduce t h e number of warnings. It therefore appears t h a t while a 375' sensor would not have been t r i g g e r e d at t h e same p r e c i s e point i n time as t h e 325' u n i t , it would have been actuated eventually, again assuming that some duct leakage did, i n f a c t , exist. / / I n any event, t h e No. 1 engine f i r e warning and shutdown, and t h e r e s u l t a n t reduction of a v a i l a b l e generators t o one, should not alone have caused t h e subsequent l o s s of a t t i t u d e o r i e n t a t i o n and crash of t h e a i r c r a f t , inasmuch a s t h e a i r c r a f t should have been operable with only one generator or, indeed, with none a t all. In other words, t h e crew should have been a b l e t o land t h e a i r c r a f t s a f e l y i f t h e r e had been no problems o t h e r t h a n ' t h e l o s s of t h e No. 1 engine. A s t h e i n v e s t i g a t i o n progressed, it became increasingly apparent t h a t t h e e l e c t r i c a l power problems encountered by F l i g h t 266 were most d i r e c t l y responsible f o r t h e eventual l o s s of orientation. I n order t o f a c i l i t a t e an analysis of t h e cause, nature, and e f f e c t of t h e s e problems, a chronological discussion of t h e pertinent events which occurred on Flight 266 i s s e t f o r t h below. The CTE shows t h a t t h e crew on F l i g h t 266 was aware t h a t t h e No. 3 generator was i n o p e r a t i v e p r i o r t o departure. It can t h e r e f o r e reasona b l y be assumed t h a t t h e second o f f i c e r t u r n e d o f f t h e g a l l e y power switch and one of t h e two air conditioning packs p r i o r t o t a k e o f f , a s prescribed by UAL procedures. Based on t h e cockpit voice recorder and t h e f l i g h t d a t a recorder, t h e t a k e o f f and e a r l y portion of t h e climbout were normal. The only i n d i c a t i o n of anything unusual during t h i s period was t h e observation o f one ground witness t h a t sparks were emanating from t h e r e a r engine and r i g h t s i d e of t h e a i r c r a f t . As noted previously, one possible explanation f o r t h e r e p o r t e d sparks would be a t r a n s i e n t compressor o r t u r b i n e rub o r t h e i n g e s t i o n of a small p a r t i c l e i n t o t h e engine. It i s a l s o p o s s i b l e t h a t t h e sparks were an e a r l y manifestation of t h e e l e c t r i c a l problem which l a t e r w a s t o cause t h e l o s s of a l l generator power. The above explanations a r e no more t h a n p o s s i b i l i t i e s , however, inasmuch a s t h e a v a i l a b l e evidence does not permit a conclusive determination concerni n g t h e sparks. A t 1.818:30, t h e sound of a warning b e l l was heard i n t h e cockpit. Four seconds l a t e r , t h e f i r s t o f f i c e r i d e n t i f i e d t h e b e l l as t h e "number one f i r e warning," and s h o r t l y t h e r e a f t e r t h e recorded conversation i n d i c a t e s t h a t he p u l l e d back t h e t h r u s t l e v e r on t h e No. 1 engine, as prescribed by-the engine f i r e emergency procedures. A t 1818:lA, a second warning horn was heard, which undoubtedly w a s t h e r e s u l t of t h e landing gear warning switch being a c t i v a t e d a s , t h e t h r u s t l e v e r was r e t a r d e d with t h e landing gear i n t h e up and locked p o s i t i o n . Commencing at 1818:45, t h e f i r s t o f f i c e r s t a t e d twice t h a t t h e airc r a f t w a s now on one generator. The c a p t a i n responded by s t a t i n g "Yeah, It i s t h e r e f o r e apparent t h a t t h e crew watch t h a t e l e c t r i c a l loading." was c l e a r l y aware of t h e l i m i t a t i o n s imposed by t h e reduction i n availa b l e e l e c t r i c a l power. A t 1818: 52, t h e f i r s t o f f i c e r posed t h e question "Everything o f f ? " which could have been d i r e c t e d t o t h e second o f f i c e r as a followup t o t h e preceding remark by t h e c a p t a i n t o assure t h a t a l l unnecessary e l e c t r i c a l l y powered components were turned o f f . The f i r s t o f f i c e r ' s i n q u i r y w a s apparently s a t i s f i e d , s i n c e t h e r e w a s no f u r t h e r conversation on t h e s u b j e c t . A t 1819:05, t h e first o f f i c e r reported t o Departure Control t h e predicament of t h e f l i g h t along w i t h t h e crew's i n t e n t i o n t o r e t u r n . A t 1819:13.5, 5 seconds a f t e r t h e end of t h e transmission t o Departure Control, CVR operation ceased. F l i g h t recorder operation terminated simultaneously. I n a d d i t i o n , t h e departure c o n t r o l l e r s t a t e d t h a t t h e transponder t a r g e t of t h e a i r c r a f t disappeared o f f t h e radarscope at approximately t h i s same point i n time. It can t h e r e f o r e b e concluded t h a t t h e a i r c r a f t l o s t i t s only o p e r a t i n g generator (No. 2) at 1819:13.5. The preceding analysis of t h e events leading up t o and including l o s s of e l e c t r i c a l power i s based p r h a r i l y on t h e cockpit voice recorder. Although t h e CVR provides no indications as t o t h e second o f f i c e r ' s actions during t h i s period, several deductions i n t h i s regard can be made. A t t h e time of t h e f i r e warnin , t h e e s s e n t i a l power s e l e c t o r switch was probably on t h e No. 1 engine. 167 The second o f f i c e r ' s f i r s t step, as prescribed by t h e emergency procedures, would have been t o move t h i s switch from t h e No. 1 engine t o t h e No. 2 engine. That he i n f a c t accomplishedthis s t e p p r i o r t o t h e shutdown of t h e No. 1 engine i s shown by t h e f a c t t h a t t h e CVR, which i s connected t o t h e e s s e n t i a l bus, remained operating a f t e r t h e No. 1 engine was shut down. The No. 1 engine would have been shut down by t h e pulling of t h e f i r e switch, which probably occurred not l a t e r than-the time (l818:52) when t h e f i r s t o f f i c e r posed t h e question "Everything off?" The pulling of t h i s switch energizes a time delay c i r c u i t t h a t i n t u r n t r i p s t h e generator f i e l d relay and t h e generator breaker within 5 t o 9 seconds. Accordingly, by 1819:01 at t h e l a t e s t , t h e No. 2 generator would have been carrying not only t h e e s s e n t i a l bus load, but a l s o t h e loads of all t h r e e buses, since it can be assumed t h a t a l l t h r e e bus t i e breakers were s t i l l closed. A t 1819:13.5, t h e No. 2 generator tripped o f f t h e l i n e , leaving t h e a i r c r a f t with no generator power. The dearth of physical evidence makes it d i f f i c u l t t o explain t h e l o s s of t h e No. 2 generator at t h i s point i n time. It i s not possible t o determine from t h e CVR whether normal e l e c t r i c a l power (115 v o l t s ) was being developed at t h e time power was l o s t . Although t h e l e v e l of power indicated on t h e CVR was apparently normal, voltage drops of 30 t o 40 v o l t s a r e not detectable on t h e CVR. If it i s assumed t h a t t h e power l e v e l was normal, any of t h e various f a u l t detection c i r c u i t s could have operated t o t r i p t h e No. 2 generator. I n any event, it i s apparent t h a t t h e placement of t h e e l e c t r i c a l load of aJ.l t h r e e generator buses plus t h e e s s e n t i a l bus on t h e No. 2 generator was instrumental i n t r i p p i n g t h a t generator o f f t h e l i n e . I f t h e l i n e voltage dropped abruptly from normal t o zero, one possible cause could have been a d i f f e r e n t i a l f a u l t . I f t h e problem were a 161 - This switch i s normally selected t o t h e operating generator which has t h e l e a s t amount of e l e c t r i c a l load on i t s bus. Of t h e t h r e e generators, No. 3 has t h e smallest bus load, No. 1 t h e next l a r g e s t load, and No. 2 t h e l a r g e s t . Since No. 3 generator had been rendered inoperative, No. 1 would have been selected. differential fault, it might not have created t h e 30 t o b.0 amperes d i f f e r e n t i a l required t o a c t i v a t e t h e d i f f e r e n t i a l protection c i r c u i t r y , u n t i l t h e l o s s of t h e No. 1 generator placed t h e f u l l e l e c t r i c a l load on t h e No. 2 generator. Another possible cause of t h e No. 2 generator's t r i p p i n g o f f t h e l i n e could have been an overload o r under voltage condition. Such a condition could have resulted from appropriate reductions i n t h e e l e c t r i c a l load not being accomplished subsequent t o t h e l o s s of t h e No. 1 generator. Single generator procedures prescribe that t h e g a l l e y power switch and both air conditioning pack switches should be turned OFF. One of t h e pack fans and t h e galley power switch should already have been i n t h e OFF position a t t h e time t h e No. 1 generator was l o s t since t h e f l a p s had not yet been retracted, 181 leaving only t h e remaining pack f a n switch t o be turned o f f t o r e a c h t h e prescribed load l e v e l . Accordingly, it i s d i f f i c u l t t o believe t h a t crew mismanagement of t h e e l e c t r i c a l system produced an overload condition. However, i f any one of the various components turned o f f were not i n f a c t disengaged from t h e e l e c t r i c a l power source, an overload could r e s u l t . Even i f t h e e l e c t r i c a l load had been reduced t o t h e proper l e v e l , it i s possible t h a t a n overload condition r e s u l t e d from t h e remaining generator supplying a lower than normal amount of voltage. I f an overload condition did i n f a c t occur, t h e s e v e r i t y of t h e condition a s well as t h e manner i n which it was imposed may have been significant. Extensive ground and f l i g h t t e s t i n g conducted a f t e r t h e accident indicated t h a t during c e r t a i n extreme overload conditions, s u f f i c i e n t induced interference may be present on some B-727 a i r c r a f t t o i n h i b i t proper operation of t h e No. 2 time delay c i r c u i t of t h e prot e c t i o n panel. The expected a c t i o n of t h i s panel during such an overload would be t o t r i p t h e bus t i e breaker (BTB), thereby i s o l a t i n g t h e generator and i t s load bus from t h e r e s t of t h e system, which usually c l e a r s t h e overload. However, i f t h e No. 2 time delay c i r c u i t i s disabled by t h e induced interference, t h e No. 1 time delay c i r c u i t w i l l continue t o sense t h e overload and, a f t e r 5 t o 9 seconds, w i l l t r i p t h e generator control r e l a y and t h e generator c i r c u i t breaker, thus removing t h e generator from A d i f f e r e n t i a l f a u l t e x i s t s when t h e r e i s a difference of a c e r t a i n preset anaunt l i n e current between t h e current transformers connected on t h e n e u t r a l side of t h e generator and those connected on t h e l i n e side. 181 - Immediately p r i o r t o t h e sound of t h e f i r e warning b e l l , t h e crew conversation indicates t h a t t h e first o f f i c e r moved t h e f l a p handle f r o m t h e 5' t o t h e 2 ' position. t h e system. Applying t h i s theory t o Flight 266, it i s possible t h a t t h e sudden s h i f t of t h e e n t i r e e l e c t r i c a l load t o t h e No. 2 generator produced a shock load of s u f f i c i e n t dimensions t o t r i g g e r t h e sequence described above. 19/ - It i s remotely possible t h a t t h e apparently uncorrected problem which existed i n t h e No. 3 generator system may have been a f a c t o r i n the l o s s of t h e No. 2 generator. The No. 3 system was r e l a t i v e l y f r e e of problems u n t i l t h e i n s t a l l a t i o n on January 13, 1969, of control panel S/N 163, which had an extensive history of malfunctions f o r a v a r i e t y of reasons. Shortly t h e r e a f t e r , t h e No. 3 generator w a s replaced because t h e f i e l d relay would not s t a y closed. Three and a half hours l a t e r a similar discrepancy occurred, a f t e r which t h e No* 3 generator w a s rendered inoperative. The occurrence of two similar problems within such a short time a f t e r i n s t a l l a t i o n of a control panel, coupled with t h e f a c t t h a t t h e generator which was removed functioned properly i n shop t e s t s , i n d i c a t e s t h a t t h e problem was not corrected and probably was associated with t h e control panel. A t t h e same time, however, it i s unlikely t h a t t h i s problem could have affected t h e No. 2 generator system since t h e No. 3 system should have been e f f e c t i v e l y i s o l a t e d when it w a s rendered inoperative 3 days p r i o r t o t h e accident, assuming that t h e relays involved i n i s o l a t i n g t h e No. 3 system c i r c u i t r y functioned properly. SO/ Regardless of t h e cause of t h e No. 2 generator's t r i p p i n g off t h e l i n e , t h e l o s s of all generator power should not i n i t s e l f have r e s u l t e d i n l o s s of a l l e l e c t r i c a l power. The a i r c r a f t i s equipped with a standby system, completely separate from t h e normal system powered by t h e genera t o r s , which supplies power from t h e b a t t e r y t o those instruments and radios necessary t o allow t h e c a p t a i n ' t o make a safe approach and landing under instrument conditions. The standby system i s activated, i f t h e b a t t e r y switch i s on, by placing t h e e s s e n t i a l power s e l e c t o r switch i n t h e standby position. There i s evidence, however, t h a t t h e standby system was not i n operation during t h e period subsequent t o l o s s of t h e No. 2 generator and p r i o r t o t h e b r i e f r e s t o r a t i o n of e l e c t r i c a l power a t an indeterminate l a t e r time. If t h e standby system had been activated, t h e crew would - 191 - a A s discussed, hereinafter, t h e b a t t e r y switch may have been inadvertently turned off p r i o r t o l o s s of t h e No. 2 generator. Flight t e s t s showed that t h i s too could a f f e c t t h e normal sequence of t h e t r i p p i n g of t h e various breakers. These problems may have been caused by t h e f a c t that Westinghouse Service Bulletin 66-103 (~eptember1966), which recommended t h e replacement of a s i l i c o n e controlled r e c t i f i e r i n order t o prevent nuisance t r i p p i n g of t h e d i f f e r e n t i a l protection c i r c u i t r y , had not been accomplished on panel S/N 163. This replacement had been accomplished on t h e panels i n s t a l l e d i n t h e Nos. 1 and 2 generating systems on IT7434U. have had available t h e No. 1 VHF transmitter and receiver and, therefore, wouldhave been able t o communicate with Departure Control. The f l i g h t , however, not only f a i l e d t o respond t o Departure Controlts repeated c a l l s , but a l s o reacted t o t h e heading instruction of 060' by turning i n t h e opposite direction. It thus appears t h a t t h e VHF communications system and, by t h e same token, t h e standby system were not functioning. Furthermore, i f t h e standby system had i n f a c t been a c t i v a t e d and had operated properly, t h e r e would have been no reason t o switch the e s s e n t i a l power back t o t h e No. 2 generator, which was t h e s e t t i n g when power was restored and t h e a i r c r a f t apparently went out of control. In view of t h e foregoing, t h e Board concludes t h a t t h e standby system was not activated o r f a i l e d t o function. I n regard t o t h e f a c t t h a t t h e a i r c r a f t was flown on a s t r a i g h t course a f t e r losing t h e No. 2 generator, without having reference t o a t t i t u d e instruments, it should be noted t h a t t h e captain would have had adequate time between t h e f i r e warning and t h e l o s s of t h e No. 2 generator t o l e v e l the a i r c r a f t and t r i m it up f o r two-engine f l i g h t . Unless he had consciously attempted t o change heading, t h e trimmed condition would have kept t h e airc r a f t on a r e l a t i v e l y s t r a i g h t course, at l e a s t f o r t h e b r i e f period of time involved. Moreover, when t h e a i r c r a f t l o s t power and t h e cockpit became darkened, the captain may have had some outside reference, even i f only t o a cloud layer. Although t h e available evidence does not permit a conclusive determination as t o why t h e standby system was not activated o r why it f a i l e d t o function, one l o g i c a l explanation therefor involves t h e r e l a t i v e positions of t h e b a t t e r y and galley power switches. N'7434U was a QC model a i r c r a f t , and due t o t h e requirements f o r i n s t a l l a t i o n of a cargo smoke detector, the b a t t e r y panel had been moved and t h e b a t t e r y switch relocated just above and s l i g h t l y t o t h e l e f t of t h e galley power switch. Both a r e ON-OFF toggle switches. When t h e No. 1 generator w a s shirt down, one of t h e f i r s t actions of t h e second o f f i c e r would have'been t o reduce t h e e l e c t r i c a l load. One of t h e c ~ p o n e n t swhich should be off when operating on one genera t o r i s t h e galley power. Accordingly, even though galley power should have been o f f since p r i o r t o takeoff, t h e second o f f i c e r may have ins t i n c t i v e l y brushed t h e galley power switch with h i s hand t o make c e r t a i n it was off and h i t t h e b a t t e r y switch instead. I f t h e b a t t e r y switch had been inadvertently turned off i n t h e above manner, t h e r e would have been no indication of i t s being o f f i n t h e cockpit at t h a t time. Thereafter, when the' No. 2 generator was l o s t , an attempt t o a c t i v a t e t h e standby system would have been unavailing with t h e b a t t e r y turned off. I f t h e b a t t e r y switch had not been turned off, there a r e several other possible explanations why t h e standby system was not activated. The f i r s t involves t h e UAL emergency procedures f o r l o s s of all generators. A s constituted a t t h e time of t h e accident, these procedures included no mention of switching t o standby, but r a t h e r prescribed t h a t any generator f i e l d relay should be closed and t h e e s s e n t i a l power s e l e c t o r placed on t h e operating generator. It i s therefore possible t h a t , following l o s s of t h e No. 2 generator, t h e first o f f i c e r , e i t h e r d i r e c t l y r e f e r r i n g t o t h e checklist o r with it i n mind, repeatedly attempted t o b r i n g t h e No. 2 generator back on t h e l i n e . On t h e other hand, a U&L i n s t r u c t o r t r a i n e d t h e second o f f i c e r t o r e s t o r e generator power only once before switching t o standby. Furthermore, i f t h e second o f f i c e r had not attempted t o switch t o standby reasonably soon a f t e r t h e No. 2 generator was l o s t , e i t h e r t h e captain o r t h e first o f f i c e r probably would have reminded him t o do so. %/ A second possible reason t h a t t h e standby system was not activated, if the b a t t e r y switch was on, involves t h e e s s e n t i a l power s e l e c t o r switch i t s e l f . This switch must pass through a gate i n order t o be moved i n t o t h e detented standby position. Although t h e second o f f i c e r should have been familiar with t h i s c h a r a c t e r i s t i c of t h e switch, it i s possible that when t h e cockpit became suddenly and unexpectedly darkened upon l o s s of t h e No. 2 generator, he moved t h i s switch counterclockwise u n t i l he encountered t h e obstruction and assumed it was i n t h e standby position. I n f a c t , it would have then been i n t h e APU position, which i s a dead c i r c u i t i n f l i g h t . It i s a l s o possible t h a t t h e standby system f a i l e d t o function because of a malfunction i n t h e b a t t e r y o r b a t t e r y charger. This could a l s o explain why t h e crew eventually switchedthe e s s e n t i a l power switch from standby back t o t h e No. 2 generator, even though t h a t generator was supplying low voltage. A b a t t e r y malfunction could a l s o c o n s t i t u t e a d i f f e r e n t i a l f a u l t which might have been t h e cause of t h e No. 2 generator i n i t i a l l y t r i p p i n g off t h e l i n e . When all generator power was l o s t , and assuming t h e standby system was not activated o r f a i l e d t o function, t h e only l i g h t i n g available, apart from t h a t which might have been provided by f l a s h l i g h t s , would have been t h e emergency e x i t l i g h t s over t h e door leading t o t h e passenger compartment. 23/ If t h a t happened, it can be assumed t h a t t h e second o f f i c e r was attempting e i t h e r t o a c t i v a t e t h e standby system o r t o bring t h e No. 2 generator back on t h e l i n e , while t h e p i l o t s were doing t h e i r best t o control t h e a i r c r a f t i n a semi-darkened cockpit with no a t t i t u d e J l 2 I n t h i s connection, it should be noted that a red l i g h t on t h e second o f f i c e r ' s instrument p e l becanes illuminated when e s s e n t i a l power i s l o s t . This l i g h t w i l l remain on a f t e r t h e e s s e n t i a l power s e l e c t o r switch i s moved t o standby, assuming that t h e b a t t e r y switch i s on, and thus does not c o n s t i t u t e an indication t h a t t h e standby system i s not operating. 22/ - The purpose of t h e detent i s apparently t o assure t h a t t h e operator i s aware t h a t he i s switching t o an emergency operation. 231 - These l i g h t s a r e powered by a separate b a t t e r y and a r e activated automatically when e l e c t r i c a l power i s l o s t . instruments. If t h e b a t t e r y switch were o f f , thus making it impossible t o a c t i v a t e t h e standby system, it i s d i f f i c u l t t o comprehend why one of t h e crewnembers did not t h i n k of t h i s p o s s i b i l i t y and check t h e switch. The only explanation i s t h a t t h e cockpit was i n a s t a t e of confusion and each of t h e crew was b u s i l y engaged with h i s own immediate problems, with t h e consequence t h a t a switch such as t h e battery, which i s presumed t o be on at all time, was overlooked. a A s r e f l e c t e d by t h e reactivation of t h e f l i g h t data recorder and t h e cockpit voice recorder f o r 15 and 9 seconds,respectively, t h e No. 2 generator came back on t h e l i n e at some l a t e r indeterminate time. Although t h e precise point i n time when t h e two recorders became reactivated, o r whether they were reactivated simultaneously cannot be determined, some rough approximations i n t h i s regard can be made. The radar c o n t r o l l e r who was handling Flight 266 estimated t h a t t h e primary t a r g e t of t h e a i r c r a f t disappeared from t h e radarscope within two sweeps, o r 5 t o 11 seconds, a f t e r he directed t h e f l i g h t t o t u r n r i g h t t o 060'. The cont r o l l e r made two successive transmissions containing t h i s heading direction, t h e f i r s t of which ended at 1820:33, while t h e second terminated a t 1820:U. Primary t a r g e t disappearance, based on f l i g h t t e s t s , should have occurred as t h e a i r c r a f t was descending through TOO f e e t and thus can be c l o s e l y r e l a t e d t o t h e f i n a l remarks a t t h e end of t h e CVR. Three seconds p r i o r t o CVR termination, t h e f i r s t o f f i c e r s a i d t o t h e captain "Keep it going up Arnie, you're a thousand f e e t " and 2 seconds l a t e r said, "Pull it up." It therefore appears t h a t t h e CVR ceased operating a t about t h e same time t h e primary t a r g e t disappeared. I n view of t h e absence on t h e CVR of t h e Departure Control transmissions at 1820:30 t o 1820:33 and 1820:kO t o 1820:44, it can be f u r t h e r approximated t h a t t h e CVR terminated 10 o r 11 seconds a f t e r completion of t h e second of these transmissions and had resumed operation at 1820: 45 o r 1820: 46. a The approximate time when t h e f l i g h t data recorder ceased operation following t h e reactivation period of 1 5 seconds can be deduced only i f t h e f i n a l t r a c e indications can be considered reasonably valid. Thus, i f t h e f i n a l a l t i t u d e t r a c e of 630 f e e t i s accepted a s a reasonably accurate r e f l e c t i o n of t h e a i r c r a f t a l t i t u d e at t h a t point, it could be concluded t h a t both recorders ceased operation at t h e same time. It would then follow t h a t t h e f l i g h t recorder resumed operation 6 seconds p r i o r t o t h e CVR. "241 - The only indication t h a t t h e b a t t e r y switch was not on, apart from t h e i n a b i l i t y t o a c t i v a t e t h e standby system, would have been t h e absence of c e r t a i n l i g h t s i n t h e cockpit. Under t h e circumstances, however, t h e i r absence might not be recognized. The conclusion that t h e CVR terminated p r i o r t o impact, while t h e airc r a f t was s t i l l airborne, i s substantiated by t h e absence of impact sounds on t h e recording. The reasons underlying r e s t o r a t i o n of t h e No. 2 generator a r e diffic u l t t o assess, again due t o t h e lack of physical evidence. The f a c t t h a t components powered by t h e e s s e n t i a l bus (CVB) t h e No. 2 bus ( f l i g h t recorder), and t h e No. 1bus ( a i r data computer) 26/ indicates t h a t t h e No. 2 f i e l d relay, c i r c u i t breaker, and bus t i e breaker were a l l closed and t h a t t h e e s s e n t i a l power s e l e c t o r switch was positioned t o t h e No. 2 generator. I n t h i s connection, t h e remark by one of t h e crew, following r e s t o r a t i o n of power, t h a t t h e " f i e l d ' s o u t " undoubtedly was a reference t o t h e f i e l d r e l a y l i g h t being off, as it should have been since t h e generator was operating. a Tests based on t h e power l e v e l r e f l e c t e d by t h e CVR showed t h a t a low voltage condition of approximately 50 v o l t s (as opposed t o normal voltage of 115 v o l t s ) existed when power was restored on Flight 266. This power l e v e l was simulated by s t a r t i n g one generator with normal a i r c r a f t loading f o r two generators applied. If t h e problem which caused t h e No. 2 generator t o t r i p off t h e l i n e s t i l l existed, it i s possible t h a t t h e second o f f i c e r on Flight 266, i n a last desperate attempt t o r e s t o r e power, manually closed t h e No. 2 f i e l d r e l a y and held it closed t o keep t h e protection c i r c u i t r y from t r i p p i n g it. Seconds l a t e r , as t h e a i r c r a f t entered an abnormal a t t i t u d e , t h e second o f f i c e r ' s hand may have been thrown away from t h e panel, thus causing the'complete l o s s of t h e remaining generator power available. It i s a l s o possible t h a t power was restored as a r e s u l t of t h e clearing of t h e d i f f e r e n t i a l f a u l t , i f one caused t h e i n i t i a l l o s s of No. 2 generator. I f t h i s happened, t h e low voltage condition should have activated t h e prot e c t i v e c i r c u i t r y which, i n turn, would have t r i p p e d t h e bus t i e breaker and t h e generator breaker. However, if t h e b a t t e r y switch were s t i l l o f f , t h e sequence and t h i n g of t h e t r i p p i n g of these breakers would again have been disrupted. 281 - The f a c t t h a t t h e two recorders operated f o r e f f e r e n t lengths of time i s d i f f i c u l t t o r a t i o n a l i z e . The most plausible explanation i s t h a t these u n i t s require d i f f e r e n t l e v e l s of voltage f o r t h e i r operation and, therefore, a s t h e voltage output of t h e No. 2 generator b u i l t up and then receded, t h e CVR e i t h e r became activated l a t e r , o r deactivated sooner, than t h e f l i g h t recorder. 261 - The f l i g h t recorder t r a c e s would have been s t r a i g h t horizontal l i n e s i f power t o t h e a i r data computer had not a l s o been restored. a The transponder did not come back on because it has an &second protective time delay c i r c u i t . 28/ The time delay c i r c u i t r y , if functioning properly, should have tripped t h e generator o f f t h e l i n e 5 t o 9 seconds a f t e r power was restored a t an undervoltage l e v e l . Based on t h e f l i g h t recorder, however, some generator power was available f o r 1 5 seconds. Regardless of t h e reasons underlying r e s t o r a t i o n of power, it appears that t h e second o f f i c e r was aware t h a t t h e predicament of t h e f l i g h t was not yet remedied. This conclusion i s based on h i s remark, several seconds a f t e r power was restored, t h a t "We're gonna get screwed up," followed by "I don't know (what's going on) ." The remaining question concerns t h e causal r e l a t i o n s h i p between t h e e l e c t r i c a l system problems discussed above and t h e eventual crash. F l i g h t t e s t s indicated that e l e c t r i c a l power outages would not have a s u b s t a n t i a l impact on t h e f l i g h t control system. It therefore appears t h a t t h e most s i g n i f i c a n t adverse e f f e c t of t h e e l e c t r i c a l power l o s s on t h e c a p a b i l i t y of t h e p i l o t s t o f l y t h e a i r c r a f t would have involved t h e a t t i t u d e reference instruments, which a r e so c r i t i c a l t o t h e operation of an a i r c r a f t under instrument conditions. The b a s i c instrument i n t h e cockpit from which a p i l o t i n a B-727 derives a t t i t u d e information i s t h e a t t i t u d e indicator, which i n t u r n receives data from an e l e c t r i c a l l y powered v e r t i c a l gyro. When MT434U was i n i t i a l l y s t a r t e d up, t h i s v e r t i c a l gyro would have established a v e r t i c a l plane with reference t o t h e ground. When e l e c t r i c a l power was l o s t i n f l i g h t , a f l a g l a b e l l e d "gyro" would have appeared i n t h e lower f a c e of t h e a t t i t u d e i n d i c a t o r instrument and t h e i n d i c a t o r would have r o l l e d t o a 90' pitchup a t t i t u d e . 291 The gyro i t s e l f would then have s t a r t e d t o coast down, although a c e r t a i n amount of s t a b i l i t y would have been retained i n t h e gyro assembly. However, i f t h e a i r c r a f t a t t i t u d e were a l t e r e d from t h e l e v e l p o s i t i o n by climbing o r descending, o r banking l e f t o r r i g h t , precession of t h e gyro gimbals would have occurred. Upon r e s t o r a t i o n of power, t h e a t t i t u d e i n d i c a t o r presentation of 90' pitchup would have r o l l e d back toward t h e a t t i t u d e of t h e v e r t i c a l gyro. I n addition, t h e v e r t i c a l gyro would have gone i n t o t h e f a s t erection cycle. However, i f t h e gyro had precessed during t h e period e l e c t r i c a l power was l o s t , o r i f t h e a i r c r a f t were i n a position other than l e v e l when power was restored, t h e gyro would not be referenced t o t h e ground, but r a t h e r would be sensing and erecting toward a f a l s e v e r t i c a l plane. Accordingly, i f t h e captain had attempted t o change t h e a t t i t u d e of t h e a i r c r a f t toward an instrument i n d i c a t i o n of l e v e l f l i g h t under t h e above conditions, he would have been maneuvering t h e a i r c r a f t with reference t o a f a l s e "horizon," which would have served t o aggravate f u r t h e r an already serious o r i e n t a t i o n problem. a The only o t h e r instrument i n t h e cockpit which provides a t t i t u d e infornation, t h e t u r n needle, i s controlled by an e l e c t r i c a l s i g n a l and t h e r e f o r e would a l s o have been rendered inoperative. When t h e e l e c t r i c a l signal t o t h i s instrument was removed, t h e needle would have remaine? centered, t h u s indicating l e v e l f l i g h t . The gyro warning f l a g should have remained i n view during t h e b r i e f period power was restored. 301 Nevertheless, when t h e cockpit l i g h t s suddenly came on upon r e s t o r a t i o n of power, causing t h e l o s s of whatever outside reference may have been available, t h e captain might have turned t o t h e gyro horizon a s a last r e s o r t i n attempting t o e s t a b l i s h t h e a t t i t u d e of t h e a i r c r a f t . On t h e other hand, t h e i n t e n s i t y of t h e cockpit l i g h t s , i n view of t h e low voltage conditions, may not have been bright enough t o allow t h e p i l o t s t o view t h e instruments. I n e i t h e r event, t h e p i l o t s would have been without a r e l i a b l e a t t i t u d e reference, e i t h e r inside o r outside t h e a i r c r a f t . 3-/l The reasons underlying t h e l e f t t u r n commenced by Flight 266 p r i o r t o disappearing from t h e radarscope cannot be conclusively determined. The captain may have been attempting t o t u r n back toward t h e a i r p o r t , and elected t o do so t o t h e l e f t i n view of h i l l y coastline which l a y t o t h e north, o r r i g h t , of t h e a i r c r a f t at t h a t time. It i s a l s o possible t h a t t h e t u r n represented t h e e a r l y stages of disorientation with regard t o t h e a t t i t u d e of t h e a i r c r a f t . I n any event, once t h e t u r n was i n i t i a t e d , t h e d i f f i c u l t y of t h e captain i n determining t h e a t t i t u d e of t h e a i r c r a f t would have accelerated. This conclusion i s substantiated by t h e remarks of t h e f i r s t o f f i c e r during t h e f i n a l moments ( " ~ e e pit going up .I' "Pull it up"), which apparently were prompted by h i s concern about t h e rapid l o s s of a l t i t u d e . Even i f t h e captain had pulled back on t h e yoke i n response t o those remarks, t h e descent would not have been a r r e s t e d unless t h e wings were levelled. Without any a t t i t u d e reference, t h e captain may have held t h e yoke as nearly centered as possible, thus causing t h e l e f t t u r n t o t i g h t e n a s t h e a i r c r a f t descended t o impact. .. One f i n a l matter which warrants comment concerns t h e f a c t t h a t t h e captain on Flight 266 had been f l y i n g only DC-8's since December 2, 1968. Apparently, t h e r e i s no difference between t h e B-727 and t h e DC-8 i n terms of cockpit configuration and instrument location t h a t could have s i g n i f i cantly affected t h e captain's reactions under emergency conditions, other than t h e f a c t t h a t t h e DO-8 has no standby e l e c t r i c a l system. Nevertheless, t h e r e l a t i v e lack of f a m i l i a r i t y i n i t s e l f , r e s u l t i n g from 7 weekst absence from t h e a i r c r a f t , nay have posed problems, a l b e i t minor. For example, t h e f l i g h t controls on t h e DC-8 require g r e a t e r pressure t o move than those on t h e B-727. That such a difference i s noticeable t o p i l o t s i s demons t r a t e d by t h e captain's comment t o t h e first o f f i c e r , shortly a f t e r takeo f f , "You handle these things l i g h t on t h e controls,'' t o which t h e f i r s t o f f i c e r responded "Yeah." 30/ 311 - Under t h e low voltage conditions prevailing a f t e r power restoration, there would have been no power supplied t o t h e f l a g r e t r a c t i o n c i r c u i t r y . The t u r n needle may a l s o have been affected by t h e deficiency i n t h e restored power l e v e l . On balance, t h e r e i s i n s u f f i c i e n t evidence t o support a conclusion t h a t t h e captain's having flown only DC-8's i n t h e 7 weeks preceding t h e accident was a contributing f a c t o r . Nevertheless, t h e Board, believes t h a t t h i s type of scheduling could p o t e n t i a l l y lead t o a compromise i n safety. Accordingly, we note with approval t h a t United Air Lines has adopted a procedure whereby p i l o t s who have completed t r a n s i t i o n a l t r a i n i n g i n a p a r t i c u l a r a i r c r a f t a r e afforded t h e opportunity t o refamiliarize themselves i n another a i r c r a f t , i n which they had previously been checked out, p r i o r t o being assigned f l i g h t s i n t h e l a t t e r a i r c r a f t 2.2 Conclusions (a) Findings The flightcrew was properly c e r t i f i c a t e d and q u a l i f i e d t o conduct t h e f l i g h t . The captain had been t r a n s i t i o n i n g t o t h e DC-8 during t h e period p r i o r t o t h e accident and had not flown i n a E727 since December 2, 1968. The a i r c r a f t was properly c e r t i f i c a t e d and airworthy. The a i r c r a f t had been operating f o r 42 f l i g h t hours p r i o r t o t h e accident with t h e No. 3 generator inoperative, a s d o w e d by t h e Minimum Equipnent List. The discrepancy which caused t h e No. 3 generator t o be rendered inoperative had not been corrected and probably was associated with i t s e l e c t r i c a l control panel. The f l i g h t experienced a f i r e warning on t h e No. 1 engine during climbout and t h e engine w a s shut down. There was no physical evidence i n t h e recovered wreckage indicating t h a t an i n - f l i g h t f i r e had occurred. Shortly a f t e r shutdown of t h e No. 1 engine, e l e c t r i c a l power from t h e remaining generator (No. 2) was l o s t . The available evidence does not permit a determination a s t o t h e exact cause of t h e l o s s of all generator power, other than associating t h i s l o s s with t h e sudden placement of aJ.l t h r e e generator bus loads, a s well as t h e e s s e n t i a l bus, on t h e No. 2 generator. Following l o s s of all generator power, t h e standby e l e c t r i c a l system e i t h e r was not activated o r f a i l e d t o function. E l e c t r i c a l power a t a voltage l e v e l of approximately 50 v o l t s was restored approximately a minute and a half a f t e r l o s s of t h e No. 2 generator. The duration of power r e s t o r a t i o n was 9 t o 15 seconds, following which power was again l o s t at some indeterminate point p r i o r t o impact. The a i r c r a f t w a s i n an abnormal a t t i t u d e at impact. The No. 2 and No. 3 engines were developing power at impact. There was no evidence of a malfunction i n t h e f l i g h t control system. The f l i g h t was conducted under night, instrument conditions. The p i l o t s would have been without a r e l i a b l e a t t i t u d e reference, e i t h e r inside o r outside t h e a i r c r a f t , from t h e point i n time t h e No. 2 generator was l o s t u n t i l impact. (b) Probable Cause The Board determines t h a t t h e probable cause of t h i s accident was l o s s of a t t i t u d e o r i e n t a t i o n during a night, instrument departure i n which t h e a t t i t u d e instruments were disabled by l o s s of e l e c t r i c a l power. The Board has been unable t o determine ( a ) why a U generator power was l o s t o r ( b ) why t h e standby e l e c t r i c a l -power system e i t h e r was not activated o r f a i l e d t o function. 3. RECCMMENDA.TIONS AMD COBEECTIVE MEASURES By l e t t e r dated J u l y 11, 1969, t h e Chairman of t h e Safety Board recommended t o t h e Administrator of t h e FAA t h a t t h e automatic switching of e s s e n t i a l power t o standby power upon l o s s of a l l generators be made a mandatory requirement f o r all turbine-powered a i r c r a f t . It was f u r t h e r recommended t h a t u n t i l such time as t h e above requirement could be implemented throughout t h e industry, t h e emergency checklists f o r a l l a i r l i n e s pertaining t o "Loss of a l l Generators" require t h a t t h e second o f f i c e r , o r captain i f appropriate, check t o assure t h a t t h e b a t t e r y switch i s ON, then immediately switch e s s e n t i a l power t o t h e standby o r emergency position. It was t h e Safety Board's view t h a t t h i s would give t h e captain t h e instruments and l i g h t s necessary t o f l y t h e a i r c r a f t while t h e second o f f i c e r could "troubleshoot" t h e e l e c t r i c a l system. I n h i s response of J u l y 28, 1969, t h e Administrator s t a t e d t h a t t h e FAA had been investigating e l e c t r i c a l emergency operating procedures f o r sane time and a c t i o n was being taken t o prescribe procedures f o r t h e B-727 consistent with Safety Board recommendations. 321 With regard t o automatic switching f o r e s s e n t i a l f l i g h t instruments, t h e ~ d m i n i s t r a t o'rs l e t t e r referred t o Sections 25.1309 and 25.1333 of Notice of Proposed Rule Making (HIRM) 68-18, which provide f o r t h e immediate a v a i l a b i l i t y of e s s e n t i a l instruments a f t e r e l e c t r i c a l f a i l u r e s and which apply t o a i r c r a f t with a date of application f o r type c e r t i f i c a t i o n a f t e r adoption of t h e proposed rule. For inservice a i r c r a f t , t h e FAA had issued IiPFZM 69-26 which provides f o r t h e i n s t a l l a t i o n i n l a r g e turbojet-powered airplanes used i n t h e a i r c a r r i e r service of a t h i r d independently powered a t t i t u d e indicator. 331 The Administrator expressed t h e b e l i e f t h a t t h i s action, combined w i t h specified a i r p l a n e f l i g h t manual emergency procedures, w i l l provide f o r a s a t i s f a c t o r y l e v e l of s a f e t y f o r inservice a i r c r a f t . I n order t o remove any doubt as t o t h e s t a t u s of t h e standby system during a "Loss of all Generators" emergency, it i s f u r t h e r recommended t h a t t h e second o f f i c e r on a B-727 be provided with a positive indication on 321 - a The FAA issued an Airworthiness Directive, e f f e c t i v e August 1, 1969, requiring revision of t h e Boeing 727 Airplane Flight Manual, Bnergency Procedures Section, Loss of all Generators paragraph, t o include procedures which would d i r e c t t h e flightcrew t o switch t o t h e standby power system, insure t h e b a t t e r y switch i s "ON", and reduce loads. The proposal embodied i n NEW 69-26 was adopted on January 8, 1970, and became e f f e c t i v e on February 5, 1970, a s Section 121.305(j) of t h e FAR, which requires t h a t t h e additional a t t i t u d e indicator be i n s t a l l e d on a l l l a r g e turbojet a i r c r a f t a f t e r August 5, 1971. h i s panel when t h e standby system i s being powered from t h e battery. Such an indication could take t h e form of a l i g h t , such as t h a t i n s t a l l e d on t h e B- 747 a i r c r a f t f o r t h e sane purpose. The l i g h t would become illuminated when t h e standby system i s activated. Another a l t e r a t i o n which might be considered i n connection with t h e foregoing recommendation would be t h e t r a n s f e r of t h e standby feature from t h e e s s e n t i a l power s e l e c t o r switch t o a separate OK-OFF toggle switch, which again i s t h e arrangement on t h e B-747. The addition of such a switch would not only serve t o simplify a c t i v a t i o n of t h e standby system, but would a l s o f a c i l i t a t e troubleshooting t h e generators when t h e standby system i s on: The FAA a l s o took several other actions r e l a t i n g t o t h e subject accident. A s a r e s u l t of information developed during t h e e a r l y stages of t h e investigation, t h e FAA issued an Airworthiness Directive by telegram on January 31, 1969, requiring B-727 operators t o provide a means t o prevent inadvertent operation of t h e b a t t e r y switch i n those a i r c r a f t i n which t h e b a t t e r y switch i s located within 10 inches of t h e galley power switch. On August 1, 1969, t h e FAA proposed an Airworthiness Directive requiring t h e i n s t a l l a t i o n of a capacitor i n accordance with b e i n g Service Bulletin No. 24-47 (March 3, 1969), f o r t h e purpose of f i l t e r i n g out e l e c t r i c a l interference which may be present t o a s u f f i c i e n t extent on some B-727 a i r c r a f t t h a t , under an overloaded condition, t h e generator control panel may disable t h e generator before opening t h e bus t i e c i r c u i t breaker. On September 10, 1969, t h e FAA proposed an Airworthiness Directive which would require replacement of both s i l i c o n controlled switches CR 10 and CR 28 with a t r a n s i s t o r i z e d amplifier and a miniature two-pole r e l a y on B-727 airplanes, i n accordance with Westinghouse Service W e t i n 103, dated September 15, 1966. A s a reason f o r t h i s replacement, t h e FAA c i t e d f a i l u r e s of t h e generator overload protection c i r c u i t s i l i c o n controlled r e c t i f i e r s , causing a single generator system lockout on B-727 a i r c r a f t . During t h e investigation, a considerable amount of a t t e n t i o n was focused on t h e Minimum Equipnent List (MEL) and, more s p e c i f i c a l l y , on t h e question of whether t h e MEL, with regard t o t h e required number of operative generators, was adequate i n l i g h t of t h e subject accident. The MEL f o r t h e B-727 was established through extensive ground and f l i g h t t e s t i n g , a f t e r which it w a s agreed through meetings with t h e involved p a r t i e s , including t h e FAA, Boeing, and United, t h a t t h e a i r c r a f t would be airworthy with two generators. An additional margin of s a f e t y was provided by t h e standby system, through which e l e c t r i c a l power could be supplied from t h e b a t t e r y t o those instruments and components necessary t o enable t h e p i l o t t o make an approach and landing under instrument conditions. The t h i r d generator was included on t h e &-727, not as a matter of safety, but r a t h e r t o enhance schedule dependability. For example, i f one of t h e t h r e e generators should become disabled, t h e a i r c r a f t would s t i l l be able t o operate without delay through small f i e l d s which lack t h e maintenance capability t o r e p a i r an inoperative generator. Subsequent t o c e r t i f i c a t i o n , the B-727 e l e c t r i c a l system has been a l t e r e d i n minor respects only, which primarily involved changes i n procedures r a t h e r than increases i n loading. Furthermore, t h e f l i g h t t e s t s conducted a f t e r t h e accident substantiated t h e a b i l i t y of t h e a i r c r a f t t o carry design loads during one and two generator operation. FinaUy, and perhaps most i m p r t a n t l y , t h e f a c t t h a t Flight 266 departed with one generator.inoperative cannot be c l a s s i f i e d as a causal f a c t o r i n t h e accident. The shutdown of t h e No. 1 engine, t h e l o s s of t h e No. 2 generator, and t h e nonactivation of t h e standby system a r e all unrelated t o t h e No. 3 generator i n t e r n s of cause. I n view of t h e foregoing, t h e Board believes there i s no b a s i s upon which t o recommend t h a t t h e MEL f o r t h e B-727 be revised t o require t h a t all t h r e e generators be operative. A t t h e sane time, we believe t h a t repairing components beyond those required by t h e MEL, as soon as p r a c t i cable,is consistent with sound maintenance and engineering practices. Furthermore, it can even be s a i d t h a t maintaining such components i n operating condition has t h e added e f f e c t of enhancing safety, inasmuch as it increases t h e available degree of redundancy. FinaUy, a b r i e f coment i s warranted concerning t h e o v e r a l l e l e c t r i c a l system on t h e B-727. Recommendations have been made and corrective measures adopted, as described hereinabove, t o correct those discrepancies and procedures uncovered during t h e investigation which might have contributed t o the accident. The Board believes t h a t these steps should go a long way toward preventing t h e occurrence of a similar accident. A t t h e same time, we recognize that e f f e c t i v e prevention i s l i m i t e d by t h e f a c t t h a t t h e lack of physical evidence has not allowed a conclusive determination of why t h e No. 2 generator was l o s t and why t h e standby system w a s not activated o r f a i l e d t o function. Our concern i n t h i s instance i s increased by t h e several incidents subsequent t o t h e accident involving l o s s of all t h r e e generators on B-727 a i r c r a f t . Despite t h e generally excellent performance history- of t h e B-'727' e l e c t r i c a l system, t h e p x s i b i l i t y remains, unless and u n t i l t h e reasons u n d e r w n g these - 33 power l o s s e s a r e determined, that a camon problem within t h e system i s responsible. Accordingly, t h e Board urges all B-727 operators t o be p r t i c u l a r l y thorough i n investigating any incidents of a s h i l a r nature i n order t h a t every possible e f f o r t be made t o uncover t h i s problem, should one e x i s t . BY THE NATIONAL TRANS PORTATION SAFETY BOARD : JOHN H. REED Chairman OSCAR M. LAUREL Member FRANCIS H. McAEfeMS Member LOUIS M. Member THAYER ISABEL A. BURGESS Member March 18, 1970 Intentionally Left Blank in Original Document Appendix A INVESTIGATION AND HEARING 1. Investigation The Board received o f f i c i a l n o t i f i c a t i o n of t h e accident a t approximately 2200 e.s.t., on January 18, 1969. An investigating team was dispatched from Washington, D. C., several hours t h e r e a f t e r and arrived i n Los Angeles i n t h e e a r l y morning hours of January 19. Upon a r r i v a l , working groups were established f o r Operations, Witnesses, Air T r a f f i c Control, Human Factors, Weather, Structures, Powerplants, Systems, Maintenance Records, Cockpit Voice Recorder, and Flight Recorder. P a r t i e s of I n t e r e s t p a r t i c i p a t i n g i n t h e investigation included t h e Federal Aviation Administration, United Air Lines, t h e Boeing Company, Air Line P i l o t s Association, P r a t t & Whitney Division of United Aircraft Corporation, and Professional Air Traffic Controllers Organization. Due t o t h e d i f f i c u l t i e s involved i n locating and recovering t h e wreckage, t h e on-scene investigation was not completed u n t i l March 19, 1969. The on-site i n v e s t i g a t i o n consisted b a s i c a l l y of four phases: ( a ) search f o r t h e wreckage, (b) i d e n t i f i c a t i o n and p l o t t i n g of wreckage, ( c ) recovery of p r i o r i t y items, and (d) recovery of remaining p a r t s of t h e wreckage. The wreckage w a s located on January 31, 1969, i n approximately 1,000 f e e t of water by a vessel equipped with side-looking sonar , The p l o t t i n g and i d e n t i f i c a t i o n of t h e wreckage was acequipnent. complished by t h i s same vessel u t i l i z i n g "J-Star" equipnent, which has both t e l e v i s i o n and sonar capability. The t h r e e engines were recovered on February 11, 1969, with t h e a s s i s t a n c e of t h i s equipnent o u t f i t t e d with a s p e c i a l clamp. The voice recorder, f l i g h t recorder,. smal1,engine components and some e l e c t r i c a l parts were recovered during t h e period February 21, 1969, through March 4, 1969, by a submersible vehicle. The f i n a l gross recovery phase was c a r r i e d out during t h e period March 6, 1969, through March 19, 1969,by means of a trawler, which involves dragging a net over t h e ocean f l o o r . 2. Hearing A public hearing was held at t h e Miramar Hotel i n Santa Monica, California, on August 13 t o 15, 1969. A preliminary aircraf't accident r e ~ r summarizing t t h e f a c t s disclosed by t h e investigation was published by t h e Board on June 9, 1969. A summary of t h e testimony which was taken at t h e public hearing w a s released on September 5, 1969. S a a z (sound navigation ranging) i s an apparatus which transmits highfrequency sound waves i n water and r e g i s t e r s t h e vibrations r e f l e c t e d back from an object . CREW IBFOBMATION Captain Leonard A. Leverson 2036 Victoria Drive Santa Ana, Calif. First Officer Walter R. Schlemmer 3131 Old Coach Drive Camarrillo, Calif. Second Officer Keith R. Ostrander 506 Dena Drive Newbury Bark, Calif. Certificates Held : ATR 470722 Class I Medical Dated 11/26/68 F/E Commercial 1582882 1601250 Class 11 1/29/68 F/E(S/O) Limitations: None None None Pilot Eatings : ASEL & MES & Instrument AMEL Total Time ( T.T.): 13,665 hours 6642 Pilot, 889 S/O T. T. in Type: 1,908 hours 1842 Pilot, T. T. Last 90 78 hours 200 hours 40 hours T. T. Last 90 Days in Type: 61 hours 200 hours 40 hours Rest Period 24 Hours Prior to Accident : 22.6 hours 22.6 hours Duty Time Last 24 Hours: 1.4 hours 1.4 hours 1.4 hours Time This Flight: .3 hours .3 hours .3 hours Address : Age: Hire kte: - - & Instrument Commercial 1711270 1812272 Class 11 9/13/68 - ASEL DC-6, B-727 174 Pilot, 460 S/O 543 S/O Days : APPENDIX c TRANSCFUFTION OF VOICE COMMOHICATIONS RECORDED OH THE LAST 2 MUTOTES AND 25 SECONDS OF THE CAM AND COPILOT'S RADIO CIRCUITS OF THE COCKPIT VOICE RECORDER TAPE FRCM UNITED AIR LIHES FLIGHT 266, N7434~,B-727, WHICH CRASHED INTO THE SEA. SHORTLY AFTER lAKEOFF FROM LOS ANGELES IHTERMATIONAL AIRPORT, LOS ANGELES, CALIPORHIA, ON J A I T O ' 18, 1969. Legend CAM - Cockpit area microphone circuit 1 - Voice identified as the Captain's 2 - Voice identified as the Copilot's KDO - TOE - Radio transmission from Los Angeles Tower's Local Control Position LAX DR - Radio transmission from Los Angeles Departure Radar % - Unrelated Radio Transmissions # Non-pertinent word or phrase (1 - --- - 3 Voice identified as the Engineer's Radio transmission from UAL 266 Words enclosed within parentheses are not clearly understood and are subject to interpretation. Those shown represent the Interpretations of what the speaker said. Series of flashes indicates a pause in a transmission. Transcript begins with flight's clearance for takeoff. When clearance is received, the aircraft is holding position for takeoff on Runway 24. Intentionally Left Blank in Original Document TIME - CORPEBT SOURCE 1816: 58 TWR 1817: 00 m United two s i x t y s i x cleared f o r takeoff 2 United two s i x s i x r o l l i n g :02 CAM1 last t h r e e items :05 CAM3 Engine start switches :06 CAM2 (Three on) :07 CAM3 Anti skid :10 CAM2 On (release) 1817:11 CAM? (yeah t h a t 1s good) CAM? O i l cooler (comin) ground off CAM? (You kicked o f f Dick?) CAM2 They're s t a b i l i z e d CAM1 Take off t h r u s t CAM2 Set CAM2 Looks good %%% CAM2 One hundred CAM2 One t e n CAM2 One twenty CAM2 VR CAM2 V2 CAM 1. Gear up CAM2 Gear up TWR United two s i x t y s i x contact departure control RDO2 Changing %%$ 1818: 09 CAM1 (YOUhandle t h e s e t h i n g s ) l i g h t on t h e c o n t r o l s CAM 2 Yeah CAM1 1818: 13 :1 5 CAM2 Five RID2 United two s i x s i x on departure LAXER United two s i x t y s i x Los Angeles departure c o n t r o l r a d a r contact, t u r n r i g h t heading two seven zero r e p o r t l e a v i n g t h r e e thousand EDO 2 Two seven zero wilco CAM1 You have a green two CAM2 Two CAM Sound of warning b e l l heard CAM2 ## CAM1 What t h e h e l l was t h a t ? CAM2 Number one f i r e warning, Arn CAM1 OK, l e t s t a k e c a r e of t h e CAM2 Pull it back f o r you? CAM1 Yeah, p u l l it back CAM 2 OK CAM Sound of warning horn heard CAM2 That p u t s u s on one CAM 1 Huh? CAM2 T h a t ' l l put u s on one generator CAM1 Yeah, watch t h a t e l e c t r i c a l loading CAM2 Everything o f f ? ## - - - - - warning generator t o o RDO 2 Ah-departure United two s i x s i x IAX VS. United two s i x t y s i x go ahead m Ah we've had a f i r e warning on number one engine, we shut down we'd l i k e t o come back 2 LAX TS. United two s i x t y s i x roger what i s your present altitude? CAM CTE operation stopped CAM GVB resumed operation a t an indeterminate l a t e r time CAM? Fields out CAM 3 We're gonna get screwed up CAM3 #, CAM2 Keep it going up Arnie you're a thousand f e e t CAM2 P u l l it up CAM End of recording. CVR ceased t o operate I don't know (what I s going on) Intentionally Left Blank in Original Document DarnDO CAM . CVR OPERATION RESUMED A 1 AN INOETERMINATE 11ME Darn.OO.5 CAM-? : FIELDS OUT Darn CAM 1 Darn A Darn-06 CAM-; 3 OOD008 CAM-2 OOOftOT CAM l n f f f , UA 266 WE'VE IIAO A FIRE WARNING ON WE SHUT NUMBER CUE EWINC DOWN Wf'O LIKE TO COME BACK Q SWEIPS 1 0 LOSS Of SICONDAtYl WE'RE GOING TO GET SCREWED UP . #, I D O N 1 KNOW W K A I ' S GOING ON1 : KEEP 17 GOING UP ARNIE YOll'RE A THOUSAND FEET PULL 1 1 U P . CVR OPtRAIIQN STOPPED 9 SECONDS AFTER RESUMPIION CAM7 18i8W C M ~ . t VthH. WATCH IHhI ILECIRCChL LOAOING 1 8 1 8 - y LOST PRIMARY TARGET--/ W 1818-48 CAM-? : THAT W I L L PUT US : EVERYTHING O M GENEHAIOR OFf lfll8.76.5 CAM I YOU HAVE A GREEN TWO 181/55 LC ? CUMIACI O I P A R l l l R l CONTROI E A R TURN RIGHI HEADING TWO SIX 1111 ZERO SIX ZERO à WRECUAGE SITE 33"56'56" H. na"39'30 w IHREI THOUSAND FIVE HUNDRED WHAT'S YOUR AIIITUDE NOW 1819-70 OS-7 8 : 5 !C-7 UNITED I W O SIXTY S I X CLIARIO FOR TAKEOH I f t l l E O TWO SIXTY SIX MAINTAIN THREE 1HOUSAHD AND SAY YOUR ALIITUDI UA 7 W W I T 1 0 W O 5 1 1 5 t X R N L I N G R18W CAM 1 . CAM 7 . VIA" . FLAPS . FIVI I 1818% CAM 7 . NUMBER O W FIRE WARNING, ARM . OK. LETS 1AKT CARE 01 II#E . . 1818-36 CAM 1 I8iRdO CAM 2 PULL IT BACK I O R YOU' 181842 CAM I YEAH PUH I T BACK CAM 2 OK CAM2 WARMNG (YOU HANOLE THESE [ I ( l N G S l I I G h l ON THE CONTROLS AH - F I V E . . ., 8 1 8 11 UA 266 UNIlTO ?0 S I X I Y SIX ON O I P A R I ~ I R I U M H D I W P SIXTY SIX tOS ANt.lE'i OS-2 O!PARIURE CUNIROI RADAR COMHCT 181821 UA-766 IURK RICH! HEADING 1AO SEVEN ZERO REPORI LEAVING THRTI THOUSAND [WO SEVEN ZERO WlLCO ' ' \ \ NATIONAL TRANSPORTATION SAFETY BOARD DEPARTMENT OF TRANSPORTATIOH Washington, D C , APPROXIMATE FLIGHT PATH CHART UAL 266. B-727. N7434U {BASED ON ATC Â¥N CVR 0 A H I ACCIDENT-APPRO< 11.3Ml WEST LOS ANGELES AIRPOR Ian. 18. 1 9 6 9 Intentionally Left Blank in Original Document
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